ML19312C224

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RO 269/76-13:on 760810,penetration Room Valve PR-2 Found Inoperable.Caused by Ruptured Diaphragm in Air Supply Exhauster.Valve PR-2 Repaired & Tested
ML19312C224
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 09/09/1976
From:
DUKE POWER CO.
To:
Shared Package
ML19312C218 List:
References
RO-269-76-13, NUDOCS 7912100701
Download: ML19312C224 (1)


Text

_.-

Regulatorj Decket SLe DUKE POWER COMPANY OCONEE UNIT 1

'c:#..! ct NJ Report No.:

R0-269/76-13 Report Date:

September 9, 1976 Occurrence Date: August 10, 1976 qg, Facility:

Oconee Unit 1, Seneca, South Carolina Identification of Occurrence: Penetration room valve PR-2 discovered inoperable Conditions Prior to Occurrence:

Unit at 75 percent full power Description of Occurrence:

On August 10, 1976, prior to purging the Reactor Building, penetration This vi.ve, which is located l

room valve PR-2 was discovered inoperable.

outside the Reactor Building in the purge piping, provides containment isolation following an ES actuation.

Valve PR-2 failed in the intermediate position and could not be cycled to a fully-open or fully-closed position.

Prior to investigation of the problem, valve PR-2 was immediately isolated by locking closed redundant valve PR-1 located inside the Reactor Building pursuant to Technical Specification 3.6.4.b.2.

7 Designation of Apparent Cause of Occurrence:

PR-2 is an air-operated valve.

The exhauster in the air supply, which removes air when the valve is closed, contained a ruptured diaphragm resulting in insufficient air pressure to activate the valve.

Analysis of Occurrence:

Valve PR-2 was properly isolated in compliance with Technical Specification 3.6.4.b.2 by securing redundant valve PR-1 in the closed position.

In the event that containment integrity had been required prior to securing valve PR-1, valve PR-1 would have closed upon an ES actuation.

There have been no previous defects in valve exhauster diaphragms. This failure is, therefore, considered a random occurrence and not an indication of a generic problem.

Containment integrity was not affected by this incident and it is, thus, concluded that the health and safety of the public were not affected.

Corrective Action:

Valve PR-2 has been repaired and its operability verified.

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