ML19269C710
| ML19269C710 | |
| Person / Time | |
|---|---|
| Site: | Point Beach |
| Issue date: | 02/02/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Burstein S WISCONSIN ELECTRIC POWER CO. |
| Shared Package | |
| ML19269C711 | List: |
| References | |
| NUDOCS 7902120110 | |
| Download: ML19269C710 (1) | |
Text
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Docket No. 50-266 Docket No. 50-301 02 OD Wisconsin Electric Power Company ATTN:
Mr. Sol Burstein Senior Executive Vice President Power Plants 231 West Michigan Milwaukee, WI 53201 Centlemen:
This Information Notice is provided as an early notificationIt is expected of a possibly significant matter.
i will review the information for possible applicability to the r this No specific action or response is requested at If further NRC evaluations so indicate, an IE Circular facilities.
or Bulletin will be issued to recommend or request specific time.
If you have questions regarding this matter, licensee actions.the Director of the appropriate NRC Regional please contact office.
Sincerely, SY James G. Ke p er Director
Enclosures:
1.
IE Information Notice No. 79-01 2.
List of IE Information Notices Issued in 1979 cc w/encls:
Mr. G. A. Reed, Plant Manager Central Files Director, NRR/DPM Director, NRR/ DOR PDR Local PDR JSIC tie Sandra A. Bast, Lakeshore Citizens for Safe Energy "i802120ll0
U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT REGION III February 2,1979 IE Information Notice No. 79-01 BERGEN-PATERSON HYDRAULIC SHOCK AND SWAY ARRESTCRS (HSSA)
On December 4, 1978, Rancho Seco Nuclear Generating Station reported the failure of seven Bergen-Paterson HSSA (Snubber) units to lockup in the compression direction and the failure of one additional unit to lockup in the extension direction. These failures were identified during surveillance testing and the affected models included HSSA-3-6, HSSA-10-6 and HSSA-20-6. When the units were disassembled, the licensee observed damage to the poppet valve and seat on the compression side of the valve blocks of the seven units that failed in the compression direction.
It was also observed that five of the seven units had the The licensee poppet spring entrapped between the poppet and the scat.
attributed the seven failures in the compression direction to abusive handling during compression of the units for installation folloeing testing at the previous refueling outage. The cause of the single failure in the extension direction has not been determined. In addition to exercising greater care in reinstallation, the licensee co=mitted to functionally test all Bergen-Paterson snubbers subjected to transient conditions which cause either physical damage to or significant movement of piping. This testing will include verification of piston movement, lockup and bleed. The Bergen-Paterson Technical Maintenance Manual reco= mends that additional inspections should be made on units which may*have participated in an unusual shock occurrence involving known damage to.' piping or equipment.
On January 3, 1079, the licensee reported that the decay heat removal system had been subjected to a transient condition in the form of a
" water hammer." This transient, caused pipe movement great enough to damage two rigid pipe support wall attachmer.ts. The subsequent functional testing of the affected Bergen-Paterson units revealed that one of seven units failed the lockup test. This unit (Model No. HSSA-3-6) was disassembled and damage to the poppet valve and seat was observed.
The damage to the poppet valves is presently being reviewed by both the licensee and Bergen-Paterson. At this time, the cause of damage has not been completely defined nor has appropriate corrective action been determined. Other licensees have reported instances of poppet valve damage; however, the cause and extent of damage are not known at this time.
OdfW 7902120059
IE Information Notice No. 79-01 February 2, 1979 This information is provided as an early notification of a possibly It is expected that recipients will review the significant matter.
No specific information for possible applicability to their facilities.
If further NRC evaluations action or response is requested at this time.
so indicate, an IE Circular or Bulletin will be issued to recommend or.
request specific licensee actions. Il you have questions regarding this matter, please contact the Director of the appropriate NRC Regional Office.
Page 2 of 2
IE Information Notice No. 79-01 February 2, 1979 LISTING OF IE INFORMATION NOTICES ISSUED IN 1979 Information Subject Date Issued To Issued Notice No.
An Information Notice is a new method of communicating items of potential interest to licensees. This item, Information Notice No. 79-01, is the first of this new form of communication.
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