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LER-1980-104, /03L-0:on 800711,while in Normal Shutdown mode,4 Kv Emergency Switchgear 2F Normal Supply Breaker Tripped & Swapped to Alternate Supply Breaker Which Also Tripped. Caused by Missing Jumper Resulting from Const Fault |
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| 3661980104R03 - NRC Website |
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LoRJ l on 7-11-80, 8:00 AM EDT while in the normal shutdown mode,_the 4 KV_em__j lergency switchgear 2F normal supply breaker tripped, and the switchgear I o
3 l swapped to the alternate supply breaker which subsequently trip _ ped at j
o 4
l2:00 PM EDT.
The 2F bus was then inoperable per Tech Specs 3.8.2.1.a.
I [o
n l An overload condi tion was suspected.
Load was reduced and normal supply 1 o
c lwas restored.
There were no effects upon public health and safety due l
o i
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33 34 35 36 Je 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lilOllAt 4:00 PM EDT, a jumper was discovered missing in relaying current I
i i lloops.
By 6:00 PM EDT, the jumper was installed.
The cause of the 1
l1 2i l missing jumper was a construction deficiency.
This event is non-repet-l litive.
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'800811OYM 912-367-7781 2,
NAME Of rHLPAHtH C. L. Caggin. Sunt. P1t. Fno. Serv.
enoye
LER #:
50-366/1980-104 Licensee-Georgia Power Company Facility Name:
Edwin 1.
ll a t c h Docket #:
50-366
Narrative
Report for LER 50-366/1980-104 On 7-11-80, 8:00 AM EDT while in the normal shutdown mode, the 4 KV emergency switchgear 2F normal supply breaker
- tripped, and the switchgear swapped to the alternate supply breaker which subsequently tripped at 2:00 PM EDT.
The 2F bus was then considered inoperable (per Tech Specs 3.8.2.1.a).
Following each trip, the "B"
diesel started and was available for powering the switchgear, if required.
An overload condition was suspected as the cause of the trips.
Load was reduced on the bus and the normal and alternate supply breakers were restored to service.
The neutral overcurrent protective relay for each supply breaker had operated.
Current readings were taken at this relay, and the neutral current was discovered to be abnormally high.
Current readings were chec,ked on the feeder loads and found to b'c acceptabic.
At 4:00 PM EDT on the same
- date, a
jumper was discovered missing within the 4 KV emergency switchgear 2F normal and alternate supply metering / relaxing current loops.
As a result of the missing
- jumper, the normal and alternate supply breakers misinterpreted normal fully loaded current conditions as an overloaded / unbalanced condition.
This jumper did not affect diesel breaker availability.
By 6:00 PM
- EDT, the jumper had been installed thereby restoring the current loop to its original design.
Current readings in the neutral icg were taken and found to be acceptable.
Current readings were also taken at switchgear 2E and 2G to verify that a similar condition did not exist.
The
cause
of the missing jumper was apparently a
construction deficiency.
This event is not repetitive in nature.
There was no disruption in reactor shutdown activities as a result of losing switchgear 2F.
The unit is now in full compliance with the requirements, and no further reporting is required.
There were no effects upon public health and safety due to this event.
Similar current checks were made on Unit I and found OK.
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| 05000321/LER-1980-001-01, /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | /01T-0:on 800103,while Performing Maint on RHR LPCI Injection Valve,Clevis Pin Found Missing from Strut on Drywell Penetration Restraint.Caused by Improper Installation.New Clevis Pin Installed | | | 05000366/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000366/LER-1980-001-03, /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. Transmitter Recalibr & Returned to Svc | /03L-0:on 800102,while Performing Narrow Range Torus Water Level Functional Test & Calibr,Level Transmitter 2T48-N021B Found Out of Tolerance.Caused by Range Drift. 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Caused by Design Deficiency.Design Change Request & Maint Request Implemented to Add Supports | | | 05000321/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000366/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000321/LER-1980-012-03, /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | /03L-0:on 800122,while Reactor Core Isolation Cooling Sys Was Tagged Out for Maint,Hpci Was Found Inoperable,Requiring Orderly Shutdown.Caused by Leak in Line to HPCI Booster Pump Discharged Pressure Gauge | | | 05000321/LER-1980-013, Forwards Updated LER 80-013/03X-1 | Forwards Updated LER 80-013/03X-1 | | | 05000321/LER-1980-013-03, Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | Reactor Recirculation Pump a Tripped Causing Power Reduction.Caused by Electrical Short Circuit Due to Steam Leak in Drywell.Terminal Board Replaced & Tested | | | 05000366/LER-1980-013-03, /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | /03L-0:on 800203,while Maint Was Performed on 2082-K002 Static Inverter,Emergency Control Transfer Switch Was Placed in Emergency Position.Reactor Core Isolation Cooling Was Rendered Inoperable.Caused by Personnel Error | | | 05000366/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000366/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000366/LER-1980-014-03, /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | /03L-0:on 800204,while Performing HNP-2-3054, Average Power Range Monitor C Failed.Caused by Instrument Drift.Instrument Adjusted Per Procedure & Returned to Svc | |
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