ML19274D761

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IE Insp Repts 50-313/78-21 & 50-368/78-28 on 781120-1217. Noncompliance Noted:Failure to Properly Approve Changes to Procedure 1304.30 Re Hydrogen Analyzer & Flow Indication Instrument Surveillance
ML19274D761
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 01/04/1979
From: Madsen G, Verduzco G, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML19274D757 List:
References
50-313-78-21, 50-368-78-28, NUDOCS 7902260022
Download: ML19274D761 (17)


See also: IR 05000313/1978021

Text

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U. S. NUCLEAR REGULATORY C0:@lISSION

OFFICE OF IllSPECTION AtlD EllFORCEMEllT

REGIO:1 IV

Report flos. 50-313/78-21

50-368/78-28

Docket Nos. 50-313

Lic;nse No. DPR-51

50-368

Construction Permit No. CPPR-89/

Facility Operating License llPF-6

Licensee:

Arkansas Power and Light Company

P. O. Box 551

Little Rock, Arkansas 72203

Facility Name: Arkansas fluclear One (Af!0), Unit !!os.1 and 2

Inspection At: Afl0 Site, Russellville, Arkansas

Inspection Condu ted: November 20 - December 17, 1978

Inspectors:

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9'

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T. F. Westerman, Reactor Inspector

Date

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G. H. Verduzco,Jeactor Inspector

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h. W. Dickerson, Reactor Inspector

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E. A. Cupp, R(attor Inspector

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h. 6. Spangler',T/ReacAor Inspector

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Approved By:

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,G. L. fladsen, Chief, Reactor Operations and

Date

Nuc1 car Support Branch

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Inspection Summary

Inspection during period of November 20 through December 17,1978 (Report

No. 50-313/ 78-21

Areas Inspected: Routine, cnnounced inspection of plant operations; design,

design changes and modifications; follow up on previous unresolved items;

and independent inspection effort. The inspection involved 99 inspector-hours

on-site by four NRC inspectors.

Results: Within the four areas inspected, one item of noncompliance was

identified relative to changes to procedures (paragraph 9, Infraction).

Inspection during period of November 20 through December 17, 1978 (Report

No. 50-368/78-28)

Areas Inspected: Routine, announced inspection of design, design changes and

modifications; preparation for Operating License issuance; witness of initial

criticality; low power physics testing; Technical Specification required

calibration; non-Technical Specification required calibrations; and

independent inspection effort.

The inspection involved 74 inspector-hours

by three NRC inspectors and 187 hours0.00216 days <br />0.0519 hours <br />3.091931e-4 weeks <br />7.11535e-5 months <br /> by the resident inspector.

Resul ts: Within the seven areas inspected, three items of noncompliance were

identified relative to surveillance testing (paragraph 11.b(2) - two Infractions),

and calibration records (paragraph 8 - Deficiency).

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DETAILS

1.

Persons Contacted

Arkansas Power & Light Company Employees

J. P. O'Hanlon, ANO Plant Manager

G. H. Miller, Acting AN0 Plant Manager

L. Alexander, QC Engineer

J. R. Anderson, Assistant Production Startup Supervisor

B. A. Baker, ANO-2 Operations Supervisor

T. N. Cogburn, Nuclear Engineer

E. C. Ewing, Production Startup Supervisor

D. R. Hamblin, QC Engineer

T. Holcomb, Scheduler

P. Jones, Maintenance Supervisor

S. M. Strasner, QC Technician

B. A. Terwilliger, Supervisor Plant Operations

J. Robertson, ANO-1 Operations Supervisor

S. Petzel, Licensing Engineer

D. Williams, Licensing Manager

F. Foster, Mechanical Maintenance Supervisor

M. Stroud, Electrical Maintenance Supervisor

G. Bruss, Shift Supervisor (Unit 2)

R. Weaver, Shift Supervisor (Unit 2)

L. Bell, Shift Supervisor (Unit 2)

Roark, Assistant Electrical Supervisor

n.

J. Lowman, Assistant I&C Supervisor

R. Elder, I&C Supervisor

R. Tucker, Assistant I&C Supervisor

R. Turner, Assistant I&C Supervisor

J. Waxenfeller, Assistant I&C Supervisor

J. McWilliams, Planning & Scheduling Supervisor

D. Hamblin, QC Inspector

R. Beta, QA Engineer

2.

Plant Status

Unit 1

Steady state 90% power operation.

Unit 2

Power ascension testing in progress.

