05000334/LER-1980-012-01, /01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby

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/01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby
ML19309B924
Person / Time
Site: Beaver Valley
Issue date: 03/31/1980
From: Werling J
DUQUESNE LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309B921 List:
References
LER-80-012-01T, LER-80-12-1T, NUDOCS 8004070346
Download: ML19309B924 (1)


LER-1980-012, /01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby
Event date:
Report date:
3341980012R01 - NRC Website

text

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.4 JS REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEOUENCES h I"oTF1 IThe emergency shutdown panel Auxiliary Feedwater Flow instrumentation readings were l o

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