ML19318A090

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Monthly Operating Rept for May 1980
ML19318A090
Person / Time
Site: Farley 
Issue date: 06/01/1980
From: Hairston W
ALABAMA POWER CO.
To:
Shared Package
ML19318A089 List:
References
NUDOCS 8006180442
Download: ML19318A090 (5)


Text

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AYERAGECAlLY UNIT POWER LEVEL

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a 50-348

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DOCKET NO.

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1 er 6/1/80 DATE COMPLETED BY W. G. Ilairston, III (205) 899-5156 7

TELEPHONE MONTH May DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)

(MWe. Net) 808 798 g,

37 811 799 2

gg 798 782' 3

g, 652 807 4

y 622 806 5

21 '

g 806 652 22 806 788 7

y

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802 800 g

3 806 796 9

25 800 '

799 10 3

' gg 804 796 W.

3' 790 800 12 28 786 804

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13 29 804 803 34.

803 792 gg 3g 798 I6 INSTRUCTIONS On this formst. list the average dsity unit power level in MWe-Net for each day in the reporting month. Ccmpute ta the nearest whole megawatt.

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OPERATING DATA REPORT DOCKET NO. 50-348-i DATE 6/1/80 COMPLETED BY

_W. G. Hairston, III

. TELEPHONE (205) 899-5156 OPERATING STATUS I. Unit Name.

Joseph M. Farley - Unit 1 Notes 1/Cumulativ'e ifata trince

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2. Reporting Period: -Mav, 1980 12/1/77, date of commercial
3. Licensed ThermalPower (MWr):

2652 operation.

4. Nameplate Rating (Gross MWe):

860

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S. Design Electrical Rating (Net MWe):

d. Maximum Dependable Capacity (Gross MWe):

e

7. Maximum Dependable Capacity (Net MWe):

S. If Changes Occurin Capacity Rstings (Items Number 3 Through 7) Since list Report.Give Reasons:

Maximum Dependable Capacity (Gross MWe and Net MWe) have been determined from operating experience.

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9. Power Level To Which Restricted,If Any (Net MWe): _N/A q
10. Reasons For Restrictions,If Any:

N/A

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II. Hours In Reporting Period 744 '

3.647'

'21.911

12. Number of Hours Reactor Was Critical 744 3,210.6 14,146.1

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13. Reactor Reserve Shutdown Hours 0-436.4 1,841.7
14. Hours Generator On4.Ine 744 3,147.7 13,738.2
35. Unit Reserve Shutdown Hours

- 16. Gross Thermal EnerEy Generated (MWH) 1,927,148.2 7,958,932.5_

34,556,946.9 e

37. Gross Electrical Energy Generated (MWH) 614,696 2,562,364.. 11,086,402

' IS. Net Electrical EnerEy Cenerated (MWH) 583,600 2,421,222 10,469,402

19. Unit Service Factor

.'..2 100.0 86.3 62.7

20. Unit Availability Factoe 100.0 86.3 62.7
23. Unit Capacity Factor (Using MDC Net) 97.6 82.6 59.5
22. Unit Capacity Factor (Using DER Net)

'94;6 80 1.__

97 6,

23. Unit Forced Outage Rate 0.0 3.9 6.6 24.' Shutdowns Scheduled OverNext 6 Months (Type.Date.and Durst" ion of Eacht:'

Refueling Outage, Mid September /Early October 1980, approximately 8 weeks'.

C 25, ifs! ut Down At End Of Report Period. Estimated Dare ofStartup:

N/A

26. Units in Test Status (Prior to Commercial Operation):

Forecast Achieved 1

INITIAL CRITICALITY 8/6/77 I

8/9/77 INITIAL ELECTRICITY 8/20/77 8/18/77 COMMERCIAL OPERATION 12/1/77 12/1/77

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50-348 UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKETNO. 7* n. Farley - Unitb'i UNIT NAME

"# 'I N DATE W. G. tiairston, III COMPLETED BY TELEPHONE (205) 899-5156 REFORT MONTH May Tee Cause & Corrective

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License,.

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No.

