05000368/LER-1980-007-03, /03L-0:on 800124,during Mode 1 Operation,Sodium Hydroxide Tank Level Found to Be 93% of Indicated Level. Following Calibr,Level Found to Be Below Tech Spec Limits. Cause Not Stated.Tank Levels Returned to Operable Limits

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/03L-0:on 800124,during Mode 1 Operation,Sodium Hydroxide Tank Level Found to Be 93% of Indicated Level. Following Calibr,Level Found to Be Below Tech Spec Limits. Cause Not Stated.Tank Levels Returned to Operable Limits
ML19296D341
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/22/1980
From: Pendergraft R
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19296D339 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8003030538
Download: ML19296D341 (1)


LER-1980-007, /03L-0:on 800124,during Mode 1 Operation,Sodium Hydroxide Tank Level Found to Be 93% of Indicated Level. Following Calibr,Level Found to Be Below Tech Spec Limits. Cause Not Stated.Tank Levels Returned to Operable Limits
Event date:
Report date:
3681980007R03 - NRC Website

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I During Mode 1 coeration the Sodium Hvdroxide Tank lovol was fnund to bp o 2 93% of indicated level, which is below the limits of Tech. Spec. 3.6.2.2. i o 3 o A IThere have been no similar occurrences.

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