LER-1980-015, /03L-0:on 800403,piston Rod on Closure Mechanism for Reactor Bldg Ventilation Automatic Isolation Valve Was Found Broken,Making Valve Inoperable.Caused by Component Failure.New Piston Rod Eye Stud Was Fabricated & Installed |
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LICENSEE EVENT REPORT 1
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60 61 DOCKET NUM8ER 68 69 EVENT CATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 101011 On April 3, 1980 an operator found the oiston rod on the c l o e n re
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The valve was inoperable and therefore secondarv i
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36 37 40 di 42 43 44 47 CAuSE DESCRIPTICN AND CORRECTIVE ACTIONS h lilCi l Component failure was *he cause of this occurrence.
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The cause of the failure i
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The piston rod eye studs on all reactor building ventilation l
automatic isolation valves will be inspected.
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Morristown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jerse/ 08731 Licensee Event Report Reportable Occurrence No. 50-219/80-15/3L Report Date May 7, 1980 Occurrence Date April 3, 1980 identification of Occurrence Degradation of secondary containment integrity when it was determined that Reactor Building ventilation system automatic isolation valve h 39) was inoperable.
This is a violation of a limiting condition for oper tion as per Technical Specificaticn 3 5.B.1.
This event is considered to be a reportable occurrence as defined in the Techni-cal Specifications, paragraph 6.9.2.b(4).
Conditions Prior to Occurrence The plant was shutdown for a refueling / maintenance outage.
The reactor was subcritical.
The reactor mode switch was locked in refuel.
The cavity was flooded.
Descriotion of Occurrence On Thursday, April 3,1980, an operator found the piston rod on the closure mechanism for the Reactor Building ventilation automatic isolation valve (V-28-39) broken.
The valve was secured in the closed position as required by the Technical Specification. A Job Crder (5054M) was initiated to repair the valve.
Acoarent Cause of Occurrence Piston rod eye stud was broken. The cause of the failure was undetermined.
Analysis of Occurrence Secondary containment is designed to minimize any ground level release of radio-active materials which might result from an accident.
The Reactor Building Jersey Centra! Power & L:gr.t Company is a Member cf me General Puclic UtMt:es System
Reportable Occurrence No. 50-219/80-15/3L Page 2 May 7, 1980 provides secondary containment during reactor operation when the drywell is sealed and in service and provides primary containment when the reactor. is shutdown and the drywell is open.
Secondary containment is required during fuel handling operations and whenever work is being performed on the reactor or its connected systems in the Reactor Building, since their operation could result in an inadvertant release of radioactive material.
V-28-39 is one of a set of two air operated valves in series that will close automatically upon a shutdown or isolation signal.
On Monday, April 1, 1980, the valve was surveilled and no problems were detected.
Two days later the va:ve was found inoperable and removed from service.
The safety significance of this event is considered minimal because the inoperability of V-28-39 only removed the redundancy to isolate the system not preventing the (fstem from per-forming its intended function.
Corrective Action
A new piston rod eye stud was fabricated and installed.
The spare parts list will be reviewed to include the recommended amount of spare parts.
Additionally, the piston rod eye studs will be inspected on all the Reactor Building ventila-tion automatic isolation valves.
