ML19308D379

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RO-77-46:on 770514,hydraulic Snubber MUH-44 Found Inoperable.Caused by Missing Cotter pin.MUH-44 Renewed W/ Functionally Tested Spare Snubber & SP-201 Revealed Other Snubbers Operable
ML19308D379
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 06/03/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D371 List:
References
NUDOCS 8002270830
Download: ML19308D379 (2)


Text

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NAME LCENSE NUMOEA TYPE

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CAftConY uoCRET NUMOEA EVENT CATE AEPCnr care h CON'T l _ l _ l QJ l1l l 0l 5l 0l-l 0l 3l 0l 2l (0 l5 l 1l 4l 7l 7l l0l6l0j3l7l7 7 u 57' bu bil 60 b) 66 69 74 7b u

EVENT OtSCnt!

l La flode 5,'il0N Cold Shutdown, in the process of performing the llydraulic Snubber Inspection g

7 09 l SP-201, liydraulic Snubber MUH-44, located on 2-1/2" H.P.

injection line in the Reactor 03 7 89 3-g l Bldg., was discovered inoperable contrary to Technical specification 3.7.9.1.

7 89 a

Q l Redundancy N/A.

First occurrence of this type.

MUH-44wasrenewedwithafunctionally'\\

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O5 l tested spare and restored operabia within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

(LER 77-46) l 7 8,9 Paua 6'

SYSitM CAUSE COMRJNENT COMPONENT C00E CCCE COMPONENT Co0E SUP8UEA MANuFaCTuf4A VOLATCN japj l W l C l l Fl l H j Al Nl Cl El Rl l Al lPj3l1l ]

lNl 7 89 10 11 12 17 43 44 47 48 q

CAUSE DESCRIPTION O

q l The cotter pin that connects the snubber eye to the pipe clamp was missing due to j

7 09 00 l conditions unknown at this time.

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I 89 FACAi1Y METHCo CF status

% POWEA OTHER STATUS DISCOVERY DISCOVERY DESCA#TCN lC l l 0l 0l 0l l N/A l

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10 12 13 44 45 46 80 ACTm TY CosfENT AELEASEO oFAELEASEl AMOUNT OF ACTMTV LCCATCN OF AELEASE b

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10 11 44 45 80 PERSGNNEL EXPOSURES NUM8EA fvpt OESCR@ TON 113 l 0l 0l 0l lZl l

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7 89 11 12 13 60 PERSONNEL INJURIES NuMOER DESCMGTON DE l 0l 0l 0l l

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7 89 11 12 60 OFFSITE CONSEQUENCES 3

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7 09 00 LOSS OR OAMAGE TO FAC:UTY k, f twE cEsCn PrCN Ql N/A 1

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W PusuCITY N/A Q'

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.l 17 7 00 L"I AOCITIONAL FACTORS g l See attached supplementary information

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W. P. Stewart

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SUPPLEMENTARY INFORMATION

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ss_s 1.

Report No.:

50-302/77-46 2.

Facility:

Crystal River Unit #3 3.

Report Date:

3 June 1977 4.

Occurrence Date:

14 May 1977 5.

Identification of occurrence:

Hydraulic Snubber MUH-44 inoperable contrary to Table 3.7-3 of Technical Specification 3. 7.9.1.

6.

Conditions Prior to Occurrence:

In Mode 5, Cold Shutdown, performing SP-201.

7.

Description of Occurrence:

o At 1400, in the process of performing the Hydraulic Snubber Inspection SP-201, Snubber MUC-44, located on the 2-1/2" H.P. injection line in the Reactor Building, was discovered disconnected from the snubber eye to the pipe clamp. The snubber ss removed and renewed with a functionally tested spare. MUH-44 was restored operable within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

8.

Designation of Apparent Cause of Occurrence:

The cocter pin that connects the snubber eye to the pipe clamp was missing. The reason for the missing cotter pin is unknown at this time.

4 9.

Analysis' of Occurrence:

There were no safety implications to the plant or public other than the loss of pipe restraint capabilities of MUH-44.

10.

Corrective Action:

MUH-44 was renewed with a functionally tested spara snubber and SP-201 revealed other _ snubbers operable.

i 11.

Failure Data:

This was the first occurrence of this type.

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