ML19263B619

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Forwards IE Circular 79-02,Failure of 120 Volt Vital AC Power Supplies
ML19263B619
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 01/16/1979
From: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Parker W
DUKE POWER CO.
References
NUDOCS 7901220215
Download: ML19263B619 (2)


Text

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1FRA en R800 UNITED STATES 9

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  1. o, NUCLEAR REGULATORY COMMISSION f

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t 101 M ARIETTA ETREET, N.W.

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ATLANTA, GEOGGIA 30303 o

JAN 161979 In Reply Refer To:

RII:JPO 50-369, 50-370 50-269, 50-270 50-287 Duke Power Company Attn:

Mr. William O. Parker, Jr.

Vice President, Steam Production P. O. Box 2178 422 South Church Street Charlotte, North Carolina 28242 Gentlemen:

The enclosed Circular 79-02 is forwarded to you for inforcation.

If there are any questions related to your understanding of the suggested actions, please contact this office.

Sincerely, b

un ces P. O'Reilly D rector

Enclosures:

1.

IE Circular 79-02 2.

List of IE Curculars Issued in the last 12 months e

790122,o;;u5

JAN 161979

, Duke Power Company cc w/ encl:

J. C. Rogers, Project Manager McGuire Nuclear Station P. O. Box 2178 Charlotte, North Carolina 28242 M. D. McIntosh, Plant Manager McGuire Nuclear Station P. O. Box 488 Cornelius, North Carolina 28031 J. E. Smith, Station Manager Oconee Nuclear Station P. O. Box 1175 Seneca, South Carolina 29678 h

UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.

20555 January 16, 1979 IE Circular No. 79-02 FAILURE OF 120 VOLT VITAL AC POWER SUPPLIES Description of Circumstances:

On September 16, 1978, Arkansas Nuclear One - Unit 2, while in hot functional testing preceding initial criticality, suffered a degrada-tion of both of the independent off-site power sources. This produced an undervoltage condition on the Engineering Safety Features (ESF) Buses and caused an inadvertent ESF actuation.

The licensee determined that the ESF actuation occurred on a loss of at least two of the uninter-ruptable 120 volt vital AC power sources.

Irrediate investigation revealed that all four of the Solidstate Controls, Inc., (SCI) inverter static switches had automatically transferred to the alternate power supply (the 120 volt AC being supplied by transformers directly off the ESF buses rather than from the inverter output.)

Figure 1 (attached) shows the functional interconnection of the 120 volt AC power supply system.

A single cenclusive cause of the undesired SCI inverter static switch transfer could not be identified. However, the following problems were discovered during subsequent investigation.

(a)

The SCI inverters have circuitry to monitot the incoming DC voltage level which, on sensing a low voltage (nominally 104 DC volts for these inverters) will trip both input breakers to the inverter component after an adjustable time delay.

The setting of these time delay relays were not verified during either preoperational testing or subsequent maintenance. The time delay is necessary in order to accommodate transient loading conditions which may be encountered.

(b) On one SCI inverter, a DC fuse within the inverter component was found blown, The vendor indicated that this fuse will blow due to an excessive DC voltage to the inverter component caused by a

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the taps on the 4 limit the DC volt maximum rating in DUPLICATE DOCUMENT Entire document previously entered into system under:

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