05000324/LER-1979-009-03, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced

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/03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced
ML19282B972
Person / Time
Site: Brunswick 
Issue date: 03/08/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19282B971 List:
References
LER-79-009-03L, LER-79-9-3L, NUDOCS 7903190184
Download: ML19282B972 (2)


LER-1979-009, /03L-0 on 790207:Bergen-Paterson Snubber 2E41-61SS99 Had Low Fluid Level.Caused by Leaking Seal.Seal Was Replaced
Event date:
Report date:
3241979009R03 - NRC Website

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8 60 61 DOCK E T Nt>MBER 68 69 EVENT DATE 14 75 HEPORT DATE 80 EVENT DESCHlPTION AND PROBABLE CONSEQUENCES h o

2 l While performinn P.T.

19.6.0.2 vis ual Inspection of Accessible Snubbers, Bergin -

l 1o a l Paterson snubber 2E41-61SS99 was found to have a low fluid level due to a leaking l

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LER CONTINUATION -- RO# 2-79-9_

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Event Date 2-7-79 BSEP Unit #2 of Unit 2 (1974 - 1975). This is considered an isolated event as proper seals were found in all past snubbers inspected since the unit became operational.

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