05000324/LER-1979-097-03, /03L-0:on 791217,during Normal Plant Operation, torus-to-drywell Vacuum Breaker CAC-X18E Had No Closed Indication.Caused by Valve Flapper Not Completely Closing. Replaced Permanent Magnet Holding Flapper Closed

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/03L-0:on 791217,during Normal Plant Operation, torus-to-drywell Vacuum Breaker CAC-X18E Had No Closed Indication.Caused by Valve Flapper Not Completely Closing. Replaced Permanent Magnet Holding Flapper Closed
ML19262C009
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 01/15/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262C007 List:
References
LER-79-097-03L-01, LER-79-97-3L-1, NUDOCS 8001220419
Download: ML19262C009 (1)


LER-1979-097, /03L-0:on 791217,during Normal Plant Operation, torus-to-drywell Vacuum Breaker CAC-X18E Had No Closed Indication.Caused by Valve Flapper Not Completely Closing. Replaced Permanent Magnet Holding Flapper Closed
Event date:
Report date:
3241979097R03 - NRC Website

text

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8 60 61 DOCKET NUMSER 6d' 69 EV E%T DATE 74

?S REPORT CATE 80 EVENT DESCRIPTION AND PRO 8ABLE CONSEQUENCES h o 2 l During normal plant operation, the control operator noticed that the torus to I

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