|
---|
Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With ML20151V2811998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Tmi,Unit 1.With ML20237C6411998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Tmi,Unit 1 ML20236R2201998-06-30030 June 1998 Monthly Operating Rept for June 1998 for TMI-1 ML20249A1061998-05-31031 May 1998 Monthly Operating Rept for May 1998 for TMI-1 ML20247G0761998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Three Mile Island Nuclear Station,Unit 1 ML20216K1061998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Three Mile Island Nuclear Station,Unit 1 ML20216F0981998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Three Mile Island Nuclear Station,Unit 1 ML20202F8121998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for TMI Nuclear Station, Unit 1 ML20199J3251997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Three Mile Island Nuclear Station,Unit 1 ML20203K4081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for TMI-1 ML20199E3401997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for TMI-1 ML20198J8121997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for TMI-1 ML20217A8761997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for TMI-1 ML20210K0331997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Three Mile Island, Unit 1 ML20196G8401997-06-30030 June 1997 Monthly Operating Rept for June 1997 for TMI-1 ML20210K0401997-06-30030 June 1997 Revised App B of Monthly Operating Rept for June 1997 for Three Mile Island,Unit 1 Correcting Calculational Error in Shutdown Duration Hours Value ML20141C6521997-05-31031 May 1997 Monthly Operating Rept for May 1997 for TMI-1 ML20141G2801997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for TMI-1 ML20140D6601997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Three Mile Island, Unit 1 ML20136G3891997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Three Mile Island Nuclear Station,Unit 1 ML20134Q2071997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for TMI-1 ML20133G8231996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for TMI-1 ML20132D5431996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Three Mile Island Nuclear Station,Unit 1 (TMI-1) ML20135A8291996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for TMI-1 ML20129B6621996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Three Mile Island Nuclear Station Unit 1 (TMI-1) ML20129C2661996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Three Mile Island Nuclear Station,Unit 1 ML20116N6571996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Three Mile Island Nuclear Station,Unit 1 ML20115E2071996-06-30030 June 1996 Monthly Operating Rept for June 1996 for TMI-1 ML20117M1581996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Three Mile Island Unit 1 ML20112A2171996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Three Mile Island Nuclear Station Unit 1 ML20117D3691996-03-31031 March 1996 Monthly Operating Rept for March 1996 for TMI-1 ML20101C6811996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Three Mile Island Nuclear Station,Unit I ML20149K7551996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for TMI-1 ML20096D5781995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for TMI Nuclear Station ML20095E0521995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for TMI-1 ML20094L7651995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for TMI-1 ML20093E6731995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for TMI-1 ML20092F4401995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for TMI-1 ML20086F5021995-06-30030 June 1995 Monthly Operating Rept for June 1995 for TMI Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G1001999-10-14014 October 1999 Errata to Safety Evaluation Supporting Amend 215 to FOL DPR-50.Credit Given for Delay in ECCS Leakage ML20217K4701999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for TMI-1.With ML20216F9231999-09-22022 September 1999 Safety Evaluation Supporting Amend 216 to License DPR-50 05000289/LER-1999-010, :on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With1999-09-21021 September 1999
- on 990830,discovery of Condition Outside UFSAR Design Basis for Flood Protection Was Noted.Caused Because Original Problem Was Not Corrected by Design Change.Flood Procedure Was Immediately Revised.With
