LER-1980-010, /03L-1:on 790417,excavation Was Started to Repair Leak Near Inside Penetration within Pipe Tunnel.Activity Was Detected in Soil Near Dedt Line.Dedt Line Rerouted on 800316.Line Will Be Repaired |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2191980010R03 - NRC Website |
|
text
.,, h LICENSEE EVENT REPORT CC".MOL BLCCK l l
l l
l l
l (PLEASE FRlNT OR TYPE ALL REOUIRED INFORMATION) lN iJ i0 lC !P l1 l@l0 l0 l-10 l0 l0 l0 10 l-l0 10 l@l4l1l1l1l1l@l l
l@
S ?
p;Er.SEE CODE 14 15 LICENSE NuuSER 25 26 LICENSE TYPE JO 57 C=I 58 cOv7 l'o l i !
C"C[ l L l@l015 10 lo 10 !2 11 19 l@l0 14 11 17 17 19 @l0161210181ol@j 7
6 60 61 COCK 17 NUYSER 6a 69 EVENT CATE 74 75 REPORT O ATE 80 EVEN T DESCRIPTION AND PROBA8LE CONSEQUENCES h t O ::! l On March 15, 1979, a leak was noticed in the vicinity of the inside I
30,3, l penetration within the pipe tunnel. Analysis showed isotopic concentra-l
- o ja; ; tion to be the same as that of the DEDT water.
The DEDT line was re-l 10 : 3
- routed.
On Apr*l 17, 1979, excavation commenced in order to effect I
r i c !e t e repairs. Activity was detected in the soll near the DEDT line.
Based I
- on analysis, the contamination was localized.
(See the attached report I
l: i:
i e i s ; j for Reportable Occurrence 50-219/79-10/3L-1)
I 8e SYSTEV
CAUSE
CAUSE COMP.
VALVE 000; 000E SUSCOOE COM?O*;E*:T OOOE SU2000E SUSCOOE ici?)
iM IA !@ l El@ l X l@ l Pl ll Pl El Xl Xl@ l Al@ W @
3 10 11 12 13 18 19 20 SEOLENTI AL CCCU R R ENCE REtCRT 9EVisiCN mo EVENT VEAR R E*CRT NO.
COOE TYPE NO.
@ N=,*=,g l21810l l-l 10 l1 l 0 l l/l l Ol 31 lLl l-l 11 l 22 23 24 26 27 23 29 00 31 32 TK A'C ON O P NT ME HOURS S8 PO 8.
SUP*LI E MANUSA RER l X lg]34 l@
l Z l@
l Zl@
l01010l0l lY l@
l Yl@
l Z l@
lZ191919l(
B 20 35 36 37 40 41 42 43 44 47 CAusE OESCRipitCN AND CCRRECTIVE ACTIONS l i l o l l The DEDT line was rerouted on March 16. 1979 to prevent further leakaae.
I litii l Corrective action will consist of repairs to the line.
The construction I
li l21 I of a structure to enclose the pipe runs from the reactor buildino to the I
y l main pipe tunnel has been completed.
I 12 14 i i I
7 8 9 80
'sYA S
- . POWER OTHER STATUS t CO Y
OISCOVERY DESCRIPTION Ii 15 l lE l@ l 0 l 9 l 5 l@l NA l
l L l@l Analysis of Soil Sample l
ACTIVt TY CO TENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE li j s l l Ll @ l M l@l See Attachme;1t l
l Drvwe11 Eautoment Drain Tank Li;te l
7 s 9 to it 44 45 80
- ERSONNEL EXPCSUROS NUMBER TYPE
DESCRIPTION
li 17 l l010 l0 l@l Zl@l NA I
,iRSO~~Ei.'imuh
% VSER OESCRIPTION li l4 l l 0l Ol Ol@l NA l
7 8 9 11 12 80 LOS?. 08 OR OAVAGE TO FACILITY Tv' E O E SCRl* TION li191lZl@l NA l
l 7
e 9 10 80 iSSvE DESCRIPTIO*4 j
l: l o l lN fhl NA l
lllllllll1Iil}
i e
's 10 GS 69 an.;
Donald A. Ross PHONE: - NM-8784 NAME 05 8RESARER 8006300g*fl
b
~.
