LER-1980-009, /03L-0:on 800201,loss of Power Occurred on 138 Kv Bus 1.Emergency Diesel Generator 1 auto-started on Loss of Offsite Power to 4160-volt 1A Station Svc Transformer.Caused by Faulty Backup Relay Timer |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3341980009R03 - NRC Website |
|
text
U 3 NUCL L Alt et t GtJL A T Ol4 Y CoM*.11',.lON NPL
..e LICENSEE ' EVENT REPORT CO*47R0t. 0LCLC l l
l l
l l
h IPLE ASt PRINT OR TYPt AL L REQUlflCD INFORMAf toNi
@ lPlAl3lV
$ l 1 l@l 010 l-l 0 l0 l 0 l 010 l-10 l 0 l[l-.11 l1 11 j ' l@l l
l@
am a
a s
. w. w... -
..m m..
co.'T
] ]l1. @l0l5l0l0l0131314 @l01210lIl310!gl0]2l2j91Mi 0l@
oi:I Eust cescnATicN A oencaA EC E '.C E S [TI" l l A t 1018 hours0.0118 days <br />0.283 hours <br />0.00168 weeks <br />3.87349e-4 months <br />, the loss of po' der occurred on the 138 KV Bus No. I and the No. I j
.iiil F.mergenev Diesel Cencrator auto-started on a loss of offsite power to the 4160V a i4 l I A Station Service Transformer. This loss of power to the 1A 4160V Normal Bus l
, t-I provides the blackout signal logic to auto-start the emereency diesel.
Core oH Ialterations were not in nrocress at the time of the incident. The operators in the l 1 l control roon controlled the incident with no problems because there was offsite j
9I:
i2 l power to the B Station Service Transformer which essentially (continued on attached)l sJ g 3 S v 5 T E '.t CALSE CA,$E Cove vAtys CODE COOE SwdC00E C0Y'ONENT CODE SwaCODE SwSCOOE [1LJ [E lE l@ lE l@ l A l@ l Zl Zl Zl Zl Zj Zj g lZ j g lZ l g 7
8 9
'J In 1:
fa
- - s 13
.J SEQUE NTI AL CCCU42E'.CE REFCRT 4EVl540N tie aC EVENTvfAR AEPORTNO.
C00E Tvet N o.
h,a t aga' l8l0l l_l l0 l0 l9 l jfl
{0 l3 l lL l l_l l oj
_:i
- 2
- 4 a
- s a
u 2i 2.
ACTION suttas E88ECT SH U'O OV.N AT*a0wvENT N 8 a o.4
'AIYE COYP COYPONENT
'!ETaOO
=0VAS SLeviTTEO 80A9 wis SL **tJ E.4 YANLSACTLaEH T A A E 's ACTION CN8LANT l E l@l Z l@
l Zl@
lZ l@
0 l0 l0 l l
lY g l N lg l43Z l@lZ l9 l9 l9 lg 40 el 42 44 41
- /.usE csscaipacs. ANo CORRECTIVE AQTIONS @
l The cause of the partial loss of power was a faulty backup relay timer that l
i..
l operated and tripped the 138 KV Buss No. I differential relay. The reason for the j backup timer operation is under investigation but is not known at the present time. ;
l On the No. 1 Diesel Generator Tuto sequencer, the ATC adjustable 180 second timer l
I was not wired as installed and unavailable because the (continued on attached) l 4
n 8A; ;. i T Y
,e YE TwCO OF dA7.3 70.'18 OTwEasTATU3
- 0:5CONERv Of 5COV E Av OE50 Ai8 TION --
j l Hl@ l 0} Of 01@l N/A.
l l A l@l Operator observation j
',/.g.,Tv w. r e.T Aveu.T :s Activity h l tcC AT'ON es af. East h 16 I W ' g s aELEastn Ql'3l
=E.EstE:
': / A l
':/A I
v v
44 45 sJ t.Fu*:$.3E5 ta
- - as g ;;n s.m.,
l l'i'l})l1 OI l_Z lwl
' /a
".i.
