ML19332B000
| ML19332B000 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 09/02/1980 |
| From: | Connell C POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | |
| Shared Package | |
| ML093441508 | List: |
| References | |
| NUDOCS 8009190451 | |
| Download: ML19332B000 (6) | |
Text
y v-O OPEltAllNG DATA lili"DitT
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DOCKI-T NO.
50-7ff G DATE 9-2-80 COMPLETED isY
'C.
Conne_11 TELEPilONE (914? 739-0200 OPEf t ATING STATUS N0fC5 TmHan Point no. 3 Nuclear Power Plant
- 1. Unit Name:
August 1980
- 2. Iteporting Period:
- 3. Liecused Thennal Power (MW ):
__3025 1013
- 4. N~ueplate Rating (Gron MWel:
A9
- 5. Design Electrical Rating (Net MWel:
952
- 6. Maximum Dependable Capacity ICross MWe):
917
- 7. blaximum Dependable Capacity (Net MWe):
- 8. If Changes Occur in Capacity itatings (items Number 3 Through 7) Since Lsst Report.Give Reasons:
=
None
- 9. Power Level To Which Restricted.If Any (Net MWel:
N/A
- 10. Itessons For itestrictions.lf Any:
This Month Yr to-Dste Cumulative 744 5,855 35.112
- 11. !!ours In Reporting Period 738.6
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4,187.6 3 g,7 7., 3
- 12. Number Of Ilours itenctor was Critic.1 0
0 0
- 13. Reactor Resene Shutdown Hours 3,727.7 24,760.6 733.1
- 14. !!ours Cenerator On-Line 0
0 0
- 15. Unit Reserve Shutdown Hours 1,999,791 8,895,499 64,999,966 16.. Gross Thermal Ener;y Generated (MWil) 551,280 2,479,000 20,844,101
- 17. Cross Electrical Ener;:y Generated (MWill 2,355,181 19,998,618 526,916
- 18. Net Electrical Energy Generated (MWil),
70.5 98.5 63.7
- 19. Unit Service Factor 63.7 70.5 98.5
- 20. Unit Availability Factor 43.9 62.1 77.2
- 21. Unit Capacity Factor (U>in;: MDC Net) 41.7 59.0 73.4
'22. Unit Capacity Factor (Using DElt Net) 21.8 7.2
- 23. Unit Forevd Outage Itate 1.5
- 24. Shutdowm Scheduled Oser Next 6 Months (Type.Date.and Duration of Eacht:
Turbine Outage October 1980 N/A
- 25. If SImt Down At End of Iteport Period. Estimated Date of Startnp:
- 26. Units In 1rst Statm Irrior to Connnercial Operationi:
Forecast Achieved A
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50-286 UNITSilUTDOWNS AliD POWER REDUCTIONS DOCKET NO.
UNITN.O!E Indian Pt. No. 3 DATE 9-2-Ro REPORTMONT11_ August COMPLETED BY c ennn, n TELEril0NE (9141 739-8200 1
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Cause & Corrective No.
Date n.
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,gg5 Event u?
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5 l Ji 5 g Report 4.
@G gu Action to Prevent Recurrence u
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26 800812 F
3.2 A
3 HF PUMPXX-B Unit trip during rapid load reductior caused by loss of all circulatit.9 water.to #33 condenser bay when #36 circulating water pump tripped with
- 35 circulating water pump previously out of service for repairs.
Repaired pump.
27 800823 F
7.7 A
3 EB GENERA-E Unit thip while placing repaired motor generator. set in service.-
Malfunction with auto synchronizing device. Repaired auto synchronizing, device.
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F: Forced
' Reason:
Method:
Exhibit F -Instructions Q
S: Sch.duled
- A Equipment Failure (Explain)
- 1. Manual for Preparation of Data na B Maintenance or Test 2 Manual Scram.
Entry Sheets for Licensee W
C. Refueling 3 Automatic Scram.
. Event Report (LER) File (NUREG-M
- D Regulatory Restriction 4 Other (Explain) 016i)
E-Operator Training & License Examination k-F Administrative 5
G-Operational Error (Explain)
Exhibi.H Same Sourec (Q77)
Il Other (Explain)
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r-v AYl:l( AGE DAILY UNIT POWEl( I.I. VEL DOCKET NO. 2M Indian Point
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UNIT No.3
--0 DATE COMPLETED DY _ C. Connell TELEPllONE 914-739-8200
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MONTil DAY AVERAGE DAILY POWER LEVEL DAY AVER ACE DAILY POWER LEVEL (MWe Net)
(gwe.ge )
830
- 690 I
)y 2
787 33 690 3
782 19 715 4
725 801 2n 688 838 5
21
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6 689 842 22 273 7
23 3
726 711 24 735 9
25 845 10 767 26 847 848 11 27 849 12 469 28 834 698 815 13 79 14 721 810 3
15 717 844 3;
16 698 m
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INSTRUCTIONS l
On this format. list the average daily unit power levelin MWe. Net for cach day in the repurting inonth. Compute to the nearest whole rnegawatt.
.s (9/77)
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MOtiTilLY I & C CATEGORY I REPORT a
August, 1980 c
Month Da te W.R.
Equipment Malfunction Corrective Action 8/26/80 1C-1-763-3B I.E.O.P.S.
No output from 3 Spare Replaced detectors detectors 8/26/80 1C-1-791-lE
- 33 Inverter No output Replaced defective output filter capacitors & pre-charge circuit capacitors 8/26/80 1C-1-852-2
- 32 Chg. Pump I/P Defective Air Regulator Replaced Regulator SM-141P 8/26/80 1C-1-524-3D Gross Failed Fuel Sys.
Defective Gamma Detector Replaced Gamma Detector and Calibrated System.
8/26/80 1C-1-778-2 Vent Header Pressure Linkage disconnected Reinstated linkage Transmitter
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SUMMARY
OF OPERATING EXPERIENCE - AUGUST 1980 Indian Point Unit 3 was synchronized to the bus for a total of 733.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> producing a gross generation of 551,280 MWe for the reporting period.
During this period the unit experienced two plant trips.
On August 12 at 0945 hours0.0109 days <br />0.263 hours <br />0.00156 weeks <br />3.595725e-4 months <br /> the unit experienced a trip during a rapid load reduction caused by the loss of all circulating water to #33 condenser bay when #36 Circulating Water Pump tripped with #35 circulating water pump out of service for repairs. The unit was returned to service at 1259 hours0.0146 days <br />0.35 hours <br />0.00208 weeks <br />4.790495e-4 months <br /> on that same day.
Commenced load escalation consistent with circulating water pump capabilities.
On August.23 at 0316 hours0.00366 days <br />0.0878 hours <br />5.224868e-4 weeks <br />1.20238e-4 months <br /> the unit experienced a trip while piacing a repaired rod drive motor generator set into service. That same day at 1057 hours0.0122 days <br />0.294 hours <br />0.00175 weeks <br />4.021885e-4 months <br /> the unit was returned to service and commenced load escalation consistent with circulating water capabilities.
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