Jersey Central Power & Light Company b
(I" ()j Madison Avenue at Punch Bowl Road Momstown, New Jersey 07960 (201)455-8200 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/79-10/3L-1 Report Date Update Report - June 20, 1980 Previous Report Date - May 17, 1979 Occurrence Date April 17, 1979 Identification of Occurrence Unmonitored release of radioactive water from the drywell equipment drain tank discharge piping. This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b.4.
Conditions Prior to Occurrence The plant parameters at the time of the occurrence were:
Power:
Reactor, 1834.18 MWt Electrical, 644 MWe Flow:
Recirculation, 14.1 x 106 gpm 4
Feedwater 6.837 x 10 lb/hr Stack Gas Activity:
3.66 x 10 pCi/sec.
Description of Occurrence On April 17, 1979, at approximately 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />, soil sample", were taken from the immediate area of the drywell equipment. drain tank line between the reactor building and the pipe tunnel. The isotopic distribution was consistent with that of primary coolant that had decayed for a month.
Apparent Cause of Occurrence The cause of this occurrence is attributed to component failure.
Jersey Central Power & Light Company is a Member of the General Pubhc Utihties System
i.__
4 Rzportable Occurrence No. 50-219/79-10/3L-1 Paga 2 Update Report:
June 20, 1980 Previous Report Date: May 17, 1979 Analysis of Occurrence LeW<s discovered in the Drywell Equipment Drain Tank discharge line (f.0. No.
50-219/79-10/3L) and Laundry Drain Tank discharge line (R.O. No. 50-211/79-26/3L) could not be completely analyzed at the time of occurrence.
Core samples taken prior to excavation and soil samples taken during excavation confirmed that the contamination was localized.
A total of 17 drums of dirt removed from the hole had contamination levels above background and were shipped as radioactive waste.
Much of this was as a result of contamination spread in the dirt during shoveling and loading into drums.
Based on the average concentration found in the drummed dirt, the following estimated activity was present:
Co 60 26 pCI Cs 134 3.6 pCi Cs 137 4.6 pCi 1
Af ter the hole was excavated to the desired depth of approximately 17 feet for construction of the vault, soil samples from the bottom were analyzed prior to pouring the concrete floor.
None of the samples showed any detectable activity above normal background.
Well water samples from the Oyster Creek site and surrounding area are collected and analyzed every four weeks a: part of the plant Radiological Environmental Monitoring Program.
There has been no observed detectable activity above normal background in samples collected.
1 It is concluded from the analytical results that:
- 1) Contamination from the leaks was indeed localized in the immediate area of the leaks; 2) No radioactivity entered into the water table; 3) All significant contamination in the soil was removed.
Corrective Action
On March 15, 1979, a leak was notired in the vicinity of the inside penetration within the pipe tunnel.
A sample of the water in the pipe tunnel was analyzed 1
and the gross beta concentration was 3.1 x 10 pCI/ml. The gamma isotopic analysis showed the isotopic composition to be the same as that of the drywell equipment drain tank water.
The immediate action taken was the preparation for rerouting of the DEDT line to prevent further leakage.
Rerouting of the line was accomplished on i
March 16, 1979 I
Corrective action will consist of repairs to the line.
The construction of a structure to enclose the pipe runs from the reactor building to the main pipe I
tunnel has been completed.
