ML19308B083

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Unusual Event 269/73-15:on 731227,during Routine Shutdown, Safeguards Valve HP-20 Proved Inoperable.Caused by Binding of Torque Limit Switch.Switch Replaced & Tested Satisfactorily
ML19308B083
Person / Time
Site: Oconee Duke Energy icon.png
Issue date: 01/25/1974
From:
DUKE POWER CO.
To:
Shared Package
ML19308B080 List:
References
RO-269-73-15, NUDOCS 7912120812
Download: ML19308B083 (1)


Text

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DUKE POWER COMPANY OCONEE NUCLEAR STATION - UNIT 1 UNUSUAL EVENT REPORT UE-269/73-15 ENGINEERED SAFEGUARDS VALVE HP-20 Description of the Incident on December 27, 1973, Oconee Unit 1 was in the process of being placed in a cold shutdown condition for routine maintenance. The controlling procedure for unit shutdown OP/1/A/1102/10 requires the closure of engineered safe-guards valve HP-20.

The valve was inoperable because the torque limit switch on the electric motor operator was binding, causing the torque switch contacts to open, thus preventing valve closure.

(Reference Oconee FSAR Figure 7-4)

Valve HP-20 is a reactor building isolation valve in the reactor coolant pump seal return header.

The limit switch is on a Limitorque riotor operator, Type SMB-00.

j Regularory Operations, Region II, was notified of the incident on December 27, 1973.

i 2

Corrective Action The torque limit switch was replaced and the valve was tested for proper operability.

The valve was satisfactorily cycled 12 times.

Safety Analysis The unit was shutdown with all reactor coolant pumps secured and in the process of being placed in cold shutdown when the incident occurred. The redundant isolation valve HP-21 was shut thus providing the required isolation.

This incident did not affect the safe operation of the plant or the health and safety of the public.

7912120 [/2

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