05000318/LER-1980-008-03, /03L-0:on 800125,containment Spray Header 22 Was Isolated.Caused by Need to Repair Shutdown Heat Exchanger Inlet Cross Connect Valve.New Packing Installed

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/03L-0:on 800125,containment Spray Header 22 Was Isolated.Caused by Need to Repair Shutdown Heat Exchanger Inlet Cross Connect Valve.New Packing Installed
ML19330C366
Person / Time
Site: Calvert Cliffs 
Issue date: 02/25/1980
From: Heibel R, Pence W
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19330C362 List:
References
LER-80-008-03L-01, LER-80-8-3L-1, NUDOCS 8008080287
Download: ML19330C366 (1)


LER-1980-008, /03L-0:on 800125,containment Spray Header 22 Was Isolated.Caused by Need to Repair Shutdown Heat Exchanger Inlet Cross Connect Valve.New Packing Installed
Event date:
Report date:
3181980008R03 - NRC Website

text

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7 8 9 LICENSEE CODE 14 15 LICENSE NUVSER 26 26 LICENSE TYPE Jo 57 CAT $8 CON'T

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- 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 1012] I o facilitate repairs to #22 Shutdown Coolina Heat Exchanaer Inlet -

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g ; Cross Connect Valve, it was necessary to isolate #22 Containment Spray i

10141IHeader.~ The Containment Spray Header was isolated from 0810 to 1230.

Durino I

i O i s ! l this event #21 Spray Header remained operable as recuired by T.S. 3.6.2.1.

I IOisi IThis is not a repetitive occurrence.

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9 10 11 12 13 18 19 20 SE QUENTI AL OCCURAENCE REPORT REVISION LER EVENT YE AR REPORT NO.

CODE TYPE NO.

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33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTloNS h l

li 101 IThe old packino was removed and found to be dry and hard from ace I

l7 ;T1 land lost its compressibility. flew packing was installed and the valve i

li 121 Iwas returned to operation with no leakace detected.

Use of alternate I

ii 3l l packing materials less susceptible to age hardening are being investicated.

I 11 1411 I

'* 'US STa sPOWER OTHER STATUS ISCO Y

DISCOVERY DESCRIPTION IiIsI (EJ @ ll 10 10 l @ l flA l

lAl@l Ocerator Observation l

ACTIVt TY CO TENT RELEASE AMOUNT OF ACTivlTY LOCATION OF RELEASE l i l 6 l W @D OF RELEASE [Z_j@l ttA l

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7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUP.*B E R TYPE

DESCRIPTION

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DESCRIPTION

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R. P. Heibel/W. B. Pence (301)269 4743/4815 E,

NA?.*E OF PREPARER pga.a g m --

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LER NO. 08/3L

' DOCKET NO.

50-318 EVENT DATE 01/25/80 REPORT DATE 02/25/80 ATTACHMENT,

CAUSE DESCRIPTION AND CCRRECTIVE ACTICHS:

(C0flTIrlUED)

In the interim, System Integrity Testing conducted per the requirements of MUREG 0578 will ensure that small packing leaks such as this are promptly identified and corrected.

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