05000324/LER-1979-036-03, /03L-0 on 790507:while Performing Visual Insp of Inaccessible Snubbers,Six Snubber Failed.Caused by Low Fluid Level.All Snubbers Disassembled,Inspected & Rebuilt

From kanterella
(Redirected from ML19289F367)
Jump to navigation Jump to search
/03L-0 on 790507:while Performing Visual Insp of Inaccessible Snubbers,Six Snubber Failed.Caused by Low Fluid Level.All Snubbers Disassembled,Inspected & Rebuilt
ML19289F367
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 06/04/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19289F365 List:
References
LER-79-036-03L, LER-79-36-3L, NUDOCS 7906070282
Download: ML19289F367 (1)


LER-1979-036, /03L-0 on 790507:while Performing Visual Insp of Inaccessible Snubbers,Six Snubber Failed.Caused by Low Fluid Level.All Snubbers Disassembled,Inspected & Rebuilt
Event date:
Report date:
3241979036R03 - NRC Website

text

..no r o..

m (7 77)

/l LICENSEE EVENT REPORT CONT 3OL BLOCK: l l

l l

l l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION1 6

e 9

lP l 2 l@l 0 0l -l 0 0 0l 0 0

0 l 0 @l 4 1l 1l 1 1 @l o

i N

C lB E

7 8 9 LICENSEE CCOE 14 15 LICENSE NUV6ER 25 26 LICE NSE T'r PE Jo 57 CAT 68 CON'T 0

4 7 9@

Lj@l 0l 5 l 0 l -l 61 3 l 2 l 4 @l 0 l 5 l 0 l 7 l 7 l 9 lgl 0l 6 RE CA o

3c 9 7

d 60 61 DOCKET NwL8gR 68 63 EVENT DATE 74 75 R E P OR T, D A T E 50 EVENT DESCRIPTION AND PROB ABLE CONSEOUENCES h o

2 l While performing PT 19.6.0.1, Visual Inspection of Inaccessible Snubbers, six snubberd o

3 l failed. These snubbers were 1) 2B21-74SS156, RPV vent; 2) 2B21-44SS146, Rx. head ventj e

2 l to Clean Radwaste; 3) 2B21-701SS164, reactor vessel level instrument; 4) 2B21-701SS184 o

3

reactor vessel instrument line; 5) 2B21-34SS300, main steam relief valve F013H dis-l 0

6 l Charges; 6) 2PS-361S, sample line. As a result of these failures, surveillance fre-1 ol7 quencies have been changed per Technical Specifications.

I o

3 l Technical Specifications 3.7.5 and 6.9.1.9b.

I 80 7

8 9 SYSTEV

CAUSE

CAUSE COYP.

VALVE CODE COCE SUSCODE COMPONENT CODE SU8COCE SUSCODE o

9 lC lB @ lE l@ l X @ l S l U l P l 0 l R l T l@ l0 l@ lZ l @

7 a

3 to 11 12 13 18 19 20 SEQUEN TI AL CCCURRENCE REPCRT R EVISIO N

,_ EVENT YE AR REPORT NO.

CCDE TYPE NO.

h (LER RO7l9l l-l l0l3l6l l/l l0 l3 l lL l-l l0l El.gR T

_ 21 22 23 24 26 27 28 29 30 31 32 ACTION EvTURE EFFECT SHUTOOWN ATT ACHV EN T NP R O.4 PRIVE COMP.

COYPCN EN T TAKEN ACTION CN PLANT MET *CD HOURS 22 SUBVITTED FORMdt3.

SUPPL ER VANUFACTURER l X lgl34X l@

l Z l@

lZl@

l0l0l0l0 lNl@

lYl@

lBlZl0l9l@

N 33 25 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l The cause of failure in all snubbers was a low fluid level.

All snubbers were dis-I i

o i

l assembled, inspected, and rebuilt.

Seal leakace has been a nroblen in the we da I hydraulic snubbers in the drywell.

We are currently investigating the feasibility of i l switching to mechanical snubbers in the drywell.

3 1

I i

4 7

3 3 80 F ACILITY YETHOD OF STATUS

% POWER CTwER STATUS CISCOV E R Y DISCOVERY CESCRIPTION A

H l@ l 0 l 0 l 0 @l NA l

lBl@l Periodic Test i

e ACTIVITY CO TENT RELEA3ED Cc RELEASE AVOUNT CK ACTIVITY LCCATION OF RELE ASE 1 le lZ l @ l Z l@l NA l

l NA l

7 8 9 IJ 11 44 45 30 PERSO*..E L E x P03L A E3 N WSEA 1l7 0l0l0j@l TYPE @lOESCRIPTICN l

s NA 7

3 9 11 12 13 E0 PE A SON'.E L, yUn tES NUYPER C E SCR.PTON t

l0 l0 0 @l NA l

8 9 11 12 80 LO35 OF OP DC.' AGE TO F ACILITY TYPE CE3C AlPTION Z l@l NA 0

7 8 9 to 30 J "hlSECmPTm @ 790607028z

""c * "'"

NA l

llll llllll ll l; 1:

n 7

a a a

sa e s a ;;

A. C. Tollison, Jr.

919-457-6701 2,

N AYE OF PREPAPEP pag