Failure Data N/A i
t
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000219/LER-1980-001-01, /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | /01T-o:on 800105,while Performing Electromatic Relief Valve Operability Test,Emergency Releie Valve D Failed to Open.Caused by Component Failure Due to Retainer Ring Being Backed Off Approx Six Threads | | | 05000219/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000219/LER-1980-002-03, /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | /03L-0:on 800116,during Fuel Bundle Clip Insp,Fuel Bundle UD-3-023 Was Misoriented & Was Not Properly Seated in Core Cell Location.Caused by Personnel Error & Inadequate Procedural Controls.Procedure 205 Revised | | | 05000219/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000219/LER-1980-003-01, /01T-0:on 800116,during Inservice Insp on Core Spray Sparger Piping for Sys Ii,Two Indications of Cracks Discovered.Ultrasonic Test Revealed through-wall Cracks. Possibly Caused by Sparger Installation Method | /01T-0:on 800116,during Inservice Insp on Core Spray Sparger Piping for Sys Ii,Two Indications of Cracks Discovered.Ultrasonic Test Revealed through-wall Cracks. Possibly Caused by Sparger Installation Method | | | 05000219/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000219/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000219/LER-1980-004-03, /03L-0:on 800125,on 800125,29 & 0213,radioactive Water Discovered Leaking from Severely Pitted Aluminum Piping of Condensate Transfer Sys.Caused by Galvanic Corrosion.Leaks Temporarily Repaired & Piping to Be Replaced | /03L-0:on 800125,on 800125,29 & 0213,radioactive Water Discovered Leaking from Severely Pitted Aluminum Piping of Condensate Transfer Sys.Caused by Galvanic Corrosion.Leaks Temporarily Repaired & Piping to Be Replaced | | | 05000219/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000219/LER-1980-005-03, /03L-0:on 800205,during Weekly Surveillance of Standby Gas Treatment Sys,Setpoints for Radiation Monitors RNO4A-1 & RNO4A-2 Found to Read Less Conservatively than Tech Spec.Caused by Personnel Error & Instrument Drift | /03L-0:on 800205,during Weekly Surveillance of Standby Gas Treatment Sys,Setpoints for Radiation Monitors RNO4A-1 & RNO4A-2 Found to Read Less Conservatively than Tech Spec.Caused by Personnel Error & Instrument Drift | | | 05000219/LER-1980-006-03, /03L-0:on 800131,during Reactor Recirculation Flow Calibr surveillance,as-found Values of Recirculation Flow Sensors at Zero Percent Simulated Flow Were Out of Tolerance.Caused by Instrument Drift | /03L-0:on 800131,during Reactor Recirculation Flow Calibr surveillance,as-found Values of Recirculation Flow Sensors at Zero Percent Simulated Flow Were Out of Tolerance.Caused by Instrument Drift | | | 05000219/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000219/LER-1980-007-03, /03L-0:on 800213,while Performing 10-h Test on Standby Gas Treatment Sys 1,flow Was Less than Tech Spec Limit.Caused by Slipping Drive Belts on Exhaust Fan EF1-8. Drive Belts Replaced | /03L-0:on 800213,while Performing 10-h Test on Standby Gas Treatment Sys 1,flow Was Less than Tech Spec Limit.Caused by Slipping Drive Belts on Exhaust Fan EF1-8. Drive Belts Replaced | | | 05000219/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000219/LER-1980-008-01, /01T-0:on 800215,during Insp for IE Bulletin 79-14,discovered Nine Pipe Clamps Installed W/O Restraining Welded Lugs.Caused by Oversight During Const.Welded Lugs to Be Installed | /01T-0:on 800215,during Insp for IE Bulletin 79-14,discovered Nine Pipe Clamps Installed W/O Restraining Welded Lugs.Caused by Oversight During Const.Welded Lugs to Be Installed | | | 05000219/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000219/LER-1980-009-03, During Annual Insp of Containment Spray Heat Exchanges,Leaks Discovered in Four Heat Exchangers.Caused by Component Failure & Design.Heat Exchangers to Be Retubed W/Titanium | During Annual Insp of Containment Spray Heat Exchanges,Leaks Discovered in Four Heat Exchangers.Caused by Component Failure & Design.Heat Exchangers to