Some problems experienced with

control drive upper mechanisms, control of steam generator levels at

low power level and steam dump valve operation.

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3.

Inspector Follow Up on Previously Identified Items (Unit 1)

(Closed) Unresolved Item (Inspection Report 50-313/77-13, paragraph 2):

Conflicts between the Quality Assurance Procedure and the Nuclear

Services Procedure in the area of 'Q' design changes.

The QAP Procedure 1004.01, revision 4, and Generation and Construction

Procedure II-5 which supersedes NSP-II-5 are no longer in conflict.

4.

Review of Plant Operations (Unit 1)

The inspector reviewed plant logs and records to verify conformance to

plant procedures and to confirm that Technical Specifications were met.

The inspector also conducted a plant tour of accessible areas to observe

general housekeeping and to verify selected component configurations.

The following logs and records for October and November 1978 were

reviewed:

Station Log

NSS Data Point Log

NSS and Safeguard Auxiliary Log

RPS Log

Auxiliary Log - Inside

Auxiliary Log - Outside

Waste Control Log

Boron Titration Log Sheets

Hot Lab Technical Specification Surveillance Report

ESAS Log

Station Battery Daily Check Log

Daily Reactor Power History Log

Quadrant Tilt and Imbalance Log

Trouble Tickets

Reactor Trip Recovery Procedure for October 13, 1978

During this review of logs and records, the inspector noted that the

Unit 1 Outside Auxiliary Log had no entry for the Emergency Pond Level

on November 22, 1978 as required by Technical Specification 4.13.1.

A

check of Unit 2 Outside Auxiliary Log showed that the pond level had

been checked and recorded on that date by Unit 2 personnel. This was

discussed with the Unit 1 operations supervisor and resolved.

The following general observations were made during the plant tour:

No excessive fluid leaks or piping vibrations were observed.

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Seismic restraints 2nd pipe hangers appeared to be in satisfactory

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condition.

Selected valves were observed to be in the required positions.

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Selected equipment caution and hold tags were verified to be

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correct.

Control room operators were knowledgeable in annunciator status.

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Selected recorders were recording properly.

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Radiation controls were observed to be established properly.

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Control Room manning was in accordance with Technical Sreci fications .

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Furthennore, the inspector noted that general cleanliness s as excellent

with the exception of the Unit 1 cable spreading room.

The licensee's

representatives indicated, prior to the conclusion of this inspection,

that actions had been initiated to correct the above.

However, the

inspector indicated a concern for the control of combustible substances

in areas such as the cable spreading room.

This item is considered

an open item.

No items of noncompliance or deviations were noted.

5.

Design, Design Changes and Modifications (Unit 1 and Unit 2)

The inspector reviewed the Controlling Procedure 1004.01 (Rev. 4),

Design Control for ANO Units 1 and 2, and selected design changes to

determine that these changes and modifications are in conformance with

the requirements of the Technical Specifications and 10 CFR 50.59.

The following design changes were selected fr

-aview:

DCR Number

Title

555

H Purge

' em Seal Water Disposal Modification

7

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557

VTtal Elt.orical Equipment Rooms Temporary Fans

570

Replacement of RCS Pressure Transmitters with

Rosemont Models

571

Replace Blocking Diodes in Diesel Generator

Control Circuits

575

Control Room Isolation Valves for HVAC - CV7905,

CV 7906 and CV 7907

584

Remove 3/4" Half Coupling and DH-1010 Vent Valve

It appears that these DCR's were conducted in accordance with formal

procedures, that applicable acceptance tests were completed, and that

changes to operating procedures as required were made. The inspector

did note that although mast of these OCR's were completed during the

March 1978 refueling outage, the as-built drawings had not been updated

to reflect more than the fact that a DCR was outsta.1 ding.

Following the

completion of work on a DCR, the Little Rock Engineering Office is

notified and requested to issue upd 'ed drawings.

There is apparently

a significant delay in the turnarour.a time for the above.

This item will

be an open item.

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No items of noncompliance or deviations weie identified in the above

DCR's for Unit 2 will be reviewed dm ing a future inspection.

area.

6.

Closcout of Mode 2 Open _ Items - Attachment 2 to Operating License

NPF-6 Amendment 7 (Unit 2)

a.

Item A.1 - Startup Punchlist

Heating in the PPS panels is still under review. With the cabinet

doors left open, there appears to be no loss of power supplies due

to heating.

The inspector was informed that a seismic analysis

with doors open has been performed.

The licensee has stated that

resolution of this problem will be pursued.

