ML19263C283

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LER 79-007/03L-0 on 790113:during Power Escalation Test, Control Element Assembly Position as Received by Core Protection Computer B Was Incorrect.Caused by Bad Multiplexer Card,Which Was Replaced
ML19263C283
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 02/09/1979
From: Shively C
ARKANSAS POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19263C280 List:
References
LER-79-007-03L, LER-79-7-3L, NUDOCS 7902130188
Download: ML19263C283 (1)


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DOCL E T sVMc E R Gd is .' EvtNT DATE 24 75 HFPOH1 0 ATE 80 EVENT DESCRIPTION AND PROBAGLE CONSEQUENCES h 92 Lywrinct the performance of Power Escalation Test TP2.800.01 j ia l Appendix Q, CPC/COLSS Verification, it was noted that the ,

i,i4 , l CEA position as rectived by CPC "B" was incorrect. _

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Lwan declared inoperable and remained in bypass following the; in I completion of Anoendix Q. There have been no similar ,

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4I C AUSE DESCR. TION AND CORREC rlVE ACTIONS ??

. iaIi Tnvestigation revealed a bad multiplexer card, which was  ;

i- I reolaced. CPC "B" was satisfactorily tested and declared ,

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