Failure Data Manufacturer:
Rockwell Manufacturing Company size:
18" Type: Air Operated Butterfly n
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| 05000219/LER-1980-001-01, /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | | | 05000219/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000219/LER-1980-002-03, /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | | | 05000219/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000219/LER-1980-003-01, /01T-0:on 800116,during Inservice Insp on Core Spray Sparger Piping for Sys Ii,Two Indications of Cracks Discovered.Ultrasonic Test Revealed through-wall Cracks. Possibly Caused by Sparger Installation Method | /01T-0:on 800116,during Inservice Insp on Core Spray Sparger Piping for Sys Ii,Two Indications of Cracks Discovered.Ultrasonic Test Revealed through-wall Cracks. Possibly Caused by Sparger Installation Method | | | 05000219/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000219/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000219/LER-1980-004-03, /03L-0:on 800125,on 800125,29 & 0213,radioactive Water Discovered Leaking from Severely Pitted Aluminum Piping of Condensate Transfer Sys.Caused by Galvanic Corrosion.Leaks Temporarily Repaired & Piping to Be Replaced | /03L-0:on 800125,on 800125,29 & 0213,radioactive Water Discovered Leaking from Severely Pitted Aluminum Piping of Condensate Transfer Sys.Caused by Galvanic Corrosion.Leaks Temporarily Repaired & Piping to Be Replaced | | | 05000219/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000219/LER-1980-005-03, /03L-0:on 800205,during Weekly Surveillance of Standby Gas Treatment Sys,Setpoints for Radiation Monitors RNO4A-1 & RNO4A-2 Found to Read Less Conservatively than Tech Spec.Caused by Personnel Error & Instrument Drift | /03L-0:on 800205,during Weekly Surveillance of Standby Gas Treatment Sys,Setpoints for Radiation Monitors RNO4A-1 & RNO4A-2 Found to Read Less Conservatively than Tech Spec.Caused by Personnel Error & Instrument Drift | | | 05000219/LER-1980-006-03, /03L-0:on 800131,during Reactor Recirculation Flow Calibr surveillance,as-found Values of Recirculation Flow Sensors at Zero Percent Simulated Flow Were Out of Tolerance.Caused by Instrument Drift | /03L-0:on 800131,during Reactor Recirculation Flow Calibr surveillance,as-found Values of Recirculation Flow Sensors at Zero Percent Simulated Flow Were Out of Tolerance.Caused by Instrument Drift | | | 05000219/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000219/LER-1980-007-03, /03L-0:on 800213,while Performing 10-h Test on Standby Gas Treatment Sys 1,flow Was Less than Tech Spec Limit.Caused by Slipping Drive Belts on Exhaust Fan EF1-8. Drive Belts Replaced | /03L-0:on 800213,while Performing 10-h Test on Standby Gas Treatment Sys 1,flow Was Less than Tech Spec Limit.Caused by Slipping Drive Belts on Exhaust Fan EF1-8. Drive Belts Replaced | | | 05000219/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000219/LER-1980-008-01, /01T-0:on 800215,during Insp for IE Bulletin 79-14,discovered Nine Pipe Clamps Installed W/O Restraining Welded Lugs.Caused by Oversight During Const.Welded Lugs to Be Installed | /01T-0:on 800215,during Insp for IE Bulletin 79-14,discovered Nine Pipe Clamps Installed W/O Restraining Welded Lugs.Caused by Oversight During Const.Welded Lugs to Be Installed | | | 05000219/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000219/LER-1980-009-03, During Annual Insp of Containment Spray Heat Exchanges,Leaks Discovered in Four Heat Exchangers.Caused by Component Failure & Design.Heat Exchangers to Be Retubed W/Titanium | During Annual Insp of Containment Spray Heat Exchanges,Leaks Discovered in Four Heat Exchangers.Caused by Component Failure & Design.Heat Exchangers to Be Retubed W/Titanium | | | 05000219/LER-1980-009, Forwards Revised LER 80-009/03L-1 | Forwards Revised LER 80-009/03L-1 | | | 05000219/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000219/LER-1980-010-01, /01T-0:on 