ML20211H5111999-08-31031 August 1999 Non-proprietary Rev 1 to MPR-1820(NP), TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis ML20211Q3551999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Tmi,Unit 1.With ML20211E8731999-08-24024 August 1999 Safety Evaluation Supporting Amend 215 to License DPR-50 ML20211B1931999-08-19019 August 1999 Safety Evaluation Supporting Amend 214 to License DPR-50 ML20210R4791999-08-13013 August 1999 Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2 ML20210U4791999-07-31031 July 1999 Monthly Operating Rept for July 1999 for TMI-1.With 05000289/LER-1999-009, :on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced1999-07-22022 July 1999
- on 990626,automatic Start of EDG 1A Occurred. Caused by Failure of Fault Pressure Relay on Auxiliary Transformer 1B.Failed Pressure Relay Has Been Replaced
ML20210K7651999-07-0909 July 1999 Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp Loca ML20209G0011999-07-0909 July 1999 Staff Evaluation of Individual Plant Exam of External Events Submittal on Plant,Unit 1 ML20209H8251999-07-0101 July 1999 Provides Commission with Evaluation of & Recommendations for Improvement in Processes Used in Staff Review & Approval of Applications for Transfer of Operating Licenses of TMI-1 & Pilgrim Station ML20209H1421999-06-30030 June 1999 Monthly Operating Rept for June 1999 for TMI-1.With ML20212H9101999-06-21021 June 1999 Safety Evaluation Supporting Amend 212 to License DPR-50 05000289/LER-1999-007, :on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed1999-06-18018 June 1999
- on 990528,increasing Failure Rate of ESAS Relays Characterized by Coil Overheating & Failing to Fully re-close After Being de-energized Was Discovered.Cause Indeterminate.Relay Check Procedure Has Been Changed
ML20195J9401999-06-15015 June 1999 Safety Evaluation Supporting Amend 211 to License DPR-50 05000289/LER-1999-005, :on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With1999-06-14014 June 1999
- on 990514,open Flood Path Between Turbine Bldg & Control Bldg Was Noted.Caused by Failure to Recognize That Mods Affected Flood Protection.Revised Flood Procedures.With
ML20195H0751999-06-0808 June 1999 Drill 9904, 1999 Biennial Exercise for Three Mile Island ML20195H9261999-05-31031 May 1999 Monthly Operating Rept for May 1999 for TMI-1.With ML20209G0351999-05-31031 May 1999 TER on Review of TMI-1 IPEEE Submittal on High Winds,Floods & Other External Events (Hfo) ML20207B6621999-05-27027 May 1999 SER Finding That Licensee Established Acceptable Program to Periodically Verify design-basis Capability of safety-related MOVs at TMI-1 & That Util Adequately Addressed Actions Required in GL 96-05 05000289/LER-1999-003-01, :on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open1999-05-0707 May 1999
- on 990310,discovered Failure of Manual Balancing Damper in Supply Duct of Control Bldg Evs.Caused by Failure to Adequately Review Risk & Consequences of Change.Failed Damper Was Clamped Open
ML20206R0571999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Tmi,Unit 1.With ML20206D4201999-04-20020 April 1999 Safety Evaluation Granting Exemption from Technical Requirements of 10CFR50,App R,Section III.G.2.c for Fire Areas/Zones AB-FZ-4,CB-FA-1,FH-FZ-1,FH-FZ-6,FH-FZ-6, IPSH-FZ-1,IPSH-FZ-2,AB-FZ-3,AB-FZ-5,AB-FZ-7 & FH-FZ-2 ML20205Q6111999-04-15015 April 1999 Safety Evaluation Supporting Amend 210 to License DPR-50 ML20205Q5981999-04-13013 April 1999 Safety Evaluation Supporting Amend 209 to License DPR-50 ML20206P2841999-04-12012 April 1999 SER Approving Transfer of License for Tmi,Unit 1,held by Gpu Nuclear,Inc to Amergen Energy Co,Llc & Conforming Amend, Per 10CFR50.80 & 50.90 ML20209G0071999-03-31031 March 1999 Submittal-Only Screening Review of Three Mile Island,Unit 1 Individual Plant Exam for External Events (Seismic Portion) ML20205K6851999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Tmi,Unit 1.With 05000289/LER-1999-002, :on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With1999-03-14014 March 1999
- on 990212,potential Failure of Multiple Containment Monitoring Sys CIV (CM-V-1,2,3 & 4) Was Noted. Caused by Inappropriate Use of Vendor Info.Personnel Will Be Trained on Mgt Expectations.With
ML20210C0161999-03-0101 March 1999 Forwards Corrected Pp 3 of SECY-98-252.Correction Makes Changes to Footnote 3 as Directed by SRM on SECY-98-246 ML20207M8461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for TMI-1.With 05000289/LER-1999-001-01, :on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys1999-02-19019 February 1999
