05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
05000346/LER-1998-002, :on 980410,plant Tripped Due to High Pressurizer Level as Result of Loss of Letdow Capability. Makeup & Purification Demineralizer 3 Was Isolated Following Trip & Tagged OOS1998-05-10010 May 1998
- on 980410,plant Tripped Due to High Pressurizer Level as Result of Loss of Letdow Capability. Makeup & Purification Demineralizer 3 Was Isolated Following Trip & Tagged OOS
05000346/LER-1997-012, :on 970904,decay Heat Cooler Seismic Design Inadequacy Occurred.Caused by Inadequate Design of Decay Heat Coolers Support Sys.Decay Heat Cooler Mounting Support Sys Will Be re-evaluated & Modified1998-05-10010 May 1998
- on 970904,decay Heat Cooler Seismic Design Inadequacy Occurred.Caused by Inadequate Design of Decay Heat Coolers Support Sys.Decay Heat Cooler Mounting Support Sys Will Be re-evaluated & Modified
05000346/LER-1998-001-02, :on 980407,main Steam Safety Valves Setpoints Were Outside of TS Allowable Values.Cause Will Be Investigated.Setpoint of Valve Adjusted to Be within Allowable Value1998-05-0606 May 1998
- on 980407,main Steam Safety Valves Setpoints Were Outside of TS Allowable Values.Cause Will Be Investigated.Setpoint of Valve Adjusted to Be within Allowable Value
05000346/LER-1997-008, :on 970318,inadequate Testing of Safety Related Logic Was Discovered.Caused by Surveillance Test Review Process Not Technically Detailed Enough to Ensure All Functions Addressed.Performed 18-month Surveillance Test1998-02-25025 February 1998
- on 970318,inadequate Testing of Safety Related Logic Was Discovered.Caused by Surveillance Test Review Process Not Technically Detailed Enough to Ensure All Functions Addressed.Performed 18-month Surveillance Test
05000346/LER-1997-016-01, :on 971217,monthly ECCS Valve Position SR Was Missed.Caused by Flow Path That Was Not Part of Contiguous ECCS Flow Path Envisioned for Compliance W/Ts 4.5.2.Verified Valves Open on 9712221998-01-16016 January 1998
- on 971217,monthly ECCS Valve Position SR Was Missed.Caused by Flow Path That Was Not Part of Contiguous ECCS Flow Path Envisioned for Compliance W/Ts 4.5.2.Verified Valves Open on 971222
05000346/LER-1997-015-01, :on 971212,discovered That EDG Tachometer Circuit Was Outside of 10CFR50 App R Design Basis.Caused by Inadequate Development & Review of Mod 84-0183.Hourly Fire Watch Established & Mod to EDG Tachometer Made1998-01-12012 January 1998
- on 971212,discovered That EDG Tachometer Circuit Was Outside of 10CFR50 App R Design Basis.Caused by Inadequate Development & Review of Mod 84-0183.Hourly Fire Watch Established & Mod to EDG Tachometer Made
05000346/LER-1997-014-01, :on 970801,pressurizer PORV Setpoint Was Less than Allowable Value.Caused by Degraded Wire Splice.Wire Containing Faulty Splice Was Replaced1997-11-26026 November 1997
- on 970801,pressurizer PORV Setpoint Was Less than Allowable Value.Caused by Degraded Wire Splice.Wire Containing Faulty Splice Was Replaced
05000346/LER-1997-013, :on 971002,potential Condition Adverse to Quality Rept Documented Failure to Perform Surveillance Test Before TS Surveillance Late Date.Caused by Administrative Error.Missed Surveillance Completed1997-11-0303 November 1997
- on 971002,potential Condition Adverse to Quality Rept Documented Failure to Perform Surveillance Test Before TS Surveillance Late Date.Caused by Administrative Error.Missed Surveillance Completed
05000346/LER-1996-009, :on 961113,failure to Apply GL 91-18 to EDG Surveillance Testing Occurred.Caused by Personnel Error. Review of GL 91-18 Was Provided to Plant Operations & Plant Engineering Personnel1997-10-24024 October 1997
- on 961113,failure to Apply GL 91-18 to EDG Surveillance Testing Occurred.Caused by Personnel Error. Review of GL 91-18 Was Provided to Plant Operations & Plant Engineering Personnel
