LER-1980-008, /01T-1:on 800225,during in-plant Insp,Potential Overstress Condition of Cable Spreading Room Floor Indicated Due to Postulated Seismic Loading.Caused by Utilizing Underside of Floor to Higher Degree than Original Design |
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4 Attachment To LER 80-08/01T-l' Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 During an in-plant inspection, it was noted that the underside of the service building floor at elevation 725 ft. 6 in, was utilized to provide support for conduit and cable trays to a higher degree than the original design anticipated.
As a result, an on-site reivew was made to determine the worst-case loading condition for the purpose of providing the basis of reanalysis. An area was investigated which was the most congested, and in which conduits and cable trays were supported in a manner which raised questions as to the adequacy of the light steel framing members. A preliminary simplified analysis indicated that, during a DBE event, the loads imposed by acceleration of cable trays and conduits
- - would overstress the structural steel beams when forces due to horizontal and vertical bending were combined together algebraically.
The floor support system was checked for the normal dead load, live load, and vertical earthquake component and was found satisfactory.
It was the imposition of forces due to the DBE horizontal acceleration of the conduits and tray supports which were attached to the lower flanges of the steel beams which caused beam local overstresses.
The analysis for the OBE condition indicated that although some beams were slightly over allowable stress, no major structural damage would occur during the shutdown condition.
This problem is limited to the cable spreading floor because no other, Category I area of the plant has this configuration of light framing beams (B Series) with similar imposed loading from conduits and cable trays.
Based on the initial analyses that were performed, Duquesne Light Company was advised of this problem by the architect-engineer on February 15, 1980.
LER 80-08/01T was submitted to the NRC, in accordance with 10 CFR 50.36, to report this condition. The approach taken to resolve this problem is as follows:
Due to the difficulties encountered in analytical modeling of the geometry of the cable tray, conduit, and their supports, it was decided to establish a conservative design criteria and. proceed with modifications rather than attempting further reanalysis. The effort was limited to ensuring the structural adequacy of steel beams supporting the floor, conduits, and cable trays below the floor. The N'
as-built configuration of cable trays, conduits, and supports was developed to provide input to the analysis which determined the necessary modifications required to limit-the combined stresses within allowable limits for the design conditions.'
The original design criteria, i.e., BVM-52, " Structural Design Criteria", governed the analysis and design.
Seismic forces imposed by cable trays and conduits were computed as static acceleration loads equal to 1.5 times the applicable peak
- - amplified resonant response, based on soil structure interaction, for the support elevation, using a value of four percent damping.
Four percent damping is acceptable according to Regulatory Guide 1.61 for bolted steel or reinforced concrete structures.
It should be noted that the 1.5 x p+ak is conservative and j
obviates the need for determining natural frequency characteristics of the system.
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Attachment To LER 80-03/OlT Page 2 Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 4
It was assumed that the top flanges of the beams are continuously supported and horizontal seismic loads in the slab and the top flanges are directly resisted by diaphragm action of the concrete slab.
Stresses due to horizontal and vertical bending of beams were combined algebraically.
Significant torsional stresses were taken into account. Any loadings from the floor above were uncoupled by modifying the connections of elements which frame to both floors.
Resultant combined stresses were limited to the allowable limits.
The modifications to the floor framing system consisted of providing lateral bracing to the bottom flanges of the floor framing beams where stresses were exceeding the allowable limits. The lateral loads were transferred to the nearest column or wall. The loads from cable trays on the floor above were disconnected and fully supported from elevation 735 ft. 6 in.
Necessary drawings and calculations for beam modifications were developed.
The service building floor at elevation 725 ft. 6 in. has been modified so that the load carrying capacity is satisfactory for the design seismic loadings.
