ML19308C002
| ML19308C002 | |
| Person / Time | |
|---|---|
| Site: | Crane, Davis Besse |
| Issue date: | 12/19/1978 |
| From: | Creswell J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Fiorelli G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| References | |
| TASK-TF, TASK-TMR NUDOCS 8001170743 | |
| Download: ML19308C002 (2) | |
See also: IR 05000346/1978006
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December 19, 1978
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Docket No. 50-346
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G. Fiore111, Chief, Reactor Operations and Nuclear ,
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MDIORANDUK FOR:
Support Branch
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J. F. Strecter, Qiicf Nuclear Suj> port Section 1
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J. S. Cresuell, Reactor Inspector-
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CONCERN REGARDING VOIDIliG OF FRESSU
SUBJECT:
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ding th$ treatment of a safety issu
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_This is to inform you'of.a concern regar
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by the Davis-Besse staff.'
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MrI streateP informed me'of'the resud Mr.' Knop, ha
On December- 18,-1978]
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. sation that he, Mr. Tambling, anApparently,iunder_certain conditions,
ith, auxiliary
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- to void the pressuriser by overfeeding the ateam generators _w
.. Davis-Basse staff.
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To my ktiowledge, this. condition is not analyzed ~inthnl sa
Further, . voiding in the hot les. associated with the
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The foregoing
[ pressurizer can result in blocked flow in that loop. c
_ analysis report.
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stion.
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ce during
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I first encounpared the problem with pressurizer level na
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an inspection 1
During the course of that inspection, I reviewed a si= nary
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November - 29, 1977
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This report stated:
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coolant shrunk, we lost level to
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"As the prinary system reac or
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the pressurizer."
In addition the following statements were noted:
"We have asked B&W to investigate why we had this rapid decreas
Specifically, we
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in temperature of the reactor coolant system.
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have asked the following:
50-346/78-06.
If IE Inspection Report
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Are we maintaining too high a level of relatively cold water in theWe int
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secondary side of the steam generators?
90 inches of 70 F water to each steam generator through the automatic
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starting of the auxiliary feedpumps.
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1 questioned the licensee about the results of the EW inquiry, and aske
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to see documentation regarding the matter.
No docu-
was available since the matter was discussed over the telephone.The licensee did
mentation of the telephone conversations were available. s
in level.
~ here was Yproblem with the. voiding of pressuris
tresponse has been, no,. there wasn' t."
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II feel'tiut NRC should conduct,a thorough investigatio
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identified it (BW or TECo') and if the issue was properly reported per
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In addition,' the licensee's performance
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the requirements of Part 21.regarding any corrective actions associa
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examined in light of reguintory requirements. --
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J. S. Creswell
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Reacter Inspector
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R. E. Knop
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T. N. Tambling
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