ML19308D528

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RO-77-33:on 770406,absolute Position Indicator for Rod 5, Group 8 Failed.Caused by Amphenol Connector Faulty Pin Connection.Connector Repaired & Indicator Restored to Operation
ML19308D528
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/28/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D524 List:
References
NUDOCS 8002280966
Download: ML19308D528 (2)


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EVENT OESCniPTION I

HE l Normal Mode I operation, inoperable position indicator for Rod 5. Group 8 ( ASPR's) con-7 09 60 !

l l HE I trary to Technical Specification 3.1.3.3.

No redundant systems available.

First occur-7 89 80 C4 l rence of this type.

Complied with Technical Specification Action Statement 3.1.3.3.A.2.B. l l 7 89 60 !

hl System restored operable on 8 April 1977.

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@l Inoperable absolute position indicator caused by amphenol connector faulty oin connection. I 7 89 00 3l l Connector was repaired and operability restored.

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O!TIONAL FACTORS See attached Supplementarv Information

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SUPPLEMENTARY INFORMATION 1

1.

Report No.:

50-302/77-33 2.

Facility:

Crystal River Unit #3 3.

Report Date: 28 April 1977 4.

Occurrence:

6 April 1977 5.

Identification of occurrence:

In the process of moving Group 8, Axial Power Shaping Rods (APSR's),

the absolute position indicaor for Rod 5 failed causing a condition contrary to Technical Specification 3.1.3.3.

6.

Conditions Prior to Occurrence:

Normal Mode I operation.

7.

Description of Occurrence:

2 At 0812, while adjusting a power imbalance wit! Group 8 Rods, absolute pcsition indicator for Rod 5 failed. Rod posi*. ion was verified by the Rod Zone Limit Switch. Commenced logging position agreement between r

reference indicator and the operable position indication as per SP-300.

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Position indicator for Rod 5 was restored operable during shutdown on 8 April 1977.

8.

Designation of Apparent Cause of Occurrence:

The amphenol connector to the position indicator was found to have a faulty pin connection.

9.

Analysis of Occurrence:

There were no safety implications as the Reactor could have been safely shut down at any time.

10.

Corrective Action:

The amphenol connector was repaired and absolute position indicator for Rod 5 of Group 8 was restored operable.

11.

Failure Data:

This occurrence wat non-repetitive for the APSR group.

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