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| 05000334/LER-1980-001-01, /01T-1:on 870626,discovered That Suction Piping on Vacuum Pump Not Adequately Supported for Seismic Event. Caused by Inaccurate Computer Code Used.Seismically Inadequate Piping Isolated & Support Added | /01T-1:on 870626,discovered That Suction Piping on Vacuum Pump Not Adequately Supported for Seismic Event. 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Caused by Leaking Effluent Valves.Corrective Actions Scheduled to Be Completed as Soon as Possible | /03L-0:on 800422,pump Being Used to Start Liquid Waste Discharge Observed to Have Higher than Normal Flow. Caused by Leaking Effluent Valves.Corrective Actions Scheduled to Be Completed as Soon as Possible | | | 05000334/LER-1980-027-03, During Maint of Diesel Generator Lube Oil Cooler,Internals of River Water Check Valve Discovered in Cooler.Caused by Flutter Due to High Flow Conditions Eroding Hinge Pin Guide.Valve Replaced | During Maint of Diesel Generator Lube Oil Cooler,Internals of River Water Check Valve Discovered in Cooler.Caused by Flutter Due to High Flow Conditions Eroding Hinge Pin Guide.Valve Replaced | | | 05000334/LER-1980-027, Forwards Updated LER 80-027/03L-1 | Forwards Updated LER 80-027/03L-1 | | | 05000334/LER-1980-028-03, /03L-0:on 800504,power Was Lost to Vital Bus Inverter 4 Due to Blown Main Power Supply Fuse.Cause Unknown.Fuse & Rectifier Replaced.Frequency Adjusted | /03L-0:on 800504,power Was Lost to Vital Bus Inverter 4 Due to Blown Main Power Supply Fuse.Cause Unknown.Fuse & Rectifier Replaced.Frequency Adjusted | | | 05000334/LER-1980-029, Forwards LER 80-029/03L-0 | Forwards LER 80-029/03L-0 | | | 05000334/LER-1980-029-03, /03L-0:on 800409,during Performance of Containment Isolation Check Valves Test,Found Safety Injection Accumulator Fill Line Check Valve Opened Beyond Limits of Tech Spec.Cause Under Investigation | /03L-0:on 800409,during Performance of Containment Isolation Check Valves Test,Found Safety Injection Accumulator Fill Line Check Valve Opened Beyond Limits of Tech Spec.Cause Under Investigation | | | 05000334/LER-1980-030-01, /01T-0:on 800519,plant Operators Testing diesel- Driven Fire Pump When High Temp Alarm Was Received & Diesel Overheated.Caused by Brittle Fan Belt Slipping | /01T-0:on 800519,plant Operators Testing diesel- Driven Fire Pump When High Temp Alarm Was Received & Diesel Overheated.Caused by Brittle Fan Belt Slipping | | | 05000334/LER-1980-031-01, /01T-0:on 800521,upon Finding Leaking RHR Sys Vent Valve Weld,Evaluation Commenced to re-energize RHR Isolation Valve in Case of Gross Failure.Caused by de-energized Process Control Signal & Vent Weld Leak | /01T-0:on 800521,upon Finding Leaking RHR Sys Vent Valve Weld,Evaluation Commenced to re-energize RHR Isolation Valve in Case of Gross Failure.Caused by de-energized Process Control Signal & Vent Weld Leak | | | 05000334/LER-1980-031, Forwards LER 80-031/01T-0 | Forwards LER 80-031/01T-0 | | | 05000334/LER-1980-032-03, /03L-0:on 800503,during Control Board Insp,Vol Control Tank Outlet Valve Was Found Shut.Caused by Short Circuited Lead in Level Comparator.Shorted Wire Replaced | /03L-0:on 800503,during Control Board Insp,Vol Control Tank Outlet Valve Was Found Shut.Caused by Short Circuited Lead in Level Comparator.Shorted Wire Replaced | | | 05000334/LER-1980-033, Forwards LER 80-033/03L-0 | Forwards LER 80-033/03L-0 | | | 05000334/LER-1980-033-03, /03L-0:on 800617,diesel Generator 1 Governor Control Motor Failed.Caused by Cycling of Governor While Attempting to Shut Down Diesel W/Fast Start Signal Still Applied.Motor Replaced | /03L-0:on 800617,diesel Generator 1 Governor Control Motor Failed.Caused by Cycling of Governor While Attempting to Shut Down Diesel W/Fast Start Signal Still Applied.Motor Replaced | | | 05000334/LER-1980-034-03, /03L-0:on 800512,during Air Flow Surveillance Test on Fire Suppression Sys,Approx 50% of Sprinkler Nozzles Found Plugged.Caused by Rust & Unidentified Matl.Nozzles Will Be Cleaned & Sys Blown Down W/Air | /03L-0:on 800512,during Air Flow Surveillance Test on Fire Suppression Sys,Approx 50% of Sprinkler Nozzles Found Plugged.Caused by Rust & Unidentified Matl.Nozzles Will Be Cleaned & Sys Blown Down W/Air | |
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