ML19308D322

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RO-77-21:on 770225,main Steam Valve MSV-36 Opened at 990 Psig Following Reactor Trip.Mainsteam Valve Lifted Due to Setpoint Drift.Main Steam Valve Calibr to Correct Lift Setpoint
ML19308D322
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 03/14/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D321 List:
References
NUDOCS 8002270769
Download: ML19308D322 (2)


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@l MSV-36 Relief Valve lifted due to reasons that are unknown at this time as the balance l

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@l of the Relief Valves did not open.

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I Supplementary Information

1.. Report No:

50-302/77-21 l

2.

Facility:

Crystal River Unit #3 3.

Report Date:

14 March 1977 4.

Occurrence Date: 25 February 1977 l!

5.

Identification of occurrence:

i Main Steam Relief Valve MSV-36 lifted at a pressure of 990 psig. The required setpoint is 1050 peig i 1%.

6.

Conditions Prior to Occurrence:

On 25 February 1977, Crystal River Unit #3 experienced a Reactor trip, t

and the Unit was returning to Mode 4 (Hot Shutdown).

7.

Description of Occurrence:

While enteri:2g Mode 4, following a Reactor trip, the Main Steam Relief Valve MSV-36 opened below the required setpoint. No other Main Steam j

Relief Valves opened at this time. There was no safety significance, i

as the Reactor was in a tripped condition at the time of the occurrence..

I The balance of the MSV's were operable and redundancy was maintained.

When the steam pressure decreased to a point below the MSV setpoint, the setpoint was checked and reset.

8.

Designation of Apparent Cause of Occurrence:

The cause of this occurrence ras determined to be a normal setpoint drift.

9.

Analysis of Occurrence:

This was the first occurrence of this event involving a Main Steam Safety Valve. When plant conditions allowed, the valve was calibrated to the proper setpoint.

10.

Corrective Action:

Main Steam Ralief Valve MSV-36 was calibrated to the correct lift setpoint of 1050 psig i 1%.

I 11.

Failure Data:

No previous events of this type have occurred.

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