ML19296B015

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Monthly Operating Repts for Jan 1980
ML19296B015
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 02/05/1980
From: Fay C
WISCONSIN ELECTRIC POWER CO.
To:
Shared Package
ML19296B012 List:
References
NUDOCS 8002190691
Download: ML19296B015 (9)


Text

~t OPERATitJG DAT A RFPORT DOCKET tJO. 50-266 DATE February 5, 1980 COMPLETFD BY C. h. FAY TELFPilONE 414 277 2811 OPER ATING STA'ItJS

1. t) NIT IJAME3 POItJT DEACil tJUCLEAR PLAtJT 11 NIT 1 . NOTES .
2. RFPORTING PERIODI JANil ARY }980 . .
3. I ICFNSFD TilERMAL POWER (MWT); 1518. .- .
4. tJAMFPLATF R ATING (GROSS MWE) 523.8 . .

S. OFSIGN EtFCTRICAt. RATING (NET MWF): 497. . .

6. MAXTMilN OFPENDADLF CAPACITY (GROSS MWE): 514 . .
7. MAXIMtiti DFPENDADLF CAPACITY (NFT MWE)3 445. . . . . . . . . . . . . . . . . . ._. . . . . .
8. 1F filAtJGFS OCCUR IN CAPACITY R ATINGS (ITFMS IJtJMDFR 3 TilROUGli 7) SINCF LAST REPORTe GIVF RFASONS:

NOT APr>LICADLE

9. POWFR I FVf L TO WillCil RESTRICTFD, IF AtJY (ilFT MwF) 390.11
10. REASONS FOR RESTRICTIONS, (IF ANY)I XMKXXVNtKKKKlu(KN:rKX Power restriction is the result of a self-imposed T reduction in core average temperature in an attempt to inhibit corrosion of steam generator tubes within the C tubesheet crevice. TilIS MONTil YR TO DATE CleMllt ATIVE C

N 11. IlOllRS 114 PFPORTItJG PERIOD 744 744 80e976 F. 12. NtJMDFR OF llOliRS REACTOR WAS CRITICAL 744.0 744.0 67,260.5 to 13. RFACTOR REStRVF SiltJTDOWN llOtJRS 0.0 0.0 582.2 c 14. IlotlRS GEtJFRATOR ON LINE 744.0 744.0 65,138.0 0 15. IJNIT RESliRVF SituTDOWN llollRS 0.0 0.0 602.4 J 16. GROS % TilERMAL FNI'RGY GEtJFRATED (MWil) anSe427 86Se427 91e638,2P

17. GROSS FLi-CTRIC AL FtJERGY GENER ATFD (MWill 290,980 290,980 30,8724 730
18. NFT FLi'CTRICAL FNERGY GEtJFRATED (MWil) 276e091 276e091 29e466e209
19. tJNIT SFRVICF FACTOR 100.0 100.0 80.4
20. IINIT AVAILADILITY FACTOR 100.0 100.0 81.2
21. IJNIT CAPACITY FACTOR (USING MDC IJET) 75.0 75.0 74.8 2/. IJNIT CAPACITY FACTOR (USING DER NET) 74.7 74.7 73.2
23. II? LIT FORCFD OllTAGE RATE 0.0 0.0 3.5
24. Silt 1TDOWNS SCllEDtiLFD OVER NEXT 6 MOtJTil5 (TYPF, DATE, AND hllRATION OF EACll):

Unit scheduled to shutdown on February 29, 1980, for 10 to 15 days to perform steam generator leak test.ing and eddy current inspection, and possibly steam generator tube pulling.

25. IF Sill 1TDOWN AT EtJD OF REPORT PERIODe ESTIMATFD DATE OF STARTilP: NOT Sill 1TDOWN DATA REPORTED AND FACTORS CALCULATFD AS RFOllESTFD IN NRC LFT'iFR DATFD SFPTFFDIR 22e 197'/

OPFRATitJG DATA REPORT DOCFET IJO. 50-301 DATF February 5, 1980 COMPL ETFD DY C. W. FAY TFL EPilOtJE 414 277 2811 OPER ATItJG STATLAS