.-1 4
A
$(,5O I'
(
1 -
I
,I s I s(O s. r.
m 4
.S.
'. I d d,, Y v i l?'
l N/A l
6 () 0;3 ( U()
...c to
.t
., g
,;l
A l
1l l I
'l' 1
l 'l i
-. A.
c i '. iN G 3-125'
- , g.,.
Attachment To LER 80-09/03L Beaver Valley Power Station Duquesne Light Company Docket No. 50-334 Event Descrintion And Probable Consequences' t
services the B train of equipment. The failure of the sequencer was found while checking locally for any relay actuations.
It was found that motor control centers MCC-E7, E9 and Ell and Supplementary Leak Collection and Release Fan (VS-F-4 Al d id not sequence onto their respective busses.
Power was restored to the la Station Service Transformer at 1046 hours0.0121 days <br />0.291 hours <br />0.00173 weeks <br />3.98003e-4 months <br />.
The backup timer has operated spuriously before, once possibly two times.
The No. 1 Emergency Diesel Generator auto-sequencer has never f ailed electrically prior to this incident. All previous problems have been due to timing sequence duration being out of specification in the 1/100 of a second range.neutral lead was also disconnected.
See accompanying ~ report of sequencer troubleshooting. The backup timer was checked and found to be operating properly so it was put back in service.
The timer problem will continue to be investigated. The No. 1 Emergency Diesel Generator auto-sequencer was wired correctly and tested. The No. 2 Emergency Diesel Generator was verified to be wired correctly. No permanent actions at present are planned to preclude any spurious backup timer operation. A Maintenance Work Request has been issued to install locks on the auto-sequencers.
m
DUQUESNE LIGilT COMPANY ueaver Valley Power Station February 25, 1980 Report On Partial Loss Of Power On February 1,1980 And Failure of No. I Diesel Generator Load Sequencer On February 1, 1980 at 1038 hours0.012 days <br />0.288 hours <br />0.00172 weeks <br />3.94959e-4 months <br />, BVPS Unit 1 experienced a partial loss
,of power due to loss of the 133 KV Bus that supplies the 4160V 1A Station Service Transformer. This la Transformer, in turn, supplies the 4160V 1A and 1B Station Service Busses. The 1A Transformer also supplies the 1AE Emergency Bus.
Upon investigation of the No. 1 sequencer (CKT SEQ 1 DWG ll700-RE-21CE) which was instituted due to the failure of MCC-E7, E9, Ell and [VS-F-4A] to auto-load, station personnel found that the cam of 62-SEQ was stopped on division eight (8) of the timer. Work was to begin at 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br />.
Work began with the approach that personnel could physically look at the equipment and then check the relays and the timers electrically. Within about thirty (30) minutes, the first class electrician found a lead that uns totally disconnected. When he checked the wiring, and additionally followed the lead out physieally, it was decided that this could be the problem. Approximately two hours had transpired to this point. The lead that was found free ~was Lead No. 8 to neutral, on Relay 74 SEQL, which is an alarm relay. The reason it was felt that this could be the problem is that the neutral system in the sequencer is
" daisy chained", or a series neutral, and is not one where each separate lead goes to a neutral bus.
Proximity of relay is the only requirement for running the leads; that is, there is no special order. The sequencer panel is randomly wired without wire markings.
It was decided to manually actuate the timer to check all contacts. When personnel checked the microswitch for cam #6 (top switch), it was found that it never opened to reset. One of the workers on the job had touched this microswitch so it was felt that, possibly, this person had knocked the microswitch out of adjustment.
It was readjusted with a slight cam movement.
The method used to check the microswitch operation was by manual timer rotation and an ohmeter to contact closure. At this point, it was felt that a couple of obvious problems that need no further checking had been solved. After talking to the shift supervisor, it was decided to put all operable equipment in " PULL-TO-LOCK" and manually initiate the timer.
Report on partial I.oss of power on February 1, 1980 (cont inue ')
When circuit breaker BKR l-22 was closed on Vital pais 1, the timer motor ran continuously. The timer did not have to he manually initiated.