Be Retubed W/Titanium | | | 05000219/LER-1980-009, Forwards Revised LER 80-009/03L-1 | Forwards Revised LER 80-009/03L-1 | | | 05000219/LER-1980-010, Forwards LER 80-010/01T-0 | Forwards LER 80-010/01T-0 | | | 05000219/LER-1980-010-01, /01T-0:on 800220,during IE Bulletin 79-14 Insp, Pipe hangers,NP-2-R8A & NP-2-R8B Found Improperly Installed. Cleanup Sys Restraint Mod & Nonrigid Restraint Added | /01T-0:on 800220,during IE Bulletin 79-14 Insp, Pipe hangers,NP-2-R8A & NP-2-R8B Found Improperly Installed. Cleanup Sys Restraint Mod & Nonrigid Restraint Added | | | 05000219/LER-1980-010-03, /03L-1:on 790417,excavation Was Started to Repair Leak Near Inside Penetration within Pipe Tunnel.Activity Was Detected in Soil Near Dedt Line.Dedt Line Rerouted on 800316.Line Will Be Repaired | /03L-1:on 790417,excavation Was Started to Repair Leak Near Inside Penetration within Pipe Tunnel.Activity Was Detected in Soil Near Dedt Line.Dedt Line Rerouted on 800316.Line Will Be Repaired | | | 05000219/LER-1980-011-03, /03L-0:on 800219,during Surveillance Test,Trip Occurred on Standby Gas Treatment Sys 1.Caused by Cracked Flow Sensing Line Which Was Probably Stepped On.Line Replaced | /03L-0:on 800219,during Surveillance Test,Trip Occurred on Standby Gas Treatment Sys 1.Caused by Cracked Flow Sensing Line Which Was Probably Stepped On.Line Replaced | | | 05000219/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000219/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000219/LER-1980-012-03, /03L-0:on 800228,discovered That Weekly Surveillance Tests for Main Station & Diesel Generator Batteries Not Performed During Seventh Wk.Caused by Error in Personnel.Evaluation Will Be Made to Determine Improvements | /03L-0:on 800228,discovered That Weekly Surveillance Tests for Main Station & Diesel Generator Batteries Not Performed During Seventh Wk.Caused by Error in Personnel.Evaluation Will Be Made to Determine Improvements | | | 05000219/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000219/LER-1980-013-01, /01T-0:on 800309,fire Suppression Water Sys Removed from Svc to Replace Cracked Valve,Contrary to Tech Specs.Fire Truck Pumper Used as Water Supply Backup. Cause of Valve Body Crack Under Investigation | /01T-0:on 800309,fire Suppression Water Sys Removed from Svc to Replace Cracked Valve,Contrary to Tech Specs.Fire Truck Pumper Used as Water Supply Backup. Cause of Valve Body Crack Under Investigation | | | 05000219/LER-1980-014-01, /01T-0:on 800302,emergency Diesel Generator 1 Failed to Synchronize & Tripped When Generator 2 Was Tagged for Mod.Caused by Component Failure.Fuse F7,found Loose in Holder.Fuseholder Repaired | /01T-0:on 800302,emergency Diesel Generator 1 Failed to Synchronize & Tripped When Generator 2 Was Tagged for Mod.Caused by Component Failure.Fuse F7,found Loose in Holder.Fuseholder Repaired | | | 05000219/LER-1980-014, Forwards LER 80-014/01T-0 | Forwards LER 80-014/01T-0 | | | 05000219/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000219/LER-1980-015-03, /03L-0:on 800403,piston Rod on Closure Mechanism for Reactor Bldg Ventilation Automatic Isolation Valve Was Found Broken,Making Valve Inoperable.Caused by Component Failure.New Piston Rod Eye Stud Was Fabricated & Installed | /03L-0:on 800403,piston Rod on Closure Mechanism for Reactor Bldg Ventilation Automatic Isolation Valve Was Found Broken,Making Valve Inoperable.Caused by Component Failure.New Piston Rod Eye Stud Was Fabricated & Installed | | | 05000219/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000219/LER-1980-016-01, /01T-0:on 800512,util Recognized That 800420 Discovery of Defective Pressure Switch,Psl D,Constituted Immediate Rept.Caused by Cocked Teflon Actuator.Switch Removed & Will Be Replaced | /01T-0:on 800512,util Recognized That 800420 Discovery of Defective Pressure Switch,Psl D,Constituted Immediate Rept.Caused by Cocked Teflon Actuator.Switch Removed & Will Be Replaced | | | 05000219/LER-1980-017-01, /01T-0:on 800516,while Performing Control Rod Interference checks,green-green Rod Position Indication Remained Illuminated While Withdrawing