ML19282B975

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Monthly Operating Rept for Feb 1979
ML19282B975
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 03/05/1979
From: Kennedy R
FLORIDA POWER CORP.
To:
Shared Package
ML19282B974 List:
References
NUDOCS 7903190187
Download: ML19282B975 (5)


Text

OPERATING DATA REPORT DOCKET NO. 50-302 DATE 3/5//9 C05!PLETED BY R. W. Kennedy TELEPHONE (904) 795-6486 OPERATING STATUS Notes

1. Unit Name: CRYSTAL RIVER #3
2. Reporting Period: 2/1/79 - 2/28/79 2452
3. Licensed Thermal Power (SIWt):
4. Nameplate Rating (Gross 51We):

890 825

5. Design Electrical Rating (Net Swe):
6. Staximum Dependable Capacity (Gross 31We):

835

  1. 97
7. 51aximum Dependable Capacity (Net 31We):
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted. If Any (Net SIWE):
10. Reasons For Restrictions. If Any:

This 51onth Yr..to.Date Cumulative

11. Hours in Reporting Period 672.0 - 1416.0 17232.0 _
12. Number Of Hours Reactor was Critical 664.6 1372.0 11229.2
13. Reactor Reserve Shutdown Hours 0 0 383.4
14. Hours Generator On.Line 659.0 1354.9 10899.5
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (51WH) 1540019 3111663 23708831 .
17. Gross Electrical Energy Generated (5tWH) 529401 _,

1067549 6065393 IS. Net Electrical Energy Generated (51WH) 503675 1013486 7643351

19. Unit Service Factor 98.1% 95.7% 63.3%
20. Unit Availability Factor 98.17. 95.77. 63.3%
21. Unit Capacity Factor (Using 51DC Net) 94.0% 69.84 55.77.
22. Unit Capacity Factor (Using DER Net) 90.9% 86.8% 53.8%
23. Unit Forced Outage Rate 1.9% 4.37. 34.5%
24. Shutdowns Scheduled Over Next 6 Stonths (Type. Date.and Duration of Each):

REFUELING SCREDULED 4-23-79,' PLANNED 6-8 WEEKS

25. If Shut Down At End Of Report Period, Estimated Date of Startup: ON LINE AT 1417 3/1/79
26. Units in Test Status t Prior to Commercial Operation): Forecast Achieved INITIAL CRITICALITY 1-14~77 INITIAL ELECTRICITY W-7 CO313f ERCIAL OPERATION 3-13-77 7903190177 elm

~ ~ ~ ~~

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-302 UNIT FLCRP-3 DATE 3/1/79 COMPLETED BY R. W. Kennedy TELEPHONE (904)795-6486 MONTH FEBRifARY 1979 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (Mwe-Net I 593 17 723 2 598 is 794 3 734 19 793 4 804 20 795 5

803 21 795 6

802 22 797 7 A1n 23 792 8 806 24 788 9 792 25 792 10 513 26 797 11 796 27 776 12 7A4 23 529 13 799 ,9 14 795 30 15 793 3, 16 589 INSTRUCTIONS On this format, list the average daily unit power levelin MWe-Net for each day in the reporting month. Compute to the nearest whole megawatt.

(W77i S . g

g e DOCKEFNO. 50 ~107 llNil SiltilllOWNS AND Powl:lt ItElitfCIIONS UNIINAME FT f'DP _ "I DALE _3/1/.79 COMPl.ETEl> i1Y R. W. Kennedy llEPOlll MONiil _EEBRITARY: 1979 TELEPflONE .(SQfd 7') S-L48(L It O C

, jE 'h - $3 I icensrc [-t, j1, Cause & Corrective No. Date g 3g @ jg5 1: vent D pu Action to H

f5 5 ygc itepint si vi u o

o Prevent itecurrence

(

O Power reduction to 76%; condensate pump 79-4 790130 F 0 B 4 I!!! PUMPXX out of service from 790130 (time 0514) until 790203 (time 0445). Reactor

". . remained critical from beginning of month.

79-5 790210 F 5.7 p llA TURBIN Eli supply line to turbine governor Al valve failed. Reactor remained critical 79,6 790216 S 0 F, -

RB CONROD Power reduction to 55% for 400 EF PD

, rod indexing 79-7 790228 F 7.4 A' !3 Ill. INSTRU Turbine tripped. Suspect momentary

, high level instrumentation signal from low pescure heater.

I 2 1 4 1:: Ionced Iteason: Metho<l: Exhibit G Instructions S: Si heiluteil A Equipinent Falkne (Explain) l-Manual In: Preparation of Data 11 Maintenance of rest 2-Manual Sciaan. Entry Sheets for I.ieensee C-Iteruelin:g 1 Automatic Sciaan. Event Iteroit (i.Ellt l'ile iNtilti G D-Itegulatory itestriction 4-Other Ilhplaini 0161I ILOperator Training & l.icense IT.nuination I: Adininistrative 5 G Operational I erm Il xpuin) Inhibit 1 Same Somce 19/77) ll Other fl% plaint

l M0flTHLY STATUS REPORT REFUELIflG If1FORMATI0fl REQUEST

1. flame of Facility: Crystal River Unit 3
2. Scheduled date of next refueling shutdown: Ap ril , 1979.
3. Scheduled date for restart following refueling: June, 1979.
4. Will refueling or resumption of operation thereafter' require a technical specification change or other license amendment? Yes.

In general, changes to the CR #3 technical specifications will include:

a. Moderator Temperature Coefficient (3.1.1.3)
b. Control Rod Insertion Limits (3.1.3.6)
c. Control Rod Group Assignments (3.1.3.7)
d. Axial Imbalance Limits (3.2.1)
e. Refueling Boron Concentration (3.9.1)

These specifications will be reviewed and changed as necessary based on the reactivity of the second cycle as compared to that of the first cycle.

5. Scheduled date(s) for submitting proposed licensing action and supporting information: February, 1979.
6. Important licensing considerations associated with refueling, e.g. ,

new or different fuel design or supplier, unreviewed design or perfor-mance analysis methods, significant changes in fuel design, or new opera-ting procedures.

Florida Power Corporation is presently discussing with the flRC staff our intent to request that the power level of CR #3 be raised from the present level of 2452 MW (t) to the ultimate core power level of 2544 MW (t) as described in the CR #3 FSAR. FPC submitted on February 28, 1979 our reload report justifying Cycle 2 operation of CR#3 at 2544 MW (t).

7. The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.

a) 177 assemblies -

b) 4 assemblies

8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, ia number of fuel assemblies.
a. Present storage capacity - pool A - 120 plus 8 failed fuel assemblies Pool B - 120 plus 8 failed fuel assemblies
  • n
8. (Continued)
b. Filed request on January 9, 1978 with NRC concerning expansion of Pool A from 120 to 544 assemblies plus 6 failed fuel assemblies and exoansion of Pool B from 120 to 609 assem-blies. Expansion of Pool A is to occur af ter the refuelino in April, 1979. The Pool B expansion will occur at a later refueling outage (approximately 1986).

Additional detailed design information co ..erning our fuel pool expansion was submitted to the Commission on March 3, March 22, 1978 and January 18, 1979.

9. The projected date of the last refueling that can be discharged to the spent fuel assuming the present licensed capacity. 1981-1982.

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