RIV does not consider

this item a further hold to entering Mode 2; however, the licensee's

resolution of this problem will continue to be followed.

b.

Item A.2 - Completion of Preoperational Test

All testing and modifications of the main steam safety relief valves

have been completed.

These actions include the following:

Hydraset of all valves

.

Verification of set point by actual lifts

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Adjustment and modification of valve internals to improve

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blowdown

Verification of blowdown to be c512%

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Analysis was conducted by the NSSS which shows up to 15%

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blowdown acceptable

Valve locking pins were replaced and valve PSV-1002 tested

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to demonstrate the adequacy of the design change

There are no further deficiencies against Preoperational

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Test 2.083.01

This item is considered closed.

c.

Item A.3 - Startup Program Test Deficiencies

The inspector verified that all 2.650 series test deficiencies

impacting on Mode 2 have been cleared.

This item is considered closed.

d.

Item A.4 - Approval and Issuance of 2.800.01, App. U

This item has been closed.

(See Inspection Report 50-368/78-25)

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e.

Item A.5 - Containment Piping Penetration Main Feedwater Line

Break Modifications

This item has been closed.

(See Inspection Report 50-368/78-26)

f.

Item A.6 - Radiation Protsetion

(1)

Item 6.a - Installation and Calibration of HP Monitoring

Equipment

The inspector verified installation if a Hand and Foot Counter

and a Portal Monitor at the exit of i he Unit 2 auxiliary

building.

The inspector also verified the availability of

two CAM's for Uni- 2.

Each of these monitors identified

above were verified to have valid calibrations.

This item is considered closed.

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(2)

Item 6.b - Area Radiation Monitors

This item has been closed.

(See Inspection Report 50-368/78-26)

(3)

Item 6.c - Process Radiation Monitors Calibration

The inspector verified the following monitors were calibrated

in accordance with Plant Calibration Procedure 2304.27,

Revision 1:

2RITS - 8271-2A

2RITS - 8231-1A

2RITS - 8233

2RITS - 8231-1B

2RITS - 8271-2B

2RITS - 8750-1

This completes calibration of all Technical Specification

required monitors.

This item is considered closed.

g.

Item 7 - Hanger Installation

This item has been closed.

(See Inspection Report 50-368/78-26)

h.

Item 8 - Penetration Breaker DC Power Supplies

This item has been closed.

(See Inspection Report 50-368/78-26)

1.

Item 9 - Facility Operating Procedures

This item has been closed.

(See Inspection Report 50-368/78-26)

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Item 10 - Resolution of Hydrogen Purge System Discrepancies

This item has been closed.

(See Inspection Report 50-368/78-26)

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Item 11 - LPSI Pump Motor Failure

This item has been previously closed.

(See Inspection Report

50-368/78-26)

1.

Item 12 - Safety Injection System Loose Part

This item has been previously closed.

(See Inspection Report

50-368/78-26)

m.

Ite. 43 - Conform oce to GDC-17 Off-Site Power Deficiencies

The inspector verified the following:

Surveillance procedures have been revised to provide for

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verification of breaker position.

All breakers (A&H) to SU Transformer 2 for Units 1 and 2

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have been red tagged and are in the pull to lock position.

Standing Orders have been issued which limit loading only

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one H (6.9 KV) and one A (4160 V) bus from either plant.

This item is considered closed.

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Item 14 - Resolution of Inverter Deficiencies

This item has been closed.

(See Inspection Report 50-368/78-26)

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Item 15 - Chloride Swipes Within Containment

This item has ' cen closed.

(See Inspection Report 50-368/78-26)

p.

Item lo - Resolution of Diesel Generator tio. 2 Failure

Three successive failures of Emergency Diesel Generator fio. 2

were experienced. The initial failure of the diesel generator

damaged the upper crank shaft and wiped the main bearings on the

upper crank shaft during a surveillance test.

The next two

failures wiped main bearings on the upper shaft prior to

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completion of the vendor's reconmended break in test. This same

diesel had experienced multiple failures in the vendor's shop

prior to shipment to the site.

Investigation into the cause of engine failure indicates a

possible aeration problem in the lube oil and a possible uneven

expansion problem.

Although the lube oil in the engine at the

time of the failures was tested and found to be within specifi-

cation, the oil was changed to another brand and adjustments

were made to the forward mounting bolts to reduce possible

uneven expansion.

Popping noises had been observed during the

contraction of the engine after each run.

Following the last repairs, the engine appeared to perform satis-

factorily. The engine was run in accordance with the vend _or's

recommended break in test.