1. litJIT tlAME: POINT DEACll NUCLEAR PLANT UtJIT 2 . t10TFS .
2. RFPORTItJG PERIODI JANUARY 1980 . .
3. l TCFNsi-D TilERMAL POWER (MWT)8 1518. . .
4. t1AMFPL ATI RATitJG (GROSS MWEl8 523.8 . .
5. DESIGtJ FLECTRICAL RATING (tET MWE)! 497. . .
6. MAXIt1 tim DEPFNDADLF CAPACITY (GROSS MhE) 519. . .
7. MAXIMUlf DEPEtJDADL F CAPACITY (NFT MWFl: 495. . . . . . . . . , . . . . . . . . . . . . . . .
8. IF CliANGFS OCrisR It1 CAPACITY RATItJGS (ITEMS NUMDER 3 TilROUGil 71 SitJCF lAST RFPOI Te GIVF REASCNSI IJOT APPLICADLE 9 POWER lFVFL TO WHICil RESTRICTEDe IF ANY (ttFT MWE) NOT APILICADLF
10. RFASONS FOR I(FSTRICTIONS, (TF ANYl: tJOT APl*l.TC Ant F THIS MONTil YR TO DATE CllMist ATIVr
11. IlOllRS IN REPOHTING PFRIOD 744 74's 6S e 7t>1
12. NtMDFR OF llOtJRS HFACTOR WAS CRITICAL 744.0 744.0 Sc,e640.9
13. REACTOR l<ESI RVt' SiltlTDOWN HOtIRS 0.0 0.0 16ei.1
14. 110t19S GENFRATOR Ot1 LINF 744.0 744.0 58,471.0
15. IIN7T RESFRVE SilllTDOWN llOljRS 0.0 0.0 106.4 16 GROS % TilERMAL FNLRGY GFNFRATFD (MWil) 1+1aie502 1eI1ie502 78e764e038
17. CROS'- EL FCTRICAL ENFRGY GENFRATI D (MWH) 369,700 369,700 26e731,040
18. NET FLl"CTRIC AL FtJL'RGY GFNFR ATFD (MWHI 353,404 353,404 25,428eS31 14 UNIT SERVICE FACTOR 100.0 100.0 88.9
20. titJIT AVAIL ADTLiTY FACTOR 100.0 100.0 89.1
21. LJNTT CAPACITY FACTOR (USING MDC NFT) 96.0 96.0 78.9
22. LJtJTT CAPACITY FACTOR (USItJG DER 14FT) 45.6 95.6 7/.8
23. UtJIT FORCED OtJTAGE RATE 0.0 0.0 1.5
24. SiluTDOWNS SCllEDilLFD OVFR NFXT 6 MONTHS (TYPFe DATF, AhD I)URATIOt1 OF EAClH:

Refueling shutdown scheduled for March 20, 1980, to last approximately five weeks.

25. IF SituTDOWil AT EllO OF RFPORT PERIOD, ESTIMATED DATF OF STARltlPt tJOT SilllTDCWil DATA REPORTFD AtJD FACTORS CALCtJL ATED AS RFollESTED Ill llRC L ETTER DATED SFPTEMDI R 22e 197/

UNIT SilDTDOWNS AND POWER REDUCTIONS DOCKET !!O. 50-266 UNIT NAME Point Beach Unit 1 REPORT MONTil January, 1980 COMPLETED . 11 . I- y TELEPIIONE 414/277-2811

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1 3 4 F: Forced Reason: Method: Exhibit G-Instruc-S: Scheduled A- Equipment Failure (explain) l- Manual tions for Prepar-B- Maintenance or Test 2- Manual Scram ation of Data Entry C- Refueling 3- Automatic Scram Sheets for LER File D- Regulatory Restriction 4- Other (explain) (NUREG-0161)

E- Operator Training & License Exam F- Administrative 5 AD-28B Exhibit I- Same G- Operational Error (explain) Source (01-78) 11- Other (explain)

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DOCKET NO. 50-266 UNIT NAME Point fleach Unit 1 DATE February 5, 1980 COMPLETED BY c. W. Pay TELEPIIONE 414/277-2811 AVERAGE DAILY UNIT POWER LEVEL MONTH January, 1980 AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1 372 11 375 21 374 2 370 12 374 22 374 3 368 13 372 23 374 4 348 14 373 24 372 5 374 15 373 __

25 367 6 370 16 370 26 369 7 374 17 373 27 361 8 372 18 372 28 372 9 377 19 374 29 371 10 376 20 373 30 371 31 371 AD-28A (1-77)

DOCKET NO. 50-301 UNIT NAME Point 13each Unit 2 DATE February 5, 1980 COMPLETED BY C. W. Fay /