- on 990122,short Sections of Piping Caused by Misplacement of Sensing Elements & Insulation.Caused by Failure to Adhere to Vendor instruction.Re-installed Heat Trace Sys
ML20196K3561999-01-22022 January 1999 Safety Evaluation Concluding That Although Original Licensee Thermal Model Was Unacceptable for Ampacity Derating Assessments Revised Model Identified in 970624 Submittal Acceptable for Installed Electrical Raceway Ampacity Limits 05000289/LER-1998-014-01, :on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With1999-01-11011 January 1999
- on 981210,missed TS Surveillance Was Noted. Caused by Human Error.Absolute & Relative Control Rod Positions Were Obtained Immediately & Verified to Agree within Required Range.With
ML20196G4661998-12-31031 December 1998 British Energy Annual Rept & Accounts 1997/98. Prospectus of British Energy Share Offer Encl ML20207A9291998-12-31031 December 1998 1998 Annual Rept for TMI-1 & TMI-2 ML20196F6861998-12-0202 December 1998 Safety Evaluation Accepting Licensee Second 10-yr Interval ISI Program Plan Request for Alternative to ASME B&PV Code Section XI Requirements Re Actions to Be Taken Upon Detecting Leakage at Bolted Connection ML20198B8641998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for TMI-1.With ML20195C6921998-11-12012 November 1998 Safety Evaluation Supporting Amend 52 to License DPR-73 ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20196B7191998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for TMI-1.With ML20203G1211998-10-30030 October 1998 Informs Commission About Staff Preliminary Views Concerning Whether Proposed Purchase of TMI-1,by Amergen,Inc,Would Cause Commission to Know or Have Reason to Believe That License for TMI-1 Would Be Controlled by Foreign Govt 05000289/LER-1998-013, :on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance1998-10-15015 October 1998
- on 980916,failure to Perform Fire Protection Program Surveillances at Required Frequency Was Noted.Caused by Changes Not Being Made to Surveillance Schedule.Performed Missed Insp Surveillance
ML20155E7511998-10-15015 October 1998 Rev 1 to Form NIS-1 Owners Data Rept for Isi,Rept on 1997 Outage 12R EC Exams of TMI-1 OTSG Tubing 05000289/LER-1998-010-01, :on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued1998-10-0909 October 1998
- on 980825,potential Violation of Design Criteria During Single Auxiliary Transformer Operation Occurred.Caused by Failure to Adequately Define Job Performance Stds.Temporary Change Notice Issued
ML20154L5541998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for TMI Unit 1.With 05000289/LER-1998-011, :on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge1998-09-23023 September 1998
- on 980825,Thermo-Lag Fire Barrier Was Found Installed Outside Approved Joint Design Arrangement.Caused by Personnel Error.Initiated Continuous Fire Watch & Installed Trowel Grade Thermo-Lag in Void & on Outer Edge
1999-09-30
[Table view] |
Text
.
OPERATING
SUMMARY
) 315' 2" Icvel range.
On May 30, 1980, the Reactor Coolant System was drained to the 314' 10" to
(
This level is 51 to 56 inches above the top of the core.
The drain down was made to enable the following work:
1.
High Pressure Injection cross tie (Restart Modification RM-14).
2.
Examination of various primary system check valves performed as a result of IE Circular 78-15 (also see TMI-I LER 80-03).
While in this condition, several precautions were taken to ensure adequate core cooling:
1.
Actual icvel indication of each loop was monitored using tygon tubing.
2.
Both decay heat loops have remained operable while drained down.
3.
Special operating procedures instituted for reinitiating decay heat removal in the event level would go below the decay heat removal line tie-ins.
On June 27, 1980, a spill occurred in the TMI-I Reactor Building as a result of an inadvertant actuation of the Emergency Safety Actuation System. The actuation occurred when vital bus A was reenergized following a transfer of the inverters-This opened valve DH-VSA allowing bor'ted water to enter the Reactor Coolant System (RCS).
The additional water caused the RCS level to increase to the point where primary coolant spilled through open manways in the Once Through Steam Generators. The total volume of the spill was approximately 10,000 gallons. There were no over exposures or contaminated individuals and air sample activities less than maximum permissible concen-trations.
