ML19317G337

From kanterella
Jump to navigation Jump to search
RO-77-36:on 770415,chemical Addition Valve CAV-2 & Makeup Valve MUV-258 Failed to Close During Performance of SP-370. Caused by Weak Closure Spring & Corroded & Dirty Contacts. Contacts Cleaned & Spring to Be Renewed
ML19317G337
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 05/09/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19317G332 List:
References
NUDOCS 8002280941
Download: ML19317G337 (2)


Text

a N 6.a.w w a Lv a=8 4 es a L.s e e e i

CONTROL OLOC-l l

l l

l l

[pttAst PRINT ALL RCOUIRED INFORM AT;.,

e LEENSEE e

NAME LCENSE EVENT i

[

lL l Cl Rl Pl 3l.

LCENSE NUMDER l1l1l1l l0 l3 l TYPE TYPE l 0 l 0-l-l 0l 0l 0l 0l 0l-l 0l 0l l4l1 C /D 14 15 25 CU 30 31 32 CAftConY TYPE t

ooCKET NUMDER EVENT oAfg REPORT oATE h CON'T l - l - l l Ll l0l5l0l-l0l3l0l2l l0 l4 l1 l 5l 7l 7l l 0 l5 l0 l9 l7 l7 7 6 57 60 59 GU G1 G8 GD 74 75 EVENT DESCRIPTION o

l In Mode 1 operation performing SP-370, Containment Isolation Valves CAV-2 and MUV-258 7 09 t

@l failed to close contYary to Technical Specification 3.6.3.1.

Redundant valves were avail-7 89 a

@l able and operable.

First occurrence of this type.

CAV-2 will be restored operable on 7 09

@l next outage. MUV-258 restored operable 15 April 1977.

7 09

@l (LER-77-36) 7 o9 pn,,,,

t SYSTEM CAUSE COMPONENT COMPONEN T CODE CODE COMPONENT CoOE SUPPULH MANUFACTUACR VOLATON

@ l Sl Dl lE l lVlA}LlVlElXl l Al lR l3 l 4l 0l lNl 7 00 10 11 12 17 43 44 47 48 CAUSE DESCn:PTION 0

oo l MUV-258 inoperable due to dirty control contacts.

Contacts cleaned and valve restored 7 89

@l operable.

CAV-2 closure spring not strong enough to effect closure. Will restore 7 ao bl operable next scheduled outage.

FACILTTY METHoo oF

\\ /

STATUS

% POWER oTHER STATUS o4CoVERY DISCOVERY oESCRIPTON Q

lEl l__0 l 8 ) 6 l l

N/A l d l

N/A 70 9

10 12 13 44 45 46 el ACTMTY CodTENT hfLEASED of f lLE ASE l AMOUNT oF ACTMTY Q

lZl LOCATION oF RELEASE W

N/A l

l N/A 7 0 D

10 11 44 45 0;

P[nSONNEL EXPOSunES NUMDER TYPE oESCRIPflotJ

@ l0l0l0l Wl N/A 7 89 11 12 13 6.

PERSONNEL INJunlES

- iUMDE R DESCFhPTioN 10l0l0l l

N/A 1

j 7 0D 11 12 0;

OFFSITE CONSEQUENCES I

gg l N/A 7 UU U:

LOSS On DAMAGE TO FACtllTY TYPE oESCA:PfloN

@Wl N/A l

7 89 10 la!.

PUBLtCITY 3l

~ N/A l

7 00 P.

SulTIONAL FACTOnS 8002 280 9W See attached Siipplewntary In fo rmat i on l,

7 00

~ i,[,

81 74 l,

7 nu

,r Naur:

% tu.t cuan

y I

,lo l

n,0Ne_ (.in) a66-4 nt

pi SUPPLEMENTARY INFORMATION

- g )

1.

Report No:

50-302/77-36 2.

Facility:

Crystal River Unit #3 3.

Report Date:

9 May 1977 1

4.

Occurrence Date:

15 April 1977 5.

Identification of occurrence:

Chemical Addition Valve CAV-2 and Make-Up Valve MUV-258 inoperable contrary to Technical Specification 3.6.3.1.

6.

Conditions Prior to Occurrence:

Normal Mode 1 operation.

7.

Description of Occurrence:

At 0600 while performing the quarterly cycling of power-operated con-tainment isolation valves, Surveillance Procedure SP-370, CAV-2 and MUV-258 failed to close from the Control Center.

Redundant isolation valves were available and operable. MUV-258 was restored operable within 4

[h hours. CAV-2 was manually isolated and will be repaired at the next g,,/

scheduled outage.

]

8.

Designation of Apparent Cause of Occurrence:

Corr.oded and dirty contacts for MUV-258.

Closure spring for CAV-2 not strong enough to close valve.

)

9.

Analysis of Occurrence:

There were no safety implications because of this occurrence as there were redundant valves available and operable.

10.

Corrective Action:

1 Contacts.ior MUV-258 were cleaned and valve restored operable. Preventive Maintenar :e Program should prevent recurrence.

Closure spring for CAV-2 will.be i inewed on next scheduled outage.

11.

Failure Data:

This was a non-repetitive occurrence.

I v

c

- - -