ML19262A727
| ML19262A727 | |
| Person / Time | |
|---|---|
| Site: | Zimmer |
| Issue date: | 11/26/1979 |
| From: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | Borgmann E CINCINNATI GAS & ELECTRIC CO. |
| References | |
| NUDOCS 7912100423 | |
| Download: ML19262A727 (1) | |
Text
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'n NUCLEAR REGULATORY CONMISSION REGION lli o,.
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799 ROOSEVELT ROAD NW d'
GLE N E LLYN. ILLINOls 60137 Docket No. 50-358 Cincinnati Gas and Electric Company ATTN:
Mr. Earl A. Borgmann Senior Vice President Engineering Services and Electric Production 139 East 4th Street Cincinnati, OH 45201 Gentlemen:
The enclosed IE Circular No. 79-24 is forwarded to you for information.
No written response is required.
Should you have any questions related to