Rod 10-23.Caused by Operator & Procedure in Bypass & Component Failure | /01T-0:on 800516,while Performing Control Rod Interference checks,green-green Rod Position Indication Remained Illuminated While Withdrawing Rod 10-23.Caused by Operator & Procedure in Bypass & Component Failure | | | 05000219/LER-1980-017, /03L-0:on 800520,during Investigation of LER 80-17/1T, One Rod Free Travel Interlock Surveillance Requirements Not Performed as Required.Causec by Failure to Perform Procedure & Schedule Surveillance | /03L-0:on 800520,during Investigation of LER 80-17/1T, One Rod Free Travel Interlock Surveillance Requirements Not Performed as Required.Causec by Failure to Perform Procedure & Schedule Surveillance | | | 05000219/LER-1980-018-03, /03L-0:on 800507,during Monthly Surveillance Testing of Reactor High Pressure Scram sensors,RE03D Found to Be Less Conservative than Specified.Caused by Sensor Repeatability.Sensor Reset | /03L-0:on 800507,during Monthly Surveillance Testing of Reactor High Pressure Scram sensors,RE03D Found to Be Less Conservative than Specified.Caused by Sensor Repeatability.Sensor Reset | | | 05000219/LER-1980-018, Forwards LER 80-018/03L-0 | Forwards LER 80-018/03L-0 | | | 05000219/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000219/LER-1980-020-01, /01T-0:on 800605,following Insp of Fire Barriers Protecting safety-related Areas,Several Penetrations Found in Degraded Condition.Caused by Deficiencies in Installation Specs & Personnel Error Re Delay in Establishing Watche | /01T-0:on 800605,following Insp of Fire Barriers Protecting safety-related Areas,Several Penetrations Found in Degraded Condition.Caused by Deficiencies in Installation Specs & Personnel Error Re Delay in Establishing Watches | | | 05000219/LER-1980-021, Has Been Cancelled | Has Been Cancelled | | | 05000219/LER-1980-022-03, /03L-0:on 800603,reactor High Pressure Isolation Condenser Initiation Switch Trip Points Found Less Conservative than Specified.Caused by Unusual Svc Condition. Pressure Switches Reset & Exercised to Ensure Operation | /03L-0:on 800603,reactor High Pressure Isolation Condenser Initiation Switch Trip Points Found Less Conservative than Specified.Caused by Unusual Svc Condition. Pressure Switches Reset & Exercised to Ensure Operation | | | 05000219/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000219/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000219/LER-1980-023-03, /03L-0:on 800523,prior to Inservice Insp Reactor Vessel Hydro,Testing Revealed That Electromatic Relief Valve High Pressure Sensor IA83B Exceeded Tech Spec Setpoint. on 800531,sensor IA83F Found to Exceed Setpoint | /03L-0:on 800523,prior to Inservice Insp Reactor Vessel Hydro,Testing Revealed That Electromatic Relief Valve High Pressure Sensor IA83B Exceeded Tech Spec Setpoint. on 800531,sensor IA83F Found to Exceed Setpoint | | | 05000219/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000219/LER-1980-025, Forwards LER 80-025/01T-0 | Forwards LER 80-025/01T-0 | | | 05000219/LER-1980-025-01, /01T-0:on 800618,during Surveillance Test, Nonfunctioning Operator Discovered in Valves V-9-12 & V-9-8 Found Leaking.Caused by Component Failure.Defective Valves Replaced & Will Be Inspected.Revised Rept Will Follow | /01T-0:on 800618,during Surveillance Test, Nonfunctioning Operator Discovered in Valves V-9-12 & V-9-8 Found Leaking.Caused by Component Failure.Defective Valves Replaced & Will Be Inspected.Revised Rept Will Follow | | | 05000219/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000219/LER-1980-026-03, /03L-0:on 800709,during Routine Testing Insp of Hydraulic Snubbers Installed in safety-related Sys,Snubber 75/5 Failed to Lock Up in Compression Direction.Caused by Foreign Matl in Snubber Fluid.Snubber Flushed & Refilled | /03L-0:on 800709,during Routine Testing Insp of Hydraulic Snubbers Installed in safety-related Sys,Snubber 75/5 Failed to Lock Up in Compression Direction.Caused by Foreign Matl in Snubber Fluid.Snubber Flushed & Refilled | | | 05000219/LER-1980-027, Forwards LER 80-027/01T-0 | Forwards LER 80-027/01T-0 | |
|