The engine was then load tested for

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with Regulatory Guide 1.108.

Vib ution

readings on the engine indicated a decreasing amplitude through-

out the final testing. The amplitude of the vibrations had

increased during earlier testing.

There was a general reduction of the aeration of the oil and

elimination of the popping noise coming from the engine. The

repairs and testing were witnessed in part by the IE Resident

Inspecto.'.

RIV plans no further action on this item.

The performance of the

diese'.s will continue to be observed by the Resident Inspector,

q.

Item 17 - Resolutio'n of CRD-58 Failur'

Exercising of the upper control rod drive (CRD) mechanism as

recommended by the NSSS appears to re~ solve the inoperability of

CRD-58.

This item is considered closed.

7.

Closecut of Mode 1 Open Items - Attachment 2 to Operating License

NPF-6 Amendment 7 (Unit 2)

a.

Item 1 - Startup Punchlist

The inspector verified that all items on the startup punchlist

have been closed.

This item is considered closed.

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b.

_ Item 2 - Operations Punchlist

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The data for the CECEC Code verification is to be taken on

brush recorders. There are sufficient brush recorders on site

between the licensee and the NSSS to perform this test'ng.

This item is considered closed.

8.

Calibration - Technical Specification Specified (Unit 2)

The inspector reviewed surveillance records, procedures, qualification

of individuals performing calibrations and held discussions with repre-

sentatives of the licensee to determine whether the calibration of

components and equipment were in conformance with the requirements of

the Technical Specifications (TS).

However, no calibrations were witnessed

since no T/S required calibrations were scheduled during the inspection.

Records of the following calibrations were reviewed:

Linear Power Level - High, Channel A

Pre-Operational Procedure 2.058.01, Plant Protection, completed

December 27, 1977.

Procedure 2304.100, Excore Instrument Channel A Test.

Steam Generator Pressure Low - Channel A

Pre-Operational Procedure 2.058.01, Plant Protection, completed

January 25, 1978.

Job Order 4836-2, completed November 8,1978 in accordance with

letter A-CE-7280.

DNBR - Low Channel A.

Pre-Operational Procedure 2.053.02, Core Protection Calculator,

completed July 20, 1978.

Pressurizer Pressure - Low, Channel A

Pre-Operational Procedure 2.058.01, Plant Protection, completed

December 28, 1977.

Job Order 4836-2, completed November 8,1978 in accordance with

letter A-CE-7280.

Containment Pressure - High, Channel A

Pre-Operational Procedure 2.058.01, Plant Protection, completed

December 27, 1977.

460 Volt Emergency Bus Unc_rvoltapa (Degraded Voltage)

DCR 649, completed April 24, 1978 for Relays 27-1/285

and 27-1/286.

DCR 251, completed October 29, 1978 for Relays 27-2/2B5 and

and 27-2/286.

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Primary Standards

DVM #6, calibrated October 16, 1978

OSC #01, calibrated November 22, 1978

PAS #03, calibrated July 27, 1977

As a result of the review, it was determined that records were not

available which would substantiate that the steam generator low

pressure trip and pressurizer pressure low trip settings for Channels

A, B, C and D were calibrated in accordance with the appropriate

plant procedures.

Changes to the trip settings were made under

J.0. 4836-2, but there were no completed data sheets.

Representatives

of the licensee stated that appropriate portions of Procedures 2304.41,

2304.42, 2304.43 and 2304.44 (Plant Protection System Channels A, B,

C and D calibration, respectively) had been utilized but had apparently

become separated from the job order and lost.

The licensee also

indicated that the set points had been checked since completion of

the job order.

The licensee was informed that failure to maintain these records was

contrary to Technical Specification 6.10.1.d which requires that

records of surveillance activities, inspections and calibrations

required by the Technical Specifications be retained for at least five

years and is considered a deficiency.

The inspector had no additional questions in this area.

9.

Calibration - Safety Related not T/S Specified (Unit 2)

The inspector reviewed calibration records, procedures, qualification

of individuals perfsrming calibration and held discussions with repre-

sentatives of the licensee.

No calibrations were witnessed since no

calibrations were scheduled during the inspection.

