ML19308D146

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RO-77-62:on 770630,eight Hr Time Limit for Reduction to Less than 60% Thermal Power Exceeded.Caused by Personnel Error. Personnel Instructed to Heed Time Limits More Conservatively
ML19308D146
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 07/07/1977
From: Stewart W
FLORIDA POWER CORP.
To:
Shared Package
ML19308D108 List:
References
NUDOCS 8002270624
Download: ML19308D146 (2)


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'/ 18 L7 LU LD 00 61 G8 09 74 73 ti EVENT O!:SCTcI'llON l3t-) l In Modo 1, reducing power to less than 607, thermal power, as required by Technical f uu il

@l Specification Action Statement 3.1.3.3.A.1, the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> time limit was exceeded by 7 il 9 Eh hl one hour and seven minute s.

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SUPPLEMEffrARY INFORMATION J

1.

Report No.:

50-302/77-62 2.

Facility:

Crystal River Unit #3 3.

Report Date:

7 July 1977 4.

Occurrence Date:

30 June 1977 5.

Identification of Occurrence:

Exceeded the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> time limit for reduction to less than / % thermal power as required by Technical Specification Action Statement 3.1.3.3. A.1.

6.

Conditions Prior to Occurrence:

Verifying the position of Rod 3, Group 6 as required by Technical Specification f-3.1.3.3, upon loss of the absolute position indication.

7.

Description of Occurrence:

As a result of loss of absolute position indication of Control Rod 3, Group 6, power reduction to less than 60% thermal power was required to be achieved within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> by Technical Specification Action Statement 3.1.3.3.A.1.

Be-cause of several minor difficulties af ter the initiation of power reduction, the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> time limit was exceeded by I hour and 7 minutes. At that time (0600),

the Action Statement was met except for the time interval. Conditions surround-ing absolute position indication failure will be reported as a 30 day written report prior to 30 July 1977.

8.

Designation of Apparent Cause:

This event was a result of operator failure to anticipate the potential for equipment problems which retarded power reduction to less than 60% in the re-quired time frame.

9.

Analysis of Occurrence:

There was no safety related significance to this event.

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10.

Corrective Action:

Operations personnel were instructed to heed Technical Specification requirements as to time frame limits more conservatively and take necessary steps to insure these time limits are met.

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This event was non-repetitive.

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