ML19329F924
| ML19329F924 | |
| Person / Time | |
|---|---|
| Site: | Hatch |
| Issue date: | 07/02/1980 |
| From: | Manry M GEORGIA POWER CO. |
| To: | |
| References | |
| IEB-79-14, NUDOCS 8007110368 | |
| Download: ML19329F924 (2) | |
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SUBJECT:
Hatch Unit 1, Docket No. 50-321 Notification of j d. Reportable occurrence No. 50-321/1980-076. Y' // NOTIFIED: Mr. Pete Taylor l DATE: 7-2-80 .I. DATE: 7-2-80 TIME: 2:35 EDST ,f DESCRIPTIDH OF Rt. PORTABLE OCCURRENCE Initial Cendition TEc Unit I reactor was in hot standby for the HPCI/RCIC i investigation and repair effort when the site engineering ) staff was n o t. I f i e d that the axial supports for the 20" line between the 1E11-F006A-D valves are inadequate. b Nature of Occurrence { CIIIl c reviewing the as-builts submitted for the IE Bulletin e' 79-14 program the AE discovered that hangers IE11-RRRH-196 and i 1 Ell-bHRH-313 would not adequately support their loads during ) a design bases earthquake. The AE then informed the site of k this problem per PDCR 52M-054. \\ Iceediate Corrective Action
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A design change request is being written to have the PDCR 4 implemented. These supports #111 be modified prior to the (o unit coming on line. Cause 3' The apparent cause is due to' a faulty design in which
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incorrect valve weights were used 'in t i. s original computer analysia. }** Supplemental Corrective Action p'. - Status of Redundant is t MA . f-S a cicup S y s t. e m s jy Eutdown cooling is not required and is not inoperable at this ,'g,y- , inoperable. time. LPCI, core spray, ADS, and RCIC are operable. EPCI is /
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D.f lapact to Other' Unit . Indicate any }. l - He IE Bulletin as-Duilt review did not 'roblems p for the stallar supporte on the Un i t. 2 RER system. g 8007110 3W 5 j l l
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