ML19316A631

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Forwards Request for Addl Info from Util Re Fsar.W/O Encl
ML19316A631
Person / Time
Site: Oconee  
Issue date: 02/24/1972
From: Van Niel C
US ATOMIC ENERGY COMMISSION (AEC)
To: Peltier I
US ATOMIC ENERGY COMMISSION (AEC)
References
NUDOCS 8001130149
Download: ML19316A631 (1)


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Febrta ry 21, 1972 4

I. A. Peltier, NR Branch f*, DE THIU:

D. Tho:rpsen, Chief, OSB, DE EEVIN OF FINAL SAFE 1T /dALYSIS IEPORT FOR THE OCONEE NUCLEAR STATION UNIIS 2 & 3 (IXXZET NOS.

% -270 & 50-287)

I have conducted a review of the FSAR for Ocones 2-3 in the areas of Conluct of Operations, ani the Aininistrative Controla section c2 the Technical Specifiestions. The encicsure identifies the additional information that vill be required of the applicant in crder to cc:splete i

I the review in these areas.

Y C., R. Van Niel i

Operational Safety Branch, DE

Enclosure:

Additicnal Information Ibgaested cc:

D. J. Skovholt, DE A. Schwencer, DE i

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NaC f onu xs EXHIGIT A (1<11l LICENSEE EVENT REPORT l

IPLEASE PRINT OR TYPE ALL REculatD IN8oRVAf t0N)

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EVENT DESCaiPTioN AND P AcS ABLE CoNSEOuENCES h It was determined that thej f oTil 10n April 6,1978, the RC leak rate exceeded 1 gpm.

l o 121 l Icak was primarily a packing leak on 2RC-3, the Spray Control Block Valve, j

line root valve were repacked.

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l o 141 I the valve and an instrument The weld was t o is j 1 another leak was discovered in the pressurizer heater bundle.

jirepaired and the unit returned to service on April 22, 1978. No adverse io lo lil I ef f ects resulted since all leakage was contained and no loss of RCS capabilityg l

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Ii la i l The valve leaks were a result of blown packing.

li li j l bundle leak was caused by a flange seal weld f ailure evidently initiated i

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during startup after the valve repairs.

I g,,,3 i g l flange was re-welded to repair the leaks.

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