05000346/LER-1997-008, :on 970318,inadequate Testing of safety-related Logic Occurred.Caused by Personnel Error.Surveillance Test Was Performed & Completed Satisfactorily W/No Equipment Deficiencies1997-10-23023 October 1997
- on 970318,inadequate Testing of safety-related Logic Occurred.Caused by Personnel Error.Surveillance Test Was Performed & Completed Satisfactorily W/No Equipment Deficiencies
05000346/LER-1997-012, :on 970904,decay Heat Cooler Seismic Design Inadequacy Occurred.Caused by Inadequate Design of Dhc Support Sys.Dhc Mounting Support Sys Will Be re-evaluated1997-10-0606 October 1997
- on 970904,decay Heat Cooler Seismic Design Inadequacy Occurred.Caused by Inadequate Design of Dhc Support Sys.Dhc Mounting Support Sys Will Be re-evaluated
05000346/LER-1997-011, :on 970825,emergency Ventilation Sys Rendered Inoperable by Maint on Room Isolation Valve Occurred.Caused by Misinterpretation of Tech Spec.Preventive Maint Activities Revised1997-10-0202 October 1997
- on 970825,emergency Ventilation Sys Rendered Inoperable by Maint on Room Isolation Valve Occurred.Caused by Misinterpretation of Tech Spec.Preventive Maint Activities Revised
05000346/LER-1997-002-01, :on 970122,identified Potential Overpressurization of Penetrations During Accident Conditions.Installed Mod to Protect Component Cooling Water Supply from Overpressurization Concerns on 9705041997-08-19019 August 1997
- on 970122,identified Potential Overpressurization of Penetrations During Accident Conditions.Installed Mod to Protect Component Cooling Water Supply from Overpressurization Concerns on 970504
05000346/LER-1997-003, :on 970130,potential Condition Adverse to Quality Rept Was Initiated W/Regard to TS Action for Degraded RCS Flow Rate.Caused Because Actions to Reset Affected RPS Trip Setpoints,Not Developed.Guidance Provided1997-08-19019 August 1997
- on 970130,potential Condition Adverse to Quality Rept Was Initiated W/Regard to TS Action for Degraded RCS Flow Rate.Caused Because Actions to Reset Affected RPS Trip Setpoints,Not Developed.Guidance Provided
05000346/LER-1997-008-01, :on 961113,switchboard Circuit Was Declared Inoperable Due to Switchyard Breaker Alignment.Caused by Misunderstanding of Design.Standing Order Was Issued on 961121 to Provide Guidance for Entering TS1997-07-31031 July 1997
- on 961113,switchboard Circuit Was Declared Inoperable Due to Switchyard Breaker Alignment.Caused by Misunderstanding of Design.Standing Order Was Issued on 961121 to Provide Guidance for Entering TS
05000346/LER-1997-007, :on 970305,determined That Acceptance Criteria of Surveillance Test to Measure Leakage Into Dh Valve Pit Potentially non-conservative.Caused by Human Error. Surveillance Test Revised1997-06-20020 June 1997
- on 970305,determined That Acceptance Criteria of Surveillance Test to Measure Leakage Into Dh Valve Pit Potentially non-conservative.Caused by Human Error. Surveillance Test Revised
05000346/LER-1997-008, :on 970318,inadequate Testing of Safety Related Logic Was Identified.Caused by Personnel Error.Testing Was Performed to Verify Equipment Operability1997-06-16016 June 1997
- on 970318,inadequate Testing of Safety Related Logic Was Identified.Caused by Personnel Error.Testing Was Performed to Verify Equipment Operability
05000346/LER-1997-010, :on 970504,Main Transformer Deluge Sys Automatically Actuated Due to Degraded Temp Sensor in Transformer Fire Detection Sys.Replaced Damaged Main Transformer & Sensors That Actuate Deluge Sys1997-06-0303 June 1997
- on 970504,Main Transformer Deluge Sys Automatically Actuated Due to Degraded Temp Sensor in Transformer Fire Detection Sys.Replaced Damaged Main Transformer & Sensors That Actuate Deluge Sys