Contact closure was checked at this time, using a voltmeter, and found that can #6 contact was working properly but would not reset the timer.
Further checking with the wiring diagram revealed that the timer motor was mis-wired.
After approximately ten or so wiring cheeks, the leads were switched back to the positions where both the schematic (RE-21CE) and the wiring diagram (RE-14C)
Indicated that they should be connected. At this point, five manually-initiated tests were run and the timer appeared to work satisfactorily. More auto-load tests will be run before station startup.
On the morning of February 27, 1980, the following checks and tests were performed:
1.
Checked to assure that cabinet was in the same condition as it was Icft in on February 1, 1980.
2.
Removed the neutral lead #8 that was originally found disconnected.
Timer was manually run through its paces and'it was found that the
~
only two relays that operated were 62-AEX2 and 162-AEX2.
This does not coincide with the test that was run when the maintenance work request (No. 791330) was signed-off. All relays worked correctly at that time.
3.
Opened Vital Bus No. 1 BKR 1-22 to replace lead #8 SEQ 1Y.
Received alarm A9-56 " AUTO SEQUENCER LOSS OF CONTROL POWER" which proved that the alarm works on a loss of power.
4.
Replaced #8 neutral lead and manually actuated the timer again. All relays operated from the cam switch in the order they are supposed to.
Two of the cognizant personnel involved in the troubleshooting of this sequencer af ter the last auto-load test were interviewed.
It is felt that these personnel would not have left the sequencer in the shape that it was in.
It has been concluded that the circuit was intact when maintenance personnel completed their work.
It was also intact when the shift supervisor signed-off the maintenance work request; therefore, the problem originated after the maintenance
~
work request sign-off date of August 10, 1979.
It is the conclusion of the Onsite Safety Committee that this event was not malicious since experience is needed to read and understand the drawing and also due to the lack of wire markings and random wiring.
Also, the time that would be needed to study the circuitry in the cabinets is a factor against malicious intent. -
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000334/LER-1980-001-01, /01T-1:on 870626,discovered That Suction Piping on Vacuum Pump Not Adequately Supported for Seismic Event. Caused by Inaccurate Computer Code Used.Seismically Inadequate Piping Isolated & Support Added | /01T-1:on 870626,discovered That Suction Piping on Vacuum Pump Not Adequately Supported for Seismic Event. Caused by Inaccurate Computer Code Used.Seismically Inadequate Piping Isolated & Support Added | | | 05000334/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000334/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000334/LER-1980-002-01, /01T-0:on 800117,during Operational Mode 5,w/RCS Temp at 100 F & Atmospheric Pressure & RCS Level mid-loop W/ RHR Flow at 1,700 Gpm,Reactor Vessel Vent Educator Was in Svc,Causing Negative Pressure | /01T-0:on 800117,during Operational Mode 5,w/RCS Temp at 100 F & Atmospheric Pressure & RCS Level mid-loop W/ RHR Flow at 1,700 Gpm,Reactor Vessel Vent Educator Was in Svc,Causing Negative Pressure | | | 05000334/LER-1980-003-01, /01T-0:on 800124,overstress Condition Was Confirmed to Exist During Postulated Seismic Event W/Pipe Support H-95 on Component Cooling Water Sys Line CC-323. Caused by Use of Incorrect Method of Pipe Stress Analysis | /01T-0:on 