Records of the

following calibrations were reviewed:

2LlS-5028 and 2LT-5028 Safety Injection Tank 2T2B Level, calibrated

October 10, 1978

2PlS-50J2 Safety Injection Tank 2T2B Pressure, calibrated March 28,

1977

2LT-5636-1 Refueling Water Tank Level, calibrated October 15, 1978

2 TIS-5675 Refueling Water Tank Temperature, calibrated September 9,

1978

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2L15-5659-1 Sodium Hydroxide Tank Level, calibrated September 14, 1978

2TlS-5670 Sodium Hydroxide Tank Temperature, calibrated February 24,

1978

2LT-1977 Condensate Storage Tank Level, calibrated Augu: t 26, 1977

2LT-1937 Condensate Storage Tank Level, calibrated October 2;

1976

2L1-2801 Emerger .y Diesel Day Tank Level, calibrated January 5,1977

2L1-2821 Emergency Diesel Day Tank Level, calibrated January 5,1977

1304.80 Emergency Cooling Pond Sounding, completed August 10, 1978

Primary Standards

DWT #6, calibrated October 1977

DMM #31, calibrated August 14, 1978

CAL #9, calibrated May 10, 1978

The inspector als.o selected calibration of the Unit 2 Hydrogen Analyzer

for review.

However, it was determined during the inspection that

calibration of this instrument had not been completed but was required

before entering Mode 2 operation.

The inspector did, however, review

records of the calibration, dated March 17, 1978, for the Unit 1

Hydrogen Analyzer. These consisted of Procedure 1304.30 Hydrogen

Analyzer and Flow Indication Instrument Surveillance and the associated

records.

During this review it was determined that changes had been

made to the procedure without the required approval for the changes.

Changes were made to the accuracy required and to the desired output

for Instruments SQT-7441, SQT-7451, SQT-7442 and SQT-7452.

While the

changes appear to have been proper, Technical Specification 6.8.3.b

spe'ifies that temporary changes to procedures required by TS 6.8.1

be approved by two members of the plant staff, at least one of whom

holds a Senior Reactor Operator's License on the unit affected.

Since this was not done, the licensee was inforned that the use of the

changed procedure without the required approval constituted an item of

noncompliance.

From the review of the records for calibration of level instruments

2L1-2801 and 2L1-2821 for the Emergency Diesel Day Tank, it was found

that the data sheets did not include a specified accuracy. A represen-

tative of the licensee indicateu that this would be corrected by requir-

ing an appropriate specified accuracy for the instruments.

This item

remains as an open item.

The i'spector had no additional questions in this area.

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10. Witness of Startup Activities (Unit 2)

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The following startup activities were witnessed by the inspector:

Plant Safety Committee (PSC) Meetings

a.

The inspector observed the December 3,1978 PSC meeting.

This

was the final review of test discrepancies prior to going to

Mode 2.

b.

Test Working Group (TWG)

The inspector observed, on a part-time basis, TWG meetings of

December 1 and 3,1978.

c.

Scheduling

The inspector continued to observe the daily startup meetings

during the period covered by this report.

d.

_2.750.01, Revision 2, Low Power Physics Testing

The inspector completed review of 2.750.01 through December 13,

1978.

_ Test Program Chronological Log

e.

The inspector completed review of this log through December 13, 1978.

11.

Inspector Witnessing of Initial Criticality (Unit 2)

a.

Scope of Inspection

The following items were reviewed prior to control rod withdrawal:

Conformance to selected Technical Specifications

.

Calibration of excore nuclear instrumentation

.

Proper count rate and signal-to-noise ratio

.

Instrument trip checks performed

.

The following items were reviewed for conformance to administrative

and procedure requirements:

~

Crew staffing of licensed operators

.

Latest version of Plant Procedure 2.700.02,

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Revision 2, " Initial Criticality" available.

Verified selected prerequisites satisfied

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Special count rate instrumentation in place

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Inverse multiplication plots maintained

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Adequacy of on-site technical support

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Control room log

.

The following items of the "as-run" procedure were reviewed for

adequacy:

Control of procedure changes

.

Revieu of test deficiencies

.

Completeness of data sheets

.

The following items relative to test results evaluation were

reviewed:

Calculation of boron concentration for criticality using

.

licensee's procedure

Dilution calculations

Observation of boron analysis

Comparison of actual critical boron concentration to predicted

.

b.

Findings

(1) The measured boron concentration at criticality was 978 ppm

0

at 260 F with group 6 cor.crol rods at 75".

The predicted was

996 ppm with a + 100 ppm acceptance criteria.

(2) During the review for conformance to Technical Specifications

the inspector identified the following two items of noncom-

pliance:

(a) Technical Specifications 6.8.1 states in part that,

" Written procedures shall be established, implem'ented

and maintained for the activities referenced below:

...

c.