The spill area was promptly decontaminated and normal activities in the Reactor Building resumed.
MAJOR SAFETY RELATED MAINTENANCE While the Unit remained in cold shutdown, with restart modifications in progress, the following major maintenance was performed:
1.
The Emergency Diesel Generator (EG-Y-1A) inspection and repairs were performed with satisfactory results. Tech Spec Surveillance 1301-8.2 was performed as the inspection item.
Repair included inspection and repair of Cenerator bearing and insulating; replaced turbocharger gaskets; replaced ex-pansion joint gaskets; repaired water bypass fittings; repair plenum; and painted muffler.
This work was performed with the "B" Decay heat loop service.
2.
Eddy Current testing of the B OTSG was performed during June.
Setup work included:
a)
Building clean room around upper and lower primary side manways.
b) Removal of upper handhole and manucy c) Building eddy current test platform for test equipment.
d) Service (breathing air supply, electrical, lighting).
3.
The pressurizer code safety valve (RC-RV-1B) was removed from the pressurizer for Tech Spec Surveillance testing. Testing and reinstalling valve back on pressurizer is expected to ocent in July.
After the valve was removed, a cover was installed ove; obe open pipe.
)
8007290
4.
RM-14, High Pressure Injection Cross-Connect - prefabrication work was performed prior to draining the RCS down.
Work performed during the drain down included:
a) cutting pipe b) pipe preparation c) fitup of pipe d) hot / root pass e) information x-ray of hot / root pass f) hot / root pass repair as required g) weld out of weld h) final x-ray 1) flush of piping The x-rays and flushing were perforned wit".. satisfactory results.
5.
Stop Check Valve Inspections - (Ref:
IE Circular 78-15 and LER 80-03).
The High Pressure Injection valves (MU-V-101 A/B/C/D; MU-V-86 A/B; MU-V-94, 95) work included:
a) Removing bonnet b) internal inspection / measurements c) remove internals for modification d) bonnets reinstalled for raising of RCS IcVel During the inspection, measutement and modification of the internals, it was determined that new internals were required to properly repair the check valves.
Because of plant conditions and the mode of operation, it was determined to re-install the bonnets at this time to raise RCS level and install new internals later this year (projected date of August,1980).
The Decay Heat stop check valves (DH-V-22 A/B work was also performed on one (1) valve at a time with the valve retest being performed prior to removing the other valve. Work included:
4 a) removing bonnet b) inspection / measurements of valve internals c) removal of valve internals d) modify valve internal (hinge pin and lock device) e)
reinstalling valve internals f) inspection g) reinstall valve bonnet All work was performed with satisfactory results and with one (1) operable decay heat loop in operation.
6.
The Borated Water Storage Tank (BWST) 24" flange work included:
replacing existing bolts - one at a time; and reinjecting furmanite to stop leak. -Repairs were performcd with satisfactory results.
OPERATING DATA REPORT DOCKET NO.
50-289
"'Y
' I980 DATE COMPLETED 11Y
...D. G v t tchel1 TELEPHONE (215) 921-6579 Ol'El(ATING STATUS Three Mile Island Nuclear Station. Unit I
- 1. Unit Name:
3""" l980
- 2. Iteporting Period:
2515
- 3. Licensed Thermal Power (MWI1:
871
- 4. Nameplate Rating (Gross MWe):
819
- 5. Design Electrical Rating (Net MWel:
840
- h. Masimum Dependable Capacity (Grou MWe).. 776
- 7. Masimum Dependable Capacity (Net MWe):
- h. If Changes Occur in Capacity Ratings (Items Number 31hrough 7i Since Last Report.Gise Reasons:
- 9. Power Lesel To which Restricted lf Any(Net MWes:
I
- 10. Reasons For Restrictions.lf Any:
This Month Yr to-Date Cumularise 720.0 436 7.0 s1006.0
- 11. Hours in Reporting Period 0.0 0.0 31731,8
- 12. Number Of Hours Reactor Was Critical 0.0 0.0 839,5
- 13. Reactor Reserse Shutdown Hours U.0 0.0 31180.9
- 14. Ilours Generator On.Line 0.0 0.0 0.0
- 15. Unis Rewrve Shutdown Hour,
- 16. Grow Thermal Energy Generated IMWil
[1. 0 0.0 76b110'il.
