ML19329F884

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RO 50-321/1980-069:on 800626,following Auto Initiation Signal,Hpci Failed to Inject to Reactor Pressure Vessel Due to Isolating on Steam Line High Dp Isolation Signal.Cause Under Investigation.Reset Isolation & Opened Inboard Valve
ML19329F884
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 06/27/1980
From: Manry M
GEORGIA POWER CO.
To:
References
NUDOCS 8007110307
Download: ML19329F884 (1)


Text

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Dirsctor Deputy Director Ass't to Director Of it.'.'. I. C Y, G E O P. C I A 31513 Admin. Officer I '. ' " ' '. J C:'W T.

D'RCILLY RONS Chief U ': 1 17. D S I /. I i : liU C L ct.R REGULAICP.Y COMffISS10Il RCES Chief D I M E C'I U S Or IiSPECIIOri ATID E t!T O R C E M E IIT tu t. I c ; IJ FFMS Chief SUllE 3100 Sygds Chief l 'I l !:nRI C I'I A S T R EF. T P A 0fficer AI L A:;1 A. U E C P.G I A 30303 Esgcy Officer A k.h5u h S U h.!I.L l'*

ll a t c h Unit 1.

Docket Ho.

50-321, Notification of krportable occurrence lio. 50-371/1980-069.

NOTIFIED: Mr.

C.

A.

Julian P4IE:

6-27-80 DATE: 6-26-80 TIME: 4: 15 PM D b C?l r I I C':

CT REPUI11ADLE OCCURREt;CE Initin1 Ce n -l i t.i o n Et n tor

r : -. iren turbinc atop velve fast closure f o l l o w i n s:

Lumbint trip nt 6: 50 CDT, 6/26/80.

fi, t v r e of Occurrt. nee

!! I C I ~ 'i U T e 4 to injcct to the RTV following an auto initiation signal dJe to isolating on a steen line high DP isolation

? c,., 1 I t:;diotr U c' r r r e t i v e Action E.Es c t isoldtion opened inboard isolation velve and outboard v-Ive received anoth*r steos line h i p, h DP isolation signal.

Mt set the i.s : l a t i o n, opened the isolation valves and HPCI auto i n i t i s t r,.!

AnI injected to the RPV and was used to centrol t c u t. L o r v., t e r icycl.

C.- s c c IITIEtion due to steam linc high DP cause of the high DP

'ir,,)

5r not yct been determined.

Suppic catal Corrective Action TF c., u c ci the s t c a --

line high DP signal is under invcstigstion.

S t s-L '.' s ef R e d ie n d i n t or Backup Systecs n D.,. Gote Sptay. and LFhi~ were operable.

RCIC was inoperable.

Irpart to Other Unit N :: n c.

l Justification for Continued Operation i t s t i n f ~E I'llIT I will be periorm2d a i. rated conditions prior to ge l c. ; i n s; the g r. n e r a t o r back on line.

8.*.dar y j Plant Manager

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