Survaillance and test activities of safety related

equipment." Plant Procedure 1004.12B, Revision 0,

Operational Test Control states in part with regard to

surveillance test scheduling, "To ensure that required

tests are performed within the specified interval, each

Plant Supervisor designated on the Master Test Control

List shall be responsible for establishing and maintaining

a departmental test control chart.

The test control chart

shall list all required tests under the cognizance of that

group, the test interval, scheduled date and date actually

performed."

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Contra.y to the above, the inspector found that the

test control charts were not being maintained current.

Examples of the failure to implement procedures include

the following:

I&C Test Control Charts

Eighteen month tests of the incore detectors and optical

isolators had not been incorporated into the test control

charts.

Scheduled dates for test completion were not shown in

some cases.

Maintenance Test Control Charts

Electrical test control chart was not being maintained

current. The flow of completed surveillance test paper-

work bypassed the designated supervisor.

Technical Test Control Chart

The schedula of testing was not being maintained current,

i.e., Main Safety Valve Testing for conformance to ASME

Section XI.

(b) Technical Specification, Table 4.3-4, Item 3, specifies

that the Triaxial-Response-Spectrum Recorder 2XR-8350 is

to receive a " Channel Functional Test" on a semiannual

"SA" frequency.

Contrary to the above, the interval of functional testing

for 2XR-8350 had exceeded six months between the period

of April 5,1978 to December 8,1978.

(3) The inspector observed one of the Intake Structure Exhaust

Fans 2VEF-25B (Hand Switch 2HS-8094 - 2SIAS MSIS) in a pull to

lock condition. The lic.ensee has indicated this hand switch

will be left in the auto position during conditions when the

Service Water System is required by Technical Specifications.

The operability of these fans is necessary under accident

conditions.

12.

Inspector Witness of Low Power Physics Testing (Unit 2)

a.

Scope

The inspector verified the following:

Appropriate procedure in use

.

Crew requirements

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Initial conditions and prerequisites met

.

Calibration and inservice use of test equipment

.

Proper control of test changes

.

Coordination of crew activities

.

Quick summary of test results

.

Proper collection of test data

.

Compliance with the test acceptance criteria

.

Adequacy of the licensee's test evaluation

.

Compliance with Technical Specifications

.

Resolution of test deficiencies

.

Adequacy of data sheets

.

The tests witnessed by the inspector included the following:

Pseudo rod ejection worth

.

Isotherral temperature coefficient

.

Control rod group worths

.

Boron concentration at all rods out position

.

Functional checkout of the reactivity computer

.

Each of the tests referenced above are included as an integral

part of Test Procedure 2.750.01, Revision No. 2, " Low Power

Physics Test."

b.

Findings

(1) The control rod initially predicted to be the most reactive

ejected rod was CEA 6-1 with a predicted worth of 0.348%

a k/k. The . measured worth of this control rod was 0.322%

a k/k which is well within the acceptance criteria of + 0.1%

a k/k.

The next most reactive control rod was predicted to

be CEA 4-11 with a predicted worth of 0.277% a k/k.

The

measured worth of this control rod was 0.345% a k/k, which

made it the most reactive.

It is still within the acceptance

criteria of + 0.1% a k/k.

The vendor subsequently found an

error in the ejected rod analysis.

CEA 4-11 was reanalyzed

as the most reactive ejected rod with a predicted worth of

.376% a k/k.

No further action on this item is considered

necessary by RIV.

(2) Due to problems in the control rod circuitry, there were a

number of rod misalignments <

to rod drops. These misalign-

ments were not a planned par t of the low power physics

testing program.

The licensee plans to make one 30 day

report to cover these events.

The start date for the report

is to be no later than the first drop in Mode 2.

. , . . ,,.

-17-

(3) The licensee has concurred that the test records associated

with the reactivity computer wil' be maintained as a part

of the permanent plant record.

This will include the

alignment check of the reactivity computer, , calibration

of vendor Digital Volt Meter, voltage sources, and picoamp

meter scale alignments.

(4) No items of nonccmpliance or deviations were identified during

this portion of the inspection.

13.

Exit Meetings (Units 1 and 2)

Exit meetings were conducted on November 24 and December 1,1978 with

Mr. Miller (Acting Plant Manager) and other members of the AP&L staff;

and on December 15, 1978 with Mr. J. O'Hanlon (Plant Manager) and other

members of the AP&L staff.

The inspectors discussed the scope of the

inspection and summarized the inspection findings which are detailed in

this report.