ML19318A090

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Monthly Operating Rept for May 1980
ML19318A090
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/01/1980
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML19318A089 List:
References
NUDOCS 8006180442
Download: ML19318A090 (5)


Text

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AYERAGECAlLY UNIT POWER LEVEL ..

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,',., DOCKET NO.

50-348 .

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er 1 DATE 6/1/80

- W. G. Ilairston, III COMPLETED BY

, 7 TELEPHONE (205) 899-5156 MONTH May .

DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL ,

, (MWe-Net) (MWe. Net) g, 808 798 .

37 811 gg 799 2 .

3 798 g, 782' -

4 807 -

y 652 806

  • 622 -

5 21 ' -

g 806 22 652 7 806 y 788

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g 802 800 3

9 806 25 796 -

10 800 ' .

3 799

' gg 804 796 . . W.

3' I 790 -

800 12 28 ,

~' 786 804 .

13 -

29 '

804 803

. 34. _

gg 803 792 .

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I6 798 INSTRUCTIONS On this formst. list the average dsity unit power level in MWe-Net for each day in the reporting month. Ccmpute ta the nearest whole megawatt.

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OPERATING DATA REPORT -

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  • DOCKET NO. 50-348-DATE 6/1/80 COMPLETED BY _W. G. Hairston, III

. . . TELEPHONE (205) 899-5156 OPERATING STATUS -

I. Unit Name. Joseph M. Farley - -

Unit 1 -

Notes 1/Cumulativ'e ifata trince l

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2. Reporting Period: -Mav, 1980 12/1/77, date of commercial I 2652 operation.
3. Licensed ThermalPower (MWr):

, 4. Nameplate Rating (Gross MWe): 860 * *

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S. Design Electrical Rating (Net MWe): _

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d. Maximum Dependable Capacity (Gross MWe):
7. Maximum Dependable Capacity (Net MWe):

S. If Changes Occurin Capacity Rstings (Items Number 3 Through 7) Since list Report.Give Reasons:

Maximum Dependable Capacity (Gross MWe and Net MWe) have been determined from operating experience.

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9. Power Level To Which Restricted,If Any (Net MWe): _N/A q
10. Reasons For Restrictions,If Any: N/A \

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II. Hours In Reporting Period .

744 ' 3.647' '21.911

12. Number of Hours Reactor Was Critical 744 3,210.6 14,146.1

{ 13. Reactor Reserve Shutdown Hours . 0- ...- .,

436.4 1,841.7 .

14. Hours Generator On4.Ine .

.- 744 - 3,147.7 13,738.2 .

35. Unit Reserve Shutdown Hours -

- 16. Gross Thermal EnerEy Generated (MWH) 1,927,148.2 7,958,932.5_ 34,556,946.9 614,696 e

37. Gross Electrical Energy Generated (MWH) 2,562,364. . 11,086,402

' IS. Net Electrical EnerEy Cenerated (MWH) .

583,600 2,421,222 10,469,402 ,

19. Unit Service Factor .'..2 100.0 ,

86.3 62.7

20. Unit Availability Factoe .

100.0 86.3 62.7 .

23. Unit Capacity Factor (Using MDC Net) . 97.6 .

82.6 59.5

'. 22. Unit Capacity Factor (Using DER Net)

23. Unit Forced Outage Rate

'94;6 0.0 80 1.__

3.9 97 6 ,

6.6 )

24.' Shutdowns Scheduled OverNext 6 Months (Type.Date.and Durst" ion of Eacht:' ,,

Refueling Outage, Mid September /Early October 1980, approximately 8 weeks'. . C 25, ifs! ut Down At End Of Report Period. Estimated Dare ofStartup: N/A -

26. Units in Test Status (Prior to Commercial Operation): Forecast . Achieved INITIAL CRITICALITY 8/6/77 I 8/9/77 1

i INITIAL ELECTRICITY 8/20/77 ,- 8/18/77 COMMERCIAL OPERATION 12/1/77 .

