ML19308D522

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RO-77-32:on 770404,while Reducing Power for Maint,Rod 6 of Group 7 Failed to Move.Caused by Control Rod Drive Mechanism Blown Fuse Due to Control Stator Failure.Stator & Fuse Renewed
ML19308D522
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/28/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D521 List:
References
NUDOCS 8002280961
Download: ML19308D522 (2)


Text

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,1 CCNTROL ULOCK:l l

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[PLCASS PntNT ALL RCouinED INTOlk.1AT:~

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Yv',"E ucENsE NUMern e!'lclnlpl1l l 0 l 0 l-l 0 l 0 l 0 l 0 l 0 l-l 0 l 0 l l4 l 1 l1 l1 l1 l l0 l3 l 7 09 14 15 25 as 30 31 32 "v7pf 3oM CAftcony coexET NUMutR EVENT DATE REPCAT DATC 0 1 CONT l - l - l W l Ll l 0l 5l 0l-l 0 l 3l 0 l 2 l l 0 l 4 l0 l4 l7 l7 l l 0 l 4 l2 l8 l7 l7 7 0 57 50 SS 60 61 68 69 74 75 UL EVENT DESCRIPTION O

l Reducine newer for maintenance Rod 6. Crono 7 would not move contrary to Technical 7 09 6L EE l Soecifiestion 3.1. 3.1. C.

There were no redundant systems available.

First occurrence 7 89 at EE l of this ern e.

System restored operable by renewing CRDM stator.

7 89 03 l BC

? U9 SC c l (1.ER-77-32) 7 03 mg 6C.

cbcE cooE ccMPCNENT CCOE A

VOLATON

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lD l1l5l0l lN l 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION

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@l Failure of CRDM stator caused control fuse to blow making Rod 6, Group 7 inoperable.

l 7 89 GG hl Maintenance restored Rod 6 operable prior 'to plan't startup.

l 7 19 80 I

l FAC&lTV METH00 CF STATUS

% POWER OTHER STATUS OtSCOVtAY CISCOVERY OESCRPf;GN 8

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70 9

10 12 13 44 45 46 CO AYENc3 07 f SE AMCUNT Of ACTMTY LOCATCN OF RELE4.SE 8

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7 8 9

10 11 44 45 e0 PERSONNEL EXPOSURES NUMBER TYPE OLSCRIPTON 13 l0 l 010 l lzl l

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7 89 11 12 13 00 PERSONNEL INJURIES NUMOCR CEScnrPTON h l0 l0 l0l l

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7 09 11 12 00 OFFSITE CONSEQUENCCS 1

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7 09 UD LOSS On OAMAGE TO TACiUTY TYPE D

@ W l EECTtPTCN N/A l

7 u9 to c0 PUOttC11y 3l N/A j

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- &10lTIONAL FACTOn3 See attached Supolementarv Information l-

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Wi P. Stewart

.l rHONt: (813) AM _41 =o

SUPPLEMENTARY INFORMATION 1.

Report No:

50-302/77-32 2.

Facilitv:

Crystal River Unit #3 3.

Raport Date:

28 April 1977 4.

Occurrence Date:

4 April 1977 5.

Identification of Occurrence:

In the process of reducing power with Control Rod Group 7, Rod 6 of this group would not move contrary to Technical Specification 3.1.3.1.C.

6.

Conditions Prior to Occurrence:

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Plant was reducing power in Mode I.

7.

Description of Occurrence:

At 1055, while reducing power for planned maintenance, Rod 6 of Group 7 was found to be inoperable. Manual movement of Rod 6 was attempted with no success. Trouble-shooting revealed that the fuse controlling Rod 6 was blown. Further investigation revealed the stator for Rod 6 CRDM had failed. The plant was shut down and after maintenance, Rod 6, Group 7 demonstrated and declared operable.

8.

Desianation of Apparent Cause of Occurrence _:

The primary cause of this event was the CRDM stator had failed which in turn caused this mechanism's fuse to blow, causing Rod 6 of Group 7 to become inoperable.

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1 9.

Analysis of occurrence:

l There were no safety implications as the Reactor could have been safely shut down at any time.

10.

Corrective Action:

l The CRDM stator and control fuse were renewed and Rod 6 of Group 7 was restored operable.

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Failure Data:

This occurrence was non-repetitive.

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