TELEPIIONE 414/277-2811 AVERAGE DAILY UNIT POWER LEVEL MONTII .Ta n ua ry , 1980 AVERAGE AVERAGE AVERAGE DAILY DAILY DAILY POWER LEVEL POWER LEVEL POWER LEVEL DAY MWe NET DAY MWe NET DAY MWe NET 1 486 11 479 21 483 2 486 12 459 22 482 3 480 13 475 23 478 4 475 14 483 24 475 5 461 15 483 25 468 6 418 16 483 26 472 7 482 17 484 27 473 8 478 18 484 28 472 9 477 19 485 29 4 71 10 479 20 480 30 469 _

31 468 AD-28A (1-77)

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE Docket No. 50-266 Unit Name Point Beach Unit 1 Date February 5, 1980 Completed By C. W. Fay Telephone 414/277-2811 Unit 1 was base loaded for 75% of the period with two load reductions.

Load was reduced to 320 MWe net on January 4, 1980, for approximately nine hours for repair of the 1B condensate pump, and again on January 27, 1980, to 285 MNe net for five hours to facilitate turbine stop valve testing. The unit has been operating at a slightly reduced efficiency because of increased circulating water temperatures caused by ice melt operation.

On January 4, 1980, the reactor coolant system operating pressure was reduced from 2235 psig to 1985 psig to comply with NRC instructions on low pressure operation. The pressure was reduced in order to reduce the differential pressure acrosn the steam generator tubes, thus reducing metal stresses and consequently reducing the possible inducing of further tube leakage. Unit primary-to-secondary leakage has remained stable at approximately 30 gallons per day during the period.

Replacement of the "B" condensate pump seal was performed during the period.

A site evacuation emergency plan drill was conducted on January 14, 1980. A critique of the drill was conducted by the Manager's Supervisory Staff on February 4, 1980.

All of the spent fuel has been moved to the newly reracked north spent fuel pit.

The unit "B" reactor coolant pump seal leakage has been below normal for the duration of this period, but is stable and at a sufficient level to provide adequate seal lubrication along with cooling to the pumps lower bearing. The leakage rate is being closely nonitored by operating personnel.

Work continues on IE Bulletin Nos. 79-02, anchor bolt inspection, and 79-14, seismic analysis for as-built safety related piping systems.

No other major safety-related maintenance was performed during the period.

NARRATIVE

SUMMARY

OF OPERATING EXPERIENCE Docke t No . 50-301 Unit Name Point Beach Unit 2 -

Date February 5, 1980 Completed By C. W. Fay Telephone 414-277/2811 Unit 2 was base loaded for 96% of the period with five load reductions.

Unit load was reduced on January 3,1980, and again on January 9, 1980, to 470 MNe net for one hour to remove the SB feedwater heater from service; on January 6, 1980, to 250 MNe net for seven hours for condenser tube plugging; on January 12, 1980, to 435 MNe net for 16 nours to maintain 345 KV system stability while line 111 was out of service; and on January 13, 1980, to 475 MNe net ft,r one hour to allow testing of the crossover steam dump system. The unit has been operating at a slightly reduced efficiency because of increased circulating water temperatures caused by ice melt operation.

All the new fuel bundles necessary for the unit refueling in April,19 80, (Refueling 6) have been received, inspected, and placed in storage.

Work performed on the 5B feedwater heat exchanger while it was out of service included rewelding of a leaking patch on the tubesheet and repair of a leaking isolation valve on the level transmitter manifold.

Charging pump maintenance work during the period included cleaning the 2C charging pump motor commutator and replacement of the " A" charging pump block we.ich was found to be cracked. The Unit 2 "A" charging pump block was the last of the origina1 plant charging pump blocks. The recent -

addition of suction line stabilizers to these pumps should greatly reduce or eliminate the incidence of block cracking.

Work continues on IE Bulletin Nos. 79-02, anchor bolt inspection, and 79-14, seismic analysis for as-built safety related piping systems.

No other major safety-related maintenance was performed during the period.

2 On January 17, 1980, the recent installation of instrument bus AC/AC motor-generator units proved to be a valuable plant modification as they kept the plant from tripping when the nearby Kewaunee Nuclear Plant tripped of f line due to an auxiliary transformer failure. The motor generator units prevented the sh 't duration line fault of approximately 1800 amps caused by t trip from affecting the instrument busses and possibly tripping the Point Beach units.

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