ML19296B357

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LER 80-004/03L-0:on 800107,during Mode 1 Operation,Core Protection Calculator B Failed.Channel B DNBR & Linear Power Density Trips Were Bypassed Placing Reactor Trip Logic in two-out-of-three Trip Sequence.Cause Unknown
ML19296B357
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/15/1980
From: Pendergraft R
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19296B355 List:
References
LER-80-004-03L, LER-80-4-3L, NUDOCS 8002200450
Download: ML19296B357 (1)


Text

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