O.
u.
O.
17
(, row Electrical Energy Generated (MWill u.
2384003T.
Ih. Net Electrical Energy Generated (MWil)
U.0 0.0 g,,g
- 19. Unit Service Factor
_070 u,o 7,
- 20. Unit Asailability Factor 0.0 0.0 59,3
- 21. Unit Capacity Factor iJsing MDC Net 1 0.0 0.0 57.0
- 22. Unit Capacity Factor (Using DER Neil 100.0 100.0 28.6
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Oser Nest 6 Months (Type.Date,and Duration of Eacht:
- 25. If Shut Demn At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior o Commercial Operations:
Forecast Achiesed INITIA L CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPER ATION tu/7" s n.
AVER AGL 0411T trN1g POhER LEVEL DOCKET NO.
50-289 TMI-I S'IT DATE I"I.V_ Ij, 1980 COMPLETED BY D-G. Mitcliell TELEPHONE (215) 921-6579 MONTH lune 1980 DAY AVER AGE DAll P
'ER LEVEL 1)W AVER AGE DAILY POWER LEVEL (MWe-Net i I
O I7 0
0 0
33 l
o 3
0 0
4 0
20 0
5 0
0 6
0 22 7
0 O
0 0
x 0
25 0
0 10 0
0 33 27 0
p-2h 0
33 29 0
I4 -
30 0
0 15 31 0
.i 0
is 9
y e
50-289 DOCKET NO.
UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT N A\\lE Dil-1 iulv 15. loso DATE COMPLETED BY D. C Mitcholl REPORT MONTH June 1980 TELEPHONE (215) 921-6579 "5
C
~;
e es 24
Cause & Correctise
.i ?
g 3sx Licensee j e, g
N...
Date
(
4 2sE Event g?
['8 A~
Action to
-=
$5 E'
j di, g Report e mO Present Recurrence H
d ep a y estraint Order 1
6/1/80 F
720 D
1 i
2 3
4 F: Forced Reason:
Method:
Edubit G Instructions 5: Scheduled A Equipment Failure (Explain) 1 Manual for Preparation of Data B-Maintenance of Test 2 Manual Seram.
Entry Sheets fe Licensee C-Refueling
.t-Autonuti. Scram.
E-ent Repart (LERI File int:RLG-D-Regulatory Restriction 4-Other ( E splain) 016!i E Operator Training 1 Licente i sami:ution F-Administrati.e 5
G-Operational Error (Esplain t Esh. bit ! Sam S urce Il Other (Esplain t
- a *. 'd REFUELING INF0,lptATijoN_ REOUEST 1.
Name of Facility:
Three Mlle Island Nuclear Station, Unit I 2.
Scheduled date for next refueling shutdown:
Unknown 3.
Scheduled date for restart followinn refueling:
Unknown 4.
Will refueling or resumption of operatiam thereaf ter require a technical k.,
specification change or other license amendment?
If answer 18 yes, in general, what will these be?
If answer is no, has the reload fuel design and core configuration been reviewed by your plant Safety Keview Conanittee to determine whether any unreviewed safety questions are associated with the core reload (Ref. 10 CFR Section 50.59)?
If no such review has taken place, when is it scheduled?
Amendment No. 50, Cycle 5 reinau, was approved on 3-16-79.
5.
Scheduled date (s) for submit ting proposed licensing action and support ing information:
N/A 6.
Important licensing considerations associated with refueling, e.g. new or different fuel design er supplier, unreviewed design or performance analysis methods, significant channes in fuel design, new operating procedurca:
N/A 7.
The number of fuel assemblies (a) in the core, and (b) in the spent fuel l
storage pool:
(a) 177 (b) 208 8.
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is i
planned, in number of fuel assemblies:
The present licensed capacity is 752.
There are no planned increases at this time.
9.
The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
1986 is the last refueling discharge which allows full core off-load i
capacity (177 fuel assemblies).
h-i