800124,overstress Condition Was Confirmed to Exist During Postulated Seismic Event W/Pipe Support H-95 on Component Cooling Water Sys Line CC-323. Caused by Use of Incorrect Method of Pipe Stress Analysis | | | 05000334/LER-1980-004-03, /03L-0:on 800123,radiation Monitor Setpoints Less Conservative than Those Required in Mode 6 During Refueling Operations.Caused by Personnel Error.Reactor Vessel Head Studs Detensioned | /03L-0:on 800123,radiation Monitor Setpoints Less Conservative than Those Required in Mode 6 During Refueling Operations.Caused by Personnel Error.Reactor Vessel Head Studs Detensioned | | | 05000334/LER-1980-005-03, /03L-0:on 800112,decontamination Proceedings Were in Progress When Waste Water Tank Filled.Operator Instructed to Do Valving in Area Was Not Familiar W/Tech Specs & Failed to Have Radiation Technician or Ratemeter Available | /03L-0:on 800112,decontamination Proceedings Were in Progress When Waste Water Tank Filled.Operator Instructed to Do Valving in Area Was Not Familiar W/Tech Specs & Failed to Have Radiation Technician or Ratemeter Available | | | 05000334/LER-1980-006-04, /04T-0:on 800130,tritium Activity in Quarterly Grab Samples Collected in Oh River Near Facility Discharge During Fourth quarter,1979 Exceeded ETS But Below 10CFR20 Limits | /04T-0:on 800130,tritium Activity in Quarterly Grab Samples Collected in Oh River Near Facility Discharge During Fourth quarter,1979 Exceeded ETS But Below 10CFR20 Limits | | | 05000334/LER-1980-007-01, Er 80-007/01T-0:on 800121,during Reload After Defueling, Main Filter Banks Found Not in Svc.Caused by Procedural Inadequacy Because None of Refueling Checklists Indicated Tech Spec Change That Required Flow | Er 80-007/01T-0:on 800121,during Reload After Defueling, Main Filter Banks Found Not in Svc.Caused by Procedural Inadequacy Because None of Refueling Checklists Indicated Tech Spec Change That Required Flow | | | 05000334/LER-1980-008, Forwards LER 80-008/01T-1 | Forwards LER 80-008/01T-1 | | | 05000334/LER-1980-008-01, /01T-1:on 800225,during in-plant Insp,Potential Overstress Condition of Cable Spreading Room Floor Indicated Due to Postulated Seismic Loading.Caused by Utilizing Underside of Floor to Higher Degree than Original Design | /01T-1:on 800225,during in-plant Insp,Potential Overstress Condition of Cable Spreading Room Floor Indicated Due to Postulated Seismic Loading.Caused by Utilizing Underside of Floor to Higher Degree than Original Design | | | 05000334/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000334/LER-1980-009-03, /03L-0:on 800201,loss of Power Occurred on 138 Kv Bus 1.Emergency Diesel Generator 1 auto-started on Loss of Offsite Power to 4160-volt 1A Station Svc Transformer.Caused by Faulty Backup Relay Timer | /03L-0:on 800201,loss of Power Occurred on 138 Kv Bus 1.Emergency Diesel Generator 1 auto-started on Loss of Offsite Power to 4160-volt 1A Station Svc Transformer.Caused by Faulty Backup Relay Timer | | | 05000334/LER-1980-010-03, /03L-0:on 800131,refueling Team Was Given Go Ahead for Core Alterations.Fifteen Minutes Later,Inservice Boric Acid Transfer Pump CH-P-2B Tripped on Thermal Overload. Probably Caused by Faulty Blender Controls Shifting Speed | /03L-0:on 800131,refueling Team Was Given Go Ahead for Core Alterations.Fifteen Minutes Later,Inservice Boric Acid Transfer Pump CH-P-2B Tripped on Thermal Overload. Probably Caused by Faulty Blender Controls Shifting Speed | | | 05000334/LER-1980-011-03, /03L-0:on 800226,during Boron Injection Flow Path Verification,Operator Stroked MOV-SI-869A