800220,during IE Bulletin 79-14 Insp, Pipe hangers,NP-2-R8A & NP-2-R8B Found Improperly Installed. Cleanup Sys Restraint Mod & Nonrigid Restraint Added | /01T-0:on 800220,during IE Bulletin 79-14 Insp, Pipe hangers,NP-2-R8A & NP-2-R8B Found Improperly Installed. Cleanup Sys Restraint Mod & Nonrigid Restraint Added | | | 05000219/LER-1980-010-03, /03L-1:on 790417,excavation Was Started to Repair Leak Near Inside Penetration within Pipe Tunnel.Activity Was Detected in Soil Near Dedt Line.Dedt Line Rerouted on 800316.Line Will Be Repaired | /03L-1:on 790417,excavation Was Started to Repair Leak Near Inside Penetration within Pipe Tunnel.Activity Was Detected in Soil Near Dedt Line.Dedt Line Rerouted on 800316.Line Will Be Repaired | | | 05000219/LER-1980-011-03, /03L-0:on 800219,during Surveillance Test,Trip Occurred on Standby Gas Treatment Sys 1.Caused by Cracked Flow Sensing Line Which Was Probably Stepped On.Line Replaced | /03L-0:on 800219,during Surveillance Test,Trip Occurred on Standby Gas Treatment Sys 1.Caused by Cracked Flow Sensing Line Which Was Probably Stepped On.Line Replaced | | | 05000219/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000219/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000219/LER-1980-012-03, /03L-0:on 800228,discovered That Weekly Surveillance Tests for Main Station & Diesel Generator Batteries Not Performed During Seventh Wk.Caused by Error in Personnel.Evaluation Will Be Made to Determine Improvements | /03L-0:on 800228,discovered That Weekly Surveillance Tests for Main Station & Diesel Generator Batteries Not Performed During Seventh Wk.Caused by Error in Personnel.Evaluation Will Be Made to Determine Improvements | | | 05000219/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000219/LER-1980-013-01, /01T-0:on 800309,fire Suppression Water Sys Removed from Svc to Replace Cracked Valve,Contrary to Tech Specs.Fire Truck Pumper Used as Water Supply Backup. Cause of Valve Body Crack Under Investigation | /01T-0:on 800309,fire Suppression Water Sys Removed from Svc to Replace Cracked Valve,Contrary to Tech Specs.Fire Truck Pumper Used as Water Supply Backup. Cause of Valve Body Crack Under Investigation | | | 05000219/LER-1980-014-01, /01T-0:on 800302,emergency Diesel Generator 1 Failed to Synchronize & Tripped When Generator 2 Was Tagged for Mod.Caused by Component Failure.Fuse F7,found Loose in Holder.Fuseholder Repaired | /01T-0:on 800302,emergency Diesel Generator 1 Failed to Synchronize & Tripped When Generator 2 Was Tagged for Mod.Caused by Component Failure.Fuse F7,found Loose in Holder.Fuseholder Repaired | | | 05000219/LER-1980-014, Forwards LER 80-014/01T-0 | Forwards LER 80-014/01T-0 | | | 05000219/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000219/LER-1980-015-03, /03L-0:on 800403,piston Rod on Closure Mechanism for Reactor Bldg Ventilation Automatic Isolation Valve Was Found Broken,Making Valve Inoperable.Caused by Component Failure.New Piston Rod Eye Stud Was Fabricated & Installed | /03L-0:on 800403,piston Rod on Closure Mechanism for Reactor Bldg Ventilation Automatic Isolation Valve Was Found Broken,Making Valve Inoperable.Caused by Component Failure.New Piston Rod Eye Stud Was Fabricated & Installed | | | 05000219/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000219/LER-1980-016-01, /01T-0:on 800512,util Recognized That 800420 Discovery of Defective Pressure Switch,Psl D,Constituted Immediate Rept.Caused by Cocked Teflon Actuator.Switch Removed & Will Be Replaced | /01T-0:on 800512,util Recognized That 800420 Discovery of Defective Pressure Switch,Psl D,Constituted Immediate Rept.Caused by Cocked Teflon Actuator.Switch Removed & Will Be Replaced | | | 05000219/LER-1980-017-01, /01T-0:on 800516,while Performing Control Rod Interference checks,green-green Rod Position Indication Remained Illuminated While Withdrawing Rod 10-23.Caused by Operator & Procedure in Bypass & Component Failure | /01T-0:on 800516,while Performing Control Rod Interference