05000346/LER-1997-006, :on 970225,both Containment Radiation Monitors Were Found to Be Missing Gaskets on Particulate Filter & Iodine Cartridge Holders.Caused by Lack of Procedural Guidance.Missing Gaskets Were Replaced1997-03-27027 March 1997
- on 970225,both Containment Radiation Monitors Were Found to Be Missing Gaskets on Particulate Filter & Iodine Cartridge Holders.Caused by Lack of Procedural Guidance.Missing Gaskets Were Replaced
05000346/LER-1997-005, :on 970212,failed to Perform Surveillance Requirement of Vacuum Leakage Rate Test.Caused by Inadequate Safety Evaluation.Personnel Entered Containment & Verified Kamlock Cover Was Properly Installed1997-03-14014 March 1997
- on 970212,failed to Perform Surveillance Requirement of Vacuum Leakage Rate Test.Caused by Inadequate Safety Evaluation.Personnel Entered Containment & Verified Kamlock Cover Was Properly Installed
05000346/LER-1997-003, :on 970130,non-conservative TS Action for Degraded Reactor Coolant Flow,Occurred Because Calculations Performed in Support of Amend of DBNPS Did Not Consider Need to Adjust Setpoints.Ts Will Be Revised1997-03-0303 March 1997
- on 970130,non-conservative TS Action for Degraded Reactor Coolant Flow,Occurred Because Calculations Performed in Support of Amend of DBNPS Did Not Consider Need to Adjust Setpoints.Ts Will Be Revised
05000346/LER-1997-004, :on 970203,RCP Motor Oil Piping Was Not Protected from Leakage as Required Per 10CFR50 App R.Caused by Personnel Not Realizing Pressurized Piping in Area. Mods Made to Contain Piping as Necessary1997-03-0303 March 1997
- on 970203,RCP Motor Oil Piping Was Not Protected from Leakage as Required Per 10CFR50 App R.Caused by Personnel Not Realizing Pressurized Piping in Area. Mods Made to Contain Piping as Necessary
05000346/LER-1997-002, :on 970122,identified Potential Overpressurization of Penetrations During Accident Conditions.Plant Mods & Procedure Changes Being Developed to Prevent Overpressurization of Piping1997-02-21021 February 1997
- on 970122,identified Potential Overpressurization of Penetrations During Accident Conditions.Plant Mods & Procedure Changes Being Developed to Prevent Overpressurization of Piping
05000346/LER-1997-001, :on 970122,nuclear Instrumentation Declared Inoperable & Incapable of Performing Safety Functions.Caused by Small Shift in Degraded Bottom Linear Amplifier.Power Range Bottom Linear Amplifier Replaced1997-02-21021 February 1997
- on 970122,nuclear Instrumentation Declared Inoperable & Incapable of Performing Safety Functions.Caused by Small Shift in Degraded Bottom Linear Amplifier.Power Range Bottom Linear Amplifier Replaced
05000346/LER-1996-010, :on 961212,CREV Sys Were Not Realized as Inoperable When Radiation Monitors Were Inoperable.Caused by Misinterpretation of Relationship Between Radiation Monitors & Crevs.Standing Order 96-006 Issued1997-01-13013 January 1997
- on 961212,CREV Sys Were Not Realized as Inoperable When Radiation Monitors Were Inoperable.Caused by Misinterpretation of Relationship Between Radiation Monitors & Crevs.Standing Order 96-006 Issued
05000346/LER-1996-008, :on 961113,switchyard Circuit Declared Inoperable Due to Switchyard Breaker Alignment.Ts 3.8.1.1 Entered & Required Breaker Alignment Checks Were Performed1996-12-13013 December 1996
- on 961113,switchyard Circuit Declared Inoperable Due to Switchyard Breaker Alignment.Ts 3.8.1.1 Entered & Required Breaker Alignment Checks Were Performed
05000346/LER-1996-009, :on 961113,failure to Apply Generic Ltr 91-18 Guidance to Emergency Diesel Generator Surveillance Testing Noted.Caused by Lack of Design or Licensing Basis Documentation.Edgs Are Being Revised1996-12-13013 December 1996
- on 961113,failure to Apply Generic Ltr 91-18 Guidance to Emergency Diesel Generator Surveillance Testing Noted.Caused by Lack of Design or Licensing Basis Documentation.Edgs Are Being Revised
