05000368/LER-1979-009-03, /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed

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/03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed
ML19263C288
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/09/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19263C280 List:
References
LER-79-009-03L, LER-79-9-3L, NUDOCS 7902130196
Download: ML19263C288 (1)


LER-1979-009, /03L-0 on 790121:during Power Escalation Testing, Reactor Protection Sys Channel C Trip Path Solid State Relay Failed,Opening Reactor Trip Path Circuit Breakers 3 & 7.Relay Was Replaced;Within 4-h Circuit Breakers Closed
Event date:
Report date:
3681979009R03 - NRC Website

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LICENSEE EVENT REPORT EXHIBIT A CONTROL BLOCK {l l l l l lh (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATIONI I

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s 79 M SOH1 CATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h i During Power Escalation Te.7, ting, Mode 1 operation, channel "C" RPS trip p oi2 ia i path solid state relav failed, openina reactor trip path circuit j

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i m i Recuirements of Action Staterent T.S. Table 3.3-1 fi4 were met.

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