LER-1978-025, /03L-0 on 781031:condensate Storage Tank Was Leaking Due to Galvanic Corrosion.Leak & Other Weak Spots Were Patch Welded |
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2 On October 31, 1978 a leak was discovered at the base of the condensate j
- storage tank.
The_ water in the tank at the time had an activity con-
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l centration of 4.30 E-05 pCi/ml. After the tank was emptied and the bot-l o
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Isotopic analyses l
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[ the tank to a depth of twenty-five f eet showed no significant amount of l
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- activity above background.
The event has minimal safety significance.
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O lThe cause of the failure is attributed to calvanic corrosion from be-neath the tank.
The tank was emptied and the area of the leak was l
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patch welded.
Patches were also welded over other areas where wall thinn-l ing was made evident by ultrasonic means. An engineering evaluation l
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% POWE R OTHER STATUS ISCOV RY DISCOVERY DESCRIPTION lHl@ l0l0l0l@l NA l
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i Morr:stown, New Jersey 07960 (201)455 4203 OYSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/78-25-3L Report Date December 1, 1978 Occurrence Date October 31, 1978 Identification of Occurrence Unmonitored release of radioactive water from the base of the condensate storage tank.
This event is considered to be a reportable occurrence as defined in the Technical Specifications, paragraph 6.9.2.b.4.
Conditions Prior to Occurrence The plant was shut down for a scheduled refueling / maintenance outage.
Reactor subcritical.
Reactor mode switch locked in refuel.
All control rods fully inserted.
Source range monitors < 40 cps.
Cavity flooded.
Reactor coolant 93 F.
Description of Occurrence On October 31, 1978, at approximately 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, a leak at the base of the condensate storage tank was discovered.
Following this observation, action was initiated to correct the problem.
The water in the tank was transferred to the hotwell and to the radwaste building.
The bottom of the' tank was cleaned and inspected.
Repair commenced approximately five days after the discovery of the leak and completed on November 11, 1978.
At approximately 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br />, on October 31, 1978, a sample of the water in the condensate storage tank was collected. An isotopic analysis was run and a concentration of 4.30 x 10-5 uti/m1 of activity was detected.
Apparent Cause of Occurrence The cause of the event is component failure which is attributed to galvanic corrosion from beneath the tank.
JU:,ev CeW Pct.er & Lt.r Comerv 3 a c -t / c' me Gen tun cn E,wm v.
- Reportable Occurrence No. 50-219/78-25-3L Page 2 December 1, 1978 Analysis of Occurrence Based on the change of water level in the condensate storage tank and the size of the hole (approximately 0.5 cm in diameter), a very small amount of wa~ter was released. On November 6, 1978, at approximately 1700 hours0.0197 days <br />0.472 hours <br />0.00281 weeks <br />6.4685e-4 months <br />, a sample of the sand beneath the condensate storage tank was collected directly under the failure.
An isotopic analysis indicated a concentration of 7.38 x 10-1 pCi/ml.
In addition to the sample beneath the condensate storage tank, core samples were taken four feet and twelve feet f rom the tank on November 20, 1978.
These samples were taken at ground elevation, five feet, ten feet, fifteen feet, and twenty feet below the surface.
No significant amount of activity was detected above background. The safety significance of this occurrence is, therefore, considered to be minimal.
Corrective Action
Upon discovery that the condensate storage tank was leaking, the water was transferred to the hotwell and to the radwaste building.
The area of the leak has been patch welded.
The entire bottom <f the storage tank was spot checked by ultrasonic testing and other locations were identified where wall thinning was evident.
Patches were welded over each of the locations.
An engineering evaluation will be performed to determine an appropriate corrosion protection scheme.
Failure Data Condensate Storage Tank Type
- - Vertical Conical Roof Nominal Capacity - 525,000 gallons Dimensions Diameter
- - 45.0 feet Height
- (Cylindrical Portion) 45.0 feet Material
- - Aluminum Alloy
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