12/1/77

,..f, N/77)

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50-348 UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKETNO. 7* n. Farley - Unitb'i UNIT NAME -

DATE "# 'I N W. G. tiairston, III COMPLETED BY May REFORT MONTH TELEPHONE (205) 899-5156 Tee

,$ ? "g License,. Et, *, Cause & Corrective No. Date k 3g ,

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a: Event g'g EO

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mO g Prevent Recurrence F

$5 & j;2 g Report #

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  • 039 800503 S 2.7 B N/A N/A HA VALVEX Unit was reduced to and held at 775 MWe for Main Turbine Governor Valve

. Testing.

040 800510 S 2.8 B N/A N/A HA VALVEX Unit was reduced to and held at 770 MWe for Main Turbine Governor Valve Testing.

041 800511 F 0.5 D N/A 80-031/03L-0 . ID INSTRU Unit was ramping down to be taken off

  • line in compliance with the Technical Specification for loss of Data Cabinets A and B Direct Rod Position Indication. At 782 MWe, one channel of the DRPI was restored and ramp-down terminated. .

3 4 i 2 Method: Exhibit G Instructions F: Forced Reason: for Preparation of Data A Equiprnent Failure (Explain) l-Manual S: Scheduled 2 Manual Scram. Entry Sheets for Licensee

. B Maintenance of Test Event Report (LER) File (NUREG-C-Refueling 3-Automatic Scram.

4-Other (Explain) 0161)

D Regulatory Restriction E Operator Training & License Examination -

5 F Administrative Exhibit I- Same Source G Operational Error (Explain)

(9/77).. Ilother(Explain)

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50-348 M. Farley - Unit I }

DOCKET NO.

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UNITSilUTDOWNS AND POWER REDUCTIONS UNITNAME DATE W. 6/1/80 6 Ha uston, m NL.ETED BY REPORT MONTH May TELEPHONE (205) 899-5156 E

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};; }YsM Licensee Ee *** Cause & Corrective No. Date k jg Event y mu Action tu Prevent Recurrence

>- g5 5 j gij g Repor: # g 6 .

800512 6.9 B N/A N/A HH XXXXXX Unit was reduced to and held at 700

'042 S MWe to repair a lube oil gasket leak on 1C condensate pump.

800519 40.8 B N/A ~N/A HH PUMPXX Unit was reduced to and held at 700 043 S MWe to replace 1A condensate pump l

  • and motor due to excessive vibration.

5.0 B N/A N/A CH PIPEXX Unit was reduced to' and held at 550 044 800521 S '

MWe to repair a pinhole leak in a socket weld in the low pressure

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steam .;upply line to 1A SCFP between the low pressure stop valve and seat drain to the condenser. .

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3 - 4 I 2 Method: Exhibit G. instructions F: Forced Reason: for Preparation of Data A Equipment Failure (Explain) l Manual S: Scheduled 2 Manual Scram. Entry Sheets for Licensee

. B-Maintenance of Test 3-Automatic Scram. Event Report (LER) File (NUREG-C-Refueling 4-Other (Explain) 0161)

D Regulatory Restriction E-Operator Training & License Examination 5 i

F-Administrative .

Exhibit I .Same Source .

G Operational Error (Explain)

Il-Other (Explain)

(9/77)

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DOCKETNO. 50-348 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT NAME .I. M. Farley , Unit 1 DATE 6/I/80 May NED BY W. C. Hn I m en 111 REPORT MONTH

. TELEPHONE (205) 899-5156' "r_ - '

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- E2 Licensee Action to No. Date E jj k 3.Esd Event m

g Prevent Recurrence

@ g5 & j;g g Repor: # g c5 045 800521 S 28.1 B N/A N/A HH PUMPXX Unit was raised to and held at 700 MWe to complete replacement of IA condensater pump and motor due to bearing failures.

046 - 800531 S 2.7 B N/A N/A HA VALVEX Unit was reduced to and held at 760 MWe for Main Turbine Governor Valve Testing.

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3 4 I 2 Exhibit G-Instructions Reason:

Method:

F: Forced 1 Manual for Preparallon of Dasa S: Scheduled A Equipment Fa.sure(Explain) Entry Sheets for 1.leenses B Maintenance or Test 2-Manual Scram.

3-Automatic Scram. Event Report (1.ER) File (NUREG-C Refueling 0161) 4-Other (Explain)

D-Regulatory Restriction E-Operator Training & Ucense Examination 5

F-Administrative Exhibit 1.Same Source G Operational Error (Explain)

(9/77). II-Other(Explain)

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