Connecting Charge Sys Fill Header to RCS Hot Leg Piping.Valve Opened & Linestarter Tripped.Caused by Burnt Motor in MOV-SI-869A | /03L-0:on 800226,during Boron Injection Flow Path Verification,Operator Stroked MOV-SI-869A Connecting Charge Sys Fill Header to RCS Hot Leg Piping.Valve Opened & Linestarter Tripped.Caused by Burnt Motor in MOV-SI-869A | | | 05000334/LER-1980-012-01, /01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby | /01T-0:on 800312,emergency Shutdown Panel Auxiliary Feedwater Flow Instrumentation Readings Were Deleted from Surveillance Testing.Caused by Meter Reading Zero in Standby | | | 05000334/LER-1980-013-04, /04T-0:on 800302,during Maint Surveillance,Cooling Tower Blowdown Temp Indicator Found Out of Calibr.Caused by Instrument Drift.Instrument Recalibr | /04T-0:on 800302,during Maint Surveillance,Cooling Tower Blowdown Temp Indicator Found Out of Calibr.Caused by Instrument Drift.Instrument Recalibr | | | 05000334/LER-1980-013, Forwards LER 80-013/04T-0 | Forwards LER 80-013/04T-0 | | | 05000334/LER-1980-014-04, /04T-0:800307,during Radiation Monitor Surveillance Test,Liquid Waste Effluent Monitor Did Not Alarm & Discharge Valve Did Not Close.Caused by Loose Relay & Solder Joints in Wiring.Deficiencies Corrected | /04T-0:800307,during Radiation Monitor Surveillance Test,Liquid Waste Effluent Monitor Did Not Alarm & Discharge Valve Did Not Close.Caused by Loose Relay & Solder Joints in Wiring.Deficiencies Corrected | | | 05000334/LER-1980-015-04, /04T-0:800308,during Radiation Monitor Surveillance Test,Component Cooling Water Radiation Monitor high-high Level Alarm Did Not Function.Caused by Alarm Potentiometer Out of Adjustment | /04T-0:800308,during Radiation Monitor Surveillance Test,Component Cooling Water Radiation Monitor high-high Level Alarm Did Not Function.Caused by Alarm Potentiometer Out of Adjustment | | | 05000334/LER-1980-016-03, /03L-0:on 800311,while Testing Battery Charger 2, Ac Input Breaker Tripped.Caused by Loose Control Wiring. Loose Wires Resoldered | /03L-0:on 800311,while Testing Battery Charger 2, Ac Input Breaker Tripped.Caused by Loose Control Wiring. Loose Wires Resoldered | | | 05000334/LER-1980-017-01, /01T-0:on 800326,reanalysis of Seismic Pipe Stress of Main Steam Piping Inside Valve House for OBE long-term Criteria Showed,For Some Conditions,Allowable Stress Level May Be Exceeded in Headers for Main Steam Relief Valves | /01T-0:on 800326,reanalysis of Seismic Pipe Stress of Main Steam Piping Inside Valve House for OBE long-term Criteria Showed,For Some Conditions,Allowable Stress Level May Be Exceeded in Headers for Main Steam Relief Valves | | | 05000334/LER-1980-017, Updated LER 80-017/01T-1:on 800326,reanalysis of Piping & Supports for Main Steam Sys Outside Containment Revealed Design Deficiencies If All Five Safety Relief Valves Opened on Any Manifold.Caused by Load Resulting from Open V | Updated LER 80-017/01T-1:on 800326,reanalysis of Piping & Supports for Main Steam Sys Outside Containment Revealed Design Deficiencies If All Five Safety Relief Valves Opened on Any Manifold.Caused by Load Resulting from Open Valves | | | 05000334/LER-1980-018-01, /01T-0:on 800326,plant Operators Were Testing Temporary Fire Pump When Section of Fire Main Failed.Caused by Piping Failure.Failed Section of Piping Replaced | /01T-0:on 800326,plant Operators Were Testing Temporary Fire Pump When Section of Fire Main Failed.Caused by Piping Failure.Failed Section of Piping Replaced | | | 05000334/LER-1980-019-03, /03L-0:on 800310,while Steam Flushing,Crack Found