Date k

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Event g'g

$5 j;2 g Report #

mO EO Prevent Recurrence F

g S

039 800503 S

2.7 B

N/A N/A HA VALVEX Unit was reduced to and held at 775 MWe for Main Turbine Governor Valve Testing.

040 800510 S

2.8 B

N/A N/A HA VALVEX Unit was reduced to and held at 770 MWe for Main Turbine Governor Valve Testing.

041 800511 F

0.5 D

N/A 80-031/03L-0. ID INSTRU Unit was ramping down to be taken off line in compliance with the Technical Specification for loss of Data Cabinets A and B Direct Rod Position Indication. At 782 MWe, one channel of the DRPI was restored and ramp-down terminated.

3 4

i 2

Method:

Exhibit G Instructions F: Forced Reason:

S: Scheduled A Equiprnent Failure (Explain) l-Manual for Preparation of Data B Maintenance of Test 2 Manual Scram.

Entry Sheets for Licensee 3-Automatic Scram.

Event Report (LER) File (NUREG-C-Refueling D Regulatory Restriction 4-Other (Explain) 0161)

E Operator Training & License Examination 5

F Administrative Exhibit I-Same Source G Operational Error (Explain)

(9/77)..

Ilother(Explain)

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50-348

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DOCKET NO.

UNITSilUTDOWNS AND POWER REDUCTIONS UNITNAME

.l. M. Farley - Unit I DATE 6/1/80 W. 6 Ha uston, m NL.ETED BY REPORT MONTH May TELEPHONE (205) 899-5156 Y )U E

Licensee Ee Cause & Corrective Eg

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}YsM Event y

Action tu No.

Date k

jg g5 5

j gij g Repor: #

mu Prevent Recurrence g

6

'042 800512 S

6.9 B

N/A N/A HH XXXXXX Unit was reduced to and held at 700 MWe to repair a lube oil gasket leak on 1C condensate pump.

043 800519 S

40.8 B

N/A

~N/A HH PUMPXX Unit was reduced to and held at 700 MWe to replace 1A condensate pump and motor due to excessive vibration.

l 044 800521 S

5.0 B

N/A N/A CH PIPEXX Unit was reduced to' and held at 550 MWe to repair a pinhole leak in a socket weld in the low pressure

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steam.;upply line to 1A SCFP between the low pressure stop valve and seat drain to the condenser.

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3 4

I 2

Method:

Exhibit G. instructions F: Forced Reason:

l Manual for Preparation of Data S: Scheduled A Equipment Failure (Explain) 2 Manual Scram.

Entry Sheets for Licensee B-Maintenance of Test 3-Automatic Scram.

Event Report (LER) File (NUREG-C-Refueling 4-Other (Explain) 0161)

D Regulatory Restriction E-Operator Training & License Examination 5

i F-Administrative Exhibit I.Same Source G Operational Error (Explain)

(9/77)

Il-Other (Explain)

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DOCKETNO. 50-348 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT NAME

.I. M. Farley, Unit 1 DATE 6/I/80 NED BY W. C. Hn I m en 111 REPORT MONTH May

. TELEPHONE (205) 899-5156' "r_

5, c,,,,, c,,,,c,,,,

b No.

Date E

jj k

3.Esd Licensee E,

E2 Action to Event g

Prevent Recurrence g5 j;g g Repor: #

m g

c5 045 800521 S

28.1 B

N/A N/A HH PUMPXX Unit was raised to and held at 700 MWe to complete replacement of IA condensater pump and motor due to bearing failures.

046

- 800531 S

2.7 B

N/A N/A HA VALVEX Unit was reduced to and held at 760 MWe for Main Turbine Governor Valve Testing.

1 l

I 2

3 4

Method:

Exhibit G-Instructions F: Forced Reason:

S: Scheduled A Equipment Fa.sure(Explain) 1 Manual for Preparallon of Dasa B Maintenance or Test 2-Manual Scram.

Entry Sheets for 1.leenses 3-Automatic Scram.

Event Report (1.ER) File (NUREG-C Refueling D-Regulatory Restriction 4-Other (Explain) 0161) i E-Operator Training & Ucense Examination 5

F-Administrative Exhibit 1.Same Source G Operational Error (Explain)

(9/77).

II-Other(Explain) l

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