05000346/LER-1996-007, :on 961003,CR Emergency Ventilation Sys Design Bases Calculation Error Occurred.Caused by Error in Bechtel Calculation 26.003,CR Pressurization Sys.Cr Boundary Openings Were Verified1996-11-0404 November 1996
- on 961003,CR Emergency Ventilation Sys Design Bases Calculation Error Occurred.Caused by Error in Bechtel Calculation 26.003,CR Pressurization Sys.Cr Boundary Openings Were Verified
05000346/LER-1996-006, :on 960614,discovered High Lip Around Top of Reactor Coolant Pump Motor 2-1 Not in Place.Caused by Inadequate Work Planning.Reactor Coolant Pump Motor Replaced1996-06-13013 June 1996
- on 960614,discovered High Lip Around Top of Reactor Coolant Pump Motor 2-1 Not in Place.Caused by Inadequate Work Planning.Reactor Coolant Pump Motor Replaced
05000346/LER-1996-004, :on 960417,PCAQR 96-0512 Document Failure to Initiate Required Compensatory Actions for Thermo-Lag for Radiant Energy Shields.Caused by Personnel Error.Util Plans to Replace Thermo-Lag1996-05-17017 May 1996
- on 960417,PCAQR 96-0512 Document Failure to Initiate Required Compensatory Actions for Thermo-Lag for Radiant Energy Shields.Caused by Personnel Error.Util Plans to Replace Thermo-Lag
05000346/LER-1996-003, :on 960328,discovered Discrepancy in SRs for Testing of Absorbent Matl in Evs.Caused by Deficiencies in Testing of nuclear-grade Activated Charcoal.Submitted Emergency Amend Request to Revise SRs1996-04-29029 April 1996
- on 960328,discovered Discrepancy in SRs for Testing of Absorbent Matl in Evs.Caused by Deficiencies in Testing of nuclear-grade Activated Charcoal.Submitted Emergency Amend Request to Revise SRs
05000346/LER-1996-002, :on 960320,noted Potential for Loss of Remote Shutdown Capability.Caused by Fire Induced Hot Short Which Could Bypass Valve Protection Features.Implemented Hourly Roving Fire Watches & Completed Evaluations1996-04-19019 April 1996
- on 960320,noted Potential for Loss of Remote Shutdown Capability.Caused by Fire Induced Hot Short Which Could Bypass Valve Protection Features.Implemented Hourly Roving Fire Watches & Completed Evaluations
05000346/LER-1996-001, :on 960304,EECS Inoperable.Caused by Inadequate Safety Review.Plant Mod to Install Manual Vent Valve Will Be Implemented in Tenth Refueling Outage1996-04-0303 April 1996
- on 960304,EECS Inoperable.Caused by Inadequate Safety Review.Plant Mod to Install Manual Vent Valve Will Be Implemented in Tenth Refueling Outage
05000346/LER-1995-003, :on 951117,determined That Removal of Fan C48 from Auxiliary Bldg Radwaste Ventilation Sys on 951006 Inadvertently Rendered Both Trains of SFP Evs Inoperable. Reinstalled Fan C48 on 951118.W/9512181995-12-18018 December 1995
- on 951117,determined That Removal of Fan C48 from Auxiliary Bldg Radwaste Ventilation Sys on 951006 Inadvertently Rendered Both Trains of SFP Evs Inoperable. Reinstalled Fan C48 on 951118.W/951218
05000346/LER-1995-002, :on 950906,discovered Six Post Nuts Missing from Terminal Strip in Cabinet C3629.Caused by Isolated Wiring Error.Terminal Post Nuts Installed on Terminal Strip in Cabinet C36291995-10-0606 October 1995
- on 950906,discovered Six Post Nuts Missing from Terminal Strip in Cabinet C3629.Caused by Isolated Wiring Error.Terminal Post Nuts Installed on Terminal Strip in Cabinet C3629
05000346/LER-1995-001, :on 950126,determined That LOCA Analysis Results for 2 Ft Core Elevation Potentially non-conservative Due to Modeling Errors.Vendor Evaluated Current Fuel Cycle to Determine If Operating Limits Valid1995-02-24024 February 1995
- on 950126,determined That LOCA Analysis Results for 2 Ft Core Elevation Potentially non-conservative Due to Modeling Errors.Vendor Evaluated Current Fuel Cycle to Determine If Operating Limits Valid