in Channel Head of Liquid Waste Evaporator Bottoms Heat Exchanger.Caused by Equipment Failure,Probably Due to Chloride Stress Corrosion.Sleeve Welded Over Channel Head | /03L-0:on 800310,while Steam Flushing,Crack Found in Channel Head of Liquid Waste Evaporator Bottoms Heat Exchanger.Caused by Equipment Failure,Probably Due to Chloride Stress Corrosion.Sleeve Welded Over Channel Head | | | 05000334/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000334/LER-1980-020-03, /03L-0:on 800329,during Operations to Increase Level in RCS Loops,Vol Control Tank Outlet MOV-CH-115C Found Closed.Vol Control Tank Level Indicated Normally.Caused by Bad Fuse Holder for Level Bistable.Fuse Holder Replaced | /03L-0:on 800329,during Operations to Increase Level in RCS Loops,Vol Control Tank Outlet MOV-CH-115C Found Closed.Vol Control Tank Level Indicated Normally.Caused by Bad Fuse Holder for Level Bistable.Fuse Holder Replaced | | | 05000334/LER-1980-021, Has Been Cancelled | Has Been Cancelled | | | 05000334/LER-1980-022, Forwards LER 80-022/01T-0 | Forwards LER 80-022/01T-0 | | | 05000334/LER-1980-022-01, /01T-0:on 800408,while Attempting to Increase RHR Flow to Tech Spec Value Required for Dilution,Total Loss of Flow Was Experienced.Caused by Pump Not Being Vented When Flow Increase Was Initiated.Operating Procedures Revised | /01T-0:on 800408,while Attempting to Increase RHR Flow to Tech Spec Value Required for Dilution,Total Loss of Flow Was Experienced.Caused by Pump Not Being Vented When Flow Increase Was Initiated.Operating Procedures Revised | | | 05000334/LER-1980-023, Forwards LER 80-023/01T-0 | Forwards LER 80-023/01T-0 | | | 05000334/LER-1980-023-01, /01T-0:on 800411,during Operational Mode 5,w/ Steam Generators Drained & RCS Level mid-span in Loops, Complete Loss of RHR Flow Occurred While Plant Operators Were Increasing RHR Heat Exchanger Flow | /01T-0:on 800411,during Operational Mode 5,w/ Steam Generators Drained & RCS Level mid-span in Loops, Complete Loss of RHR Flow Occurred While Plant Operators Were Increasing RHR Heat Exchanger Flow | | | 05000334/LER-1980-024-03, /03L-0:on 780428,audit Revealed That Weekly Surveillance Tests on Boric Acid Pumps Missed During Wk of 780810.Caused by Operator Error Due to Confusion Between Modes.Test Scheduling Mods Have Been Made | /03L-0:on 780428,audit Revealed That Weekly Surveillance Tests on Boric Acid Pumps Missed During Wk of 780810.Caused by Operator Error Due to Confusion Between Modes.Test Scheduling Mods Have Been Made | | | 05000334/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000334/LER-1980-025-01, /01T-0:on 800415,during Tank Mod Project,Weld on 12-inch Nozzle Penetration to Refueling Water Storage Tank OS-TK-1 Reported Not to Be in Conformance W/Design.Caused by Failure of Manufacturer to Follow Drawings | /01T-0:on 800415,during Tank Mod Project,Weld on 12-inch Nozzle Penetration to Refueling Water Storage Tank OS-TK-1 Reported Not to Be in Conformance W/Design.Caused by Failure of Manufacturer to Follow Drawings | | | 05000334/LER-1980-025, Forwards LER 80-025/01T-0 | Forwards LER 80-025/01T-0 | | | 05000334/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000334/LER-1980-026-03, /03L-0:on 800422,pump Being Used to Start Liquid Waste Discharge Observed to Have Higher than Normal Flow. Caused by Leaking Effluent Valves.Corrective Actions Scheduled to Be Completed as Soon as Possible | /03L-0:on 800422,pump Being Used to Start Liquid Waste Discharge Observed to Have Higher than Normal Flow. Caused by Leaking Effluent Valves.Corrective