ML19309B924

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LER 80-012/01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby
ML19309B924
Person / Time
Site: Beaver Valley
Issue date: 03/31/1980
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309B921 List:
References
LER-80-012-01T, LER-80-12-1T, NUDOCS 8004070346
Download: ML19309B924 (1)


Text

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EVENT DESCRIPTION ANO PROBABLE CONSEOUENCES h I"oTF1 o IThe emergency shutdown panel Auxiliary Feedwater Flow instrumentation readings were l p573-] l deleted f rom surveillance testing due to the meter indication always reading zero, l in ja l lduring power operation. There were no implications to the health and safety of the i I o l s j Igeneral public because the shutdown panel was not needed or used. I l

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JS Jta JJ 40 el 42 44 47 CAUSE CESCRIPTION AND CORRECTIVE ACTIONS h I i l o l lThe surveillance test readine was removed from the data sheet because, during power I b .

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i,i,iIthe future, the flow indicator checks will be done during startup when the pumps are i

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