05000324/LER-1978-076-03, /03L-0 on 781202:during Routine Check Noted That Recorder for Chloride Intrusion Monitor Channel CO-CIS-3075- 1 Was Not Indicating.Cause Not Determined at This Time,Will Be Investigated During Next Condensate Sys Outage

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/03L-0 on 781202:during Routine Check Noted That Recorder for Chloride Intrusion Monitor Channel CO-CIS-3075- 1 Was Not Indicating.Cause Not Determined at This Time,Will Be Investigated During Next Condensate Sys Outage
ML19274D150
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/05/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19274D145 List:
References
LER-78-076-03L, LER-78-76-3L, NUDOCS 7901150103
Download: ML19274D150 (1)


LER-1978-076, /03L-0 on 781202:during Routine Check Noted That Recorder for Chloride Intrusion Monitor Channel CO-CIS-3075- 1 Was Not Indicating.Cause Not Determined at This Time,Will Be Investigated During Next Condensate Sys Outage
Event date:
Report date:
3241978076R03 - NRC Website

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EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h o

2 l During a routine panel check on 12/2/78, the Control Operator noticed that the recor-1 der for chloride intrusion monitor channel CO-CIS-3075-1 (Condensate Pump Discharge) o 3

o.: lwas not indicating. Further investigation revealed that the detector was malfunction-l o

5 ling. Technical Specification 3.3.5.6.

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o l Since the condensate system must be out of service to remove the detector. it will be1 1

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