ML19323J003

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Monthly Operating Rept for May 1980
ML19323J003
Person / Time
Site: Dresden  
Issue date: 06/02/1980
From: Cieszkiewicz S
COMMONWEALTH EDISON CO.
To:
Shared Package
ML19323J001 List:
References
NUDOCS 8006170457
Download: ML19323J003 (6)


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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 050-237 UlllT Dresden II DATE June 2, 1980 COMPLETED 8Y S. A. Cieszkiewicz TELEPHONE (815) 942-2920, ext. 489 MONTH MAY, 1980 DAY.

AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe-Ne t) l 1

720 17 0 714 18 17 3

703 19 436 4

623 20 637 5

711 21 626 6

707 22 304 7-

-70 7 23 572 8

707 24 664 9

70 3 25 603

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10 695 26 681 11 691 27_

692 12 284 28 679 13 0

29 672 14 0

30 669 15-0' 31.

670 16-0

8006:17Off7

OPERATING DATA REPORT DOCKET NO. 050-237 OATE June 2.

1980 COMPLETED BY S. Cieszkiewicz_,

TELEPHONE (815) 942-2920 OPERATING STATUS NOTES 1.

. Unit Name: Dresden II 2.

Reporting Period: May, 1980 3

Licensed Thermal Power (MWt): 2.527 4.

Nameplate Rating (Gross MWe):

828 5

Design Electrical Rating (Net NWe): 794 6.

Maximum Dependable Capacity (Gross MWe): 812 7.

Maximum Dependable Capacity (Net MWe): 772 8.

If Changes Occur in Capacity Ratings (items 3 Through 7) Since Last Report, Give Reasons:

NA 9

Power Level to Which Restricted, If Any (Net MWe): NA 10.

Reasons For Restrictions, if Any: NA This Month Yr-to-Date Cumulative 11.

Hours in Reporting Period 744 3,647 88,103 12.

Number of Hours Reactor Was Critical 599.35 3,487.03 68,223.47 13 Reactor Reserve Shutdown Hours 0

0 0

14.-

Hours Generator On-Line 578.58 3,456.6 64,719.13 15 Unit Reserve Shutdown Hours 0

0 0

16.

Gross Thermal Energy Generated (MWH) 1,287,238 8,113,608 134,839,223 17 Gross Electrical Energy Generated (MWH) 401,639 2.582.138 41.588.757 j

18.

Net Electrical Energy Generated (MWH) 378,731 2,452,499.4 39,340,610.617 19 Unit Service Factor 78 95 73 20.

Unit Availability Factor 78 95 73 21.

Uni t Capaci ty Factor (Using MOC Net) 66 87 58 22.

Unit Capacity. Factor (Using DER Net) 64 85 56 23 Unit Forced Outage Rate 3

1 13 24.

Shutdowns' Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

NA-25.

If Shut Down At End Of Report Period, Estimated Date of Startup: NA

UtH.I.L i 114. 050-237 UNIT SIIUTD0V115 AND POVER REDUCT10lls Utili flNIE Dreedin II DATE Jun* 2.

1980 00ftPLETED nY S. A. Cieszkiewice TELEPil0llE (815) 942-2920 REPORT N0HTil RW, 1980 q

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Licensee 7e E"e Cause & Corrective

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Date E

No E

2US Event

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Prevent Recurrence O

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800512 F

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3 Rx scrammed on MSL 111 Rad (spurious signal) 4 800512 S

144.6 A

Maintenance outage - replaced "B" recirc.

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t pomp seals s

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10.8 G

3 Rx scrammed on Rx low level (instrument r'

rack jarred) s 1

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s Ft Forced Reason:

G-Operational Error fa-other (Explain)

SI Scheduled A-Equipment Failure (Explain) '

Il-Other (Explain)

B-Itaintenance of Test is Exhibit G-Instructions.for C-Refueling D-Regulatory ltestriction 3 liet hod:

preparation of Data 1 -itanua l Entry Sheets fo* licensee E-Operator. Training & License Examina 1

2-Ilonudi Scrnm Event Report (

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F-Administrative 3-Aut'omotic Scram 0161)

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DRESDEtt UtilT 2

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SAFETY RELATED 11AINTEllAllCE - MAY, 1980 NATURE OF LER OR OUTAGE IIALFullCT10ft CORRECTIVI-Acil0N EQUIPl1ENT liAINTEllAtlCE

- IlultBER CAUSE RESULT NA -

NA Lubricated shaf t & stroked A0 Velve 1601-62 Preventive WR #6350 Outage #2-2 valve.

NA NA Changed wirinF-HPCI Valve Preventive WR #6168 Outage #2-2 2301-35 & 36 NA NA Ad' justed lever..

HPCI Turbine Preventive WR #6219 Outage #2-2 Turning Gear i

NA NA Replaced pots.

2"A" 125V Preventive WR #6424 Outage #2-2 Battery Charger NA NA Replaced locking screw Icolation Con-Preventive WR #6135 Outage #2-2 threads.

drnser Steam Linn Flow Switch NA NA Replaced relay.

Main Steam Line Preventive WR #6392 Outage #2-3 Iligh Radiation LER #80-14/03L-0 Monitor "C" 1

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SUMMARY

OF OPERATING EXPERIENCE UNIT TWO MAY, 1980 5-1 to 5-12 Unit Two started the month operating at a power level of 720 MWe.

On May 12, at 1011, a spurious signal developed on the main steam high radiation monitors, resulting in a Group I isolation and subsequent reactor scram.

5-12 to 5-18 Unit Two commenced its scheduled main-tenance outage at 2011 on May 12, 1980 to replace "B" recire. pump seals.

5 to 5-22 The Unit was placed back on line at 2047 l

on May 18 and reached a power level of 630 MWe when the inadvertent jarring of an instrument rack by Mechanical Main-4 l

tenance resulted in the Unit scramming on reactor low level at 1137 on May 22.

1 5-22 to 5-31 The Unit was again placed on line at 2226 and operated the remainder of the month at an average power level of 621 MRe, with a capacity factor of 64% for the entire month.