Actions Scheduled to Be Completed as Soon as Possible | | | 05000334/LER-1980-027-03, During Maint of Diesel Generator Lube Oil Cooler,Internals of River Water Check Valve Discovered in Cooler.Caused by Flutter Due to High Flow Conditions Eroding Hinge Pin Guide.Valve Replaced | During Maint of Diesel Generator Lube Oil Cooler,Internals of River Water Check Valve Discovered in Cooler.Caused by Flutter Due to High Flow Conditions Eroding Hinge Pin Guide.Valve Replaced | | | 05000334/LER-1980-027, Forwards Updated LER 80-027/03L-1 | Forwards Updated LER 80-027/03L-1 | | | 05000334/LER-1980-028-03, /03L-0:on 800504,power Was Lost to Vital Bus Inverter 4 Due to Blown Main Power Supply Fuse.Cause Unknown.Fuse & Rectifier Replaced.Frequency Adjusted | /03L-0:on 800504,power Was Lost to Vital Bus Inverter 4 Due to Blown Main Power Supply Fuse.Cause Unknown.Fuse & Rectifier Replaced.Frequency Adjusted | | | 05000334/LER-1980-029, Forwards LER 80-029/03L-0 | Forwards LER 80-029/03L-0 | | | 05000334/LER-1980-029-03, /03L-0:on 800409,during Performance of Containment Isolation Check Valves Test,Found Safety Injection Accumulator Fill Line Check Valve Opened Beyond Limits of Tech Spec.Cause Under Investigation | /03L-0:on 800409,during Performance of Containment Isolation Check Valves Test,Found Safety Injection Accumulator Fill Line Check Valve Opened Beyond Limits of Tech Spec.Cause Under Investigation | | | 05000334/LER-1980-030-01, /01T-0:on 800519,plant Operators Testing diesel- Driven Fire Pump When High Temp Alarm Was Received & Diesel Overheated.Caused by Brittle Fan Belt Slipping | /01T-0:on 800519,plant Operators Testing diesel- Driven Fire Pump When High Temp Alarm Was Received & Diesel Overheated.Caused by Brittle Fan Belt Slipping | | | 05000334/LER-1980-031-01, /01T-0:on 800521,upon Finding Leaking RHR Sys Vent Valve Weld,Evaluation Commenced to re-energize RHR Isolation Valve in Case of Gross Failure.Caused by de-energized Process Control Signal & Vent Weld Leak | /01T-0:on 800521,upon Finding Leaking RHR Sys Vent Valve Weld,Evaluation Commenced to re-energize RHR Isolation Valve in Case of Gross Failure.Caused by de-energized Process Control Signal & Vent Weld Leak | | | 05000334/LER-1980-031, Forwards LER 80-031/01T-0 | Forwards LER 80-031/01T-0 | | | 05000334/LER-1980-032-03, /03L-0:on 800503,during Control Board Insp,Vol Control Tank Outlet Valve Was Found Shut.Caused by Short Circuited Lead in Level Comparator.Shorted Wire Replaced | /03L-0:on 800503,during Control Board Insp,Vol Control Tank Outlet Valve Was Found Shut.Caused by Short Circuited Lead in Level Comparator.Shorted Wire Replaced | | | 05000334/LER-1980-033, Forwards LER 80-033/03L-0 | Forwards LER 80-033/03L-0 | | | 05000334/LER-1980-033-03, /03L-0:on 800617,diesel Generator 1 Governor Control Motor Failed.Caused by Cycling of Governor While Attempting to Shut Down Diesel W/Fast Start Signal Still Applied.Motor Replaced | /03L-0:on 800617,diesel Generator 1 Governor Control Motor Failed.Caused by Cycling of Governor While Attempting to Shut Down Diesel W/Fast Start Signal Still Applied.Motor Replaced | | | 05000334/LER-1980-034-03, /03L-0:on 800512,during Air Flow Surveillance Test on Fire Suppression Sys,Approx 50% of Sprinkler Nozzles Found Plugged.Caused by Rust & Unidentified Matl.Nozzles Will Be Cleaned & Sys Blown Down W/Air | /03L-0:on 800512,during Air Flow Surveillance Test on Fire Suppression Sys,Approx 50% of Sprinkler Nozzles Found Plugged.Caused by Rust & Unidentified Matl.Nozzles Will Be Cleaned & Sys Blown Down W/Air | |
|