ML19317G221
| ML19317G221 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 08/03/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19317G217 | List: |
| References | |
| NUDOCS 8002280855 | |
| Download: ML19317G221 (2) | |
Text
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LICEhiEIEE EVENT REPORT i{
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[pLEASE PRIfJT ALL PEQUtntD INFCRT.1AT;O7;;
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S NAME LCENSE NUMBER TYPE lFl} lCl Rl Pl 3l l 0 l 0-l-l 0 l 0 l 0 l-0 l 0 l-l O l 0 l l 4l 1l 1l ll 1l l0l3l 7 09 14 15 25 25 30 31 32 CATECORY TYP O
00CMET NUMOER EVENT CATE REPORT oATE D 1 CONT l - l - l lL l lL l l 0 l 5 l 0 l-l 0 l 3 l 0 l 2 l l 0 l 7 l 0 l8 l7 l7 l l0 l8 l0 l 3 l7 l7 l 7 8 57 50 59 60 61 68 69 74 75 00 EVENT OESCRIPTION Ql During calibration of the Fisher gas chromatograph, the 1 and 4 volume percent hydrogen l
7 89 e
Q[ balance nitrogen did' not meet the acceptance criteria required by Tech Spec 4.6.4.1.
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l Redundancy was maintained as the H2 analyzer was available and operable. This was the l
7 89 00 05 l first occurrence of this event. A replacement separation colu=n was ordered and the l
7 U9 gl chromatograph was restored operable.
(LER 77-79) 7 89 60 E
00E COMPONENT COCE A
MAP UA R VCLAICN lPlBl l,,,,Ej lXlXlXlXlXlXl lN l l Zl 9 [ 9 l 9 l lN [
O 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION
- *s ldTEl l This occurrence was caused by the loss of resolution of the chromatograph's separation y
7 89 OO l column. A replacement column will be maintained at all times to ensure timely l
7 7
80 corrective action.
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FAC:UTY METHoo oF STATUS 4 POWER oTHER STATUS DISCOVERY DISCoVERf CESCRPTON
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l 1l 0l 0l l NA l
l Cl l
NA l
ss 70 9
10 12 13 44 45 46 c0 ACTMTV CONTENT RELEASEo OF RELEASE l AMOUNT CF ACTMTY.
LoCATCN OF RELEASE lZ l lZj NA l
l NA l
7 0 0
10 11 44 45 80 PERSONNEL EXPOSURES NUM0ER TYPE CESCRIPTCN III3l l0 l 0l 0l
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NA l
7 09 11 12 13 60 PERSONNEL INJUPIES NUM0E R DESCR.PTON 3 l0l0l0l l
NA l
7 8D 11 12 60 OFFSITE CONSEQUENCES 7 00 00 LOSS OR OAMAGE TO FACILITY T Yl'E CESCRPTCN
$dl NA l
7 8D 10 LU PUBUCITY
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..g DITIONAL FACTORS See attached Suppletanntarv Information 8 002 2H
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7 oo nu NAME:
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P. St?# art PHONE: -(813) 866-4159 an.u,.,
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SUPPLEMENTARY INFORMATION 1.
Repdre No.:
50-302/77-79 2.
Facility:
Crystal River Unit #3 3.
Report Date:
3 August 1977 4.
Occurrence Date:
8 J917 1977 5.
Identification of Occurrence:
Inoperability of gas chromatograph contrary to Technical Specification 4.6.4.1.
6.
Conditions Prior to Occurrence:
Mode 1 power operation.
7.
Description of Occurrence:
At 2150 the Fisher gas chromatograph failed to meet the calibration acceptance i
criteria as required by Technical Specifications. The 1 and 4 volume percent hydrogen, balsace nitrogen calibration would not meet the requirements due to apparent separation column degradation resulting in a loss of resolution. A replacement separation column was ordered and the gas chromatograph has been restored operable.
B,, Designation of Apparent Cause:
The cause of this event was the failure of the colum to perform its intended function.
9.
Analysis of Occurrence:
The safety and health of the plant and public were not affected as a redundant hydrogen analyzer was available and operable.
10.
Corrective Action:
A spare separation column will be maintained at all times in order that corrective action can be accomplished in a timely manner.
11.
Failure Data:
This was the first occurrence of this event. It was the second occurrence of the inoperability of this device. Refer to LER 77-72.
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