checks,green-green Rod Position Indication Remained Illuminated While Withdrawing Rod 10-23.Caused by Operator & Procedure in Bypass & Component Failure | | | 05000219/LER-1980-017, /03L-0:on 800520,during Investigation of LER 80-17/1T, One Rod Free Travel Interlock Surveillance Requirements Not Performed as Required.Causec by Failure to Perform Procedure & Schedule Surveillance | /03L-0:on 800520,during Investigation of LER 80-17/1T, One Rod Free Travel Interlock Surveillance Requirements Not Performed as Required.Causec by Failure to Perform Procedure & Schedule Surveillance | | | 05000219/LER-1980-018-03, /03L-0:on 800507,during Monthly Surveillance Testing of Reactor High Pressure Scram sensors,RE03D Found to Be Less Conservative than Specified.Caused by Sensor Repeatability.Sensor Reset | /03L-0:on 800507,during Monthly Surveillance Testing of Reactor High Pressure Scram sensors,RE03D Found to Be Less Conservative than Specified.Caused by Sensor Repeatability.Sensor Reset | | | 05000219/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000219/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000219/LER-1980-020-01, /01T-0:on 800605,following Insp of Fire Barriers Protecting safety-related Areas,Several Penetrations Found in Degraded Condition.Caused by Deficiencies in Installation Specs & Personnel Error Re Delay in Establishing Watche | /01T-0:on 800605,following Insp of Fire Barriers Protecting safety-related Areas,Several Penetrations Found in Degraded Condition.Caused by Deficiencies in Installation Specs & Personnel Error Re Delay in Establishing Watches | | | 05000219/LER-1980-021, Has Been Cancelled | Has Been Cancelled | | | 05000219/LER-1980-022-03, /03L-0:on 800603,reactor High Pressure Isolation Condenser Initiation Switch Trip Points Found Less Conservative than Specified.Caused by Unusual Svc Condition. Pressure Switches Reset & Exercised to Ensure Operation | /03L-0:on 800603,reactor High Pressure Isolation Condenser Initiation Switch Trip Points Found Less Conservative than Specified.Caused by Unusual Svc Condition. Pressure Switches Reset & Exercised to Ensure Operation | | | 05000219/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000219/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000219/LER-1980-023-03, /03L-0:on 800523,prior to Inservice Insp Reactor Vessel Hydro,Testing Revealed That Electromatic Relief Valve High Pressure Sensor IA83B Exceeded Tech Spec Setpoint. on 800531,sensor IA83F Found to Exceed Setpoint | /03L-0:on 800523,prior to Inservice Insp Reactor Vessel Hydro,Testing Revealed That Electromatic Relief Valve High Pressure Sensor IA83B Exceeded Tech Spec Setpoint. on 800531,sensor IA83F Found to Exceed Setpoint | | | 05000219/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000219/LER-1980-025, Forwards LER 80-025/01T-0 | Forwards LER 80-025/01T-0 | | | 05000219/LER-1980-025-01, /01T-0:on 800618,during Surveillance Test, Nonfunctioning Operator Discovered in Valves V-9-12 & V-9-8 Found Leaking.Caused by Component Failure.Defective Valves Replaced & Will Be Inspected.Revised Rept Will Follow | /01T-0:on 800618,during Surveillance Test, Nonfunctioning Operator Discovered in Valves V-9-12 & V-9-8 Found Leaking.Caused by Component Failure.Defective Valves Replaced & Will Be Inspected.Revised Rept Will Follow | | | 05000219/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000219/LER-1980-026-03, /03L-0:on 800709,during Routine Testing Insp of Hydraulic Snubbers Installed in safety-related Sys,Snubber 75/5 Failed to Lock Up in Compression Direction.Caused by Foreign Matl in Snubber Fluid.Snubber Flushed & Refilled | /03L-0:on 800709,during Routine Testing Insp of Hydraulic Snubbers Installed in safety-related Sys,Snubber 75/5 Failed to Lock Up in Compression Direction.Caused by Foreign Matl in Snubber Fluid.Snubber Flushed & Refilled | | | 05000219/LER-1980-027, Forwards LER 80-027/01T-0 | Forwards LER 80-027/01T-0 | |
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