ML19329A685

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RO 287/76-15:on 760911,incorrect Power Level Indication on Thermal Power Best Computer Point.Caused by Incorrect Data Value Storage within Program.Present Software Controls Evaluated & Appropriate Administrative Policies Implemented
ML19329A685
Person / Time
Site: Oconee 
Issue date: 09/27/1976
From:
DUKE POWER CO.
To:
Shared Package
ML19329A679 List:
References
RO-287-76-15, NUDOCS 8001090670
Download: ML19329A685 (1)


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Oconee Unit 3 Report No: 50-287/76-15 Report Date: September 27, 1976 Occurrence Date: September 11, 1976 Facility: Oconee Unit 3, Seneca, South Carolina Identification of Occurrence:

Incorrect " thermal power best" valve resulting from erroneous data input to Core Thermal Power Analysis Program Conditions Prior to Occurrence: Unit at 53% full power Description of Occurrence:

On September 11, 1976, it was discovered that on September 10, 1976, a data val,ue had been incorrectly input into the Core Thermal Power Analysis (CTPA) program on the Oconee Unit 3 computer.

As a result, for approximately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br />, the " thermal power best" computer point, a determination of the reactor power calculated from primary and secondary system heat balances, indicated a power level of 44% full power rather than the correct value of 53% full power.

Upon discovery of this error the computer program was corrected and the power range out of core detectors which had previously been calibrated to the incor-rect reactor power calculation, were recalibrated to the corrected " thermal power best" value.

Apparent Cause of Occurrence:

This incident resulted from the incorrect storage of a data valus within the CTPA program. The technician involved, needing a computer location in which to store a numerical constant, placed the constant in a location occupied by a zero, thinking such to be an unused computer memory location.

The zero stored in that location.however, was normally used by the program for calcu-lation of Reactor Coolant pressure. Therefore, changing this data value resulted in an incorrect pressure calculation and in a 10% error in the " thermal power best" determination.

Analysis of Occurrence:

This incident resulted in the operation of the unit for a period of approxi-mately 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> during which the out-of-core detectors were indicating a power level approximately 10% below the actual power. During this time, however, no safety limits were exceeded because the unit was operating at a reduced power level in preparation for a refueling outage.

It is concluded therefore, that the health and safety of the public was not affected by this occurrence.

i Corrective Action:

It is felt that this occurrence is an isolated incident.

However, efforts are underway to evaluate the present controls for computer software and to imple-ment, as determined necessary, appropriate formal administrative policies.

8001090870

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