ML19317G227
| ML19317G227 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 08/03/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19317G224 | List: |
| References | |
| NUDOCS 8002280860 | |
| Download: ML19317G227 (2) | |
Text
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g,, LEA;E p AINT ALL RtOutRE2 INFORMAT:C.
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6 UCENSEE*
LCENSE EVENT NAME UCENSE NUMBER TYPE TYPE l Fli, l Cl R l P l 3 l l0 l0 l-l0 l 0 l 0 l 0 l 0 l-l 0 l 0 l l 4 l1 l1 l1 l 1l l0 l3 l 7 89 14 15 25 26 30 31 32 T7PE CATEcoRY So CoCXET NUMBER EVENT oATE REPORT cATE O 1 CONT l _ l _ l lLl lLl lo l5 lo l-l0 l3 lo l? l l0 l 7l 1l 1l 7 l 7 l l0 l8 l0 l3 l7 l7 7 8 57 58 SS 60 61 68 69 74 75 E
EVENT DESCRIPTICN gg l In reviewing' previous shift logs, Chem / Rad personnel discovered that a power change 7 89 E-gg { greater'than 15% per hour had been completed without analyzing the DE-I 131 as required 7 89 S
g l by Table 4.4-8 of Tech Spec 4.4.8.
Redundancy NA.
This event was not repetitive.
7 89 E
g l Changes to operating procedures dealing with power changes have been initiated to ensure prompt notification of Chem / Rad personnel upon a power change greater than'15% per hour.
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'SE" ca"oE "sE E IcdER 7 - 0) couPoNENT coat vouroN o
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l Nl 7 89 10 11 12 17 43 44 47 48 CAUSE DESCR:9 TION
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2 oe l The cause of this event was deternined to be a procedural inadequacy in that the operating 7 89 6.
O9 l procedures dealing with power changes did not refer i:o the Special Condition Surveillance 7 89 8:
] [rocedure SP-442. The Op's will be changed to ensure notification.
% POWER oTHER STATUS o
VERY oGCoVERY oESCRIPTON
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NA 1
70 9
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o o f ASE AMcVNT oF ACTMTY LoCATEN cF RELEASE
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CC PERSONNEL EXPOSURES NUMBER TYPE CESCRaPTON gg l 0 ] 0 l 0l y[
NA 7 89 11 12 13 6C PERSCNNEL INJURIES NUMBER DESCRIPTON E l0l0l0l l
N'A 7 89 11,12 6C OFFSTTE CONSEQUENCES 1
l NA 7 89 8t LOSS OR DAMAGE TO FAC:UTY Type cESCRPTON L:J l
1 n
7 89 10 LC PUBUCITY Ql NA 7 89 bC 8002280 860 N ADDITIONAL FACT. RS
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1o l See Attached Supolecentarv Information 3
7 89 HL W. P. Stewart (813) 866-4159 NAME:
PHONE:
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0 SUPPLEMENTARY INFORMATION
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1.
Report No.
50-302/77-78 2.
Facility:
Crystal River Unit #3 3.
Report Date:
3 August 1977 4.
Occurrence Date:
11 July 1977 5.
Identification of Occurrence:
Failure to analyze Dose Equivalent Iodine 131 upon a power change greater than 15%
within a one hour period contrary to Table 4.4-8 of Technical Specification 4.4.8.
6.
Conditions Prior to Occurrence:
Mode 1 power operations.
7.
Description of Occurrence:
At 1130 when reviewing turnover from the previous shift, the chief Chem / Rad technician discovered that the DE-I 131 was not analyzed upon a power change of 30%
~
within one hour. The Chem / Rad personnel were not notified of the power escalation as required by the special condition surveillance plan SP-442. The analysis was immediately initiated and analyses were made upon subsequent power changes, substantiating the DE-I 131 remained within acceptable limits.
g Designation of Apparent Cause:
The cause of this occurrence is attributed to procedural inadequacies in that the Chem / Rad personnel were not notified of power escalation.
9.
Analysis of Occurrence:
During power escalations the Iodine spiking phenomena can cause DE-I 131 to exceed the allowable Tech Spec limits.
10.
Corrective Action:
Changes to the operating procedures dealing with power changes have been initiated to insure notification of Cham / Rad personnel upon power level changes greater than 15%/ hour.
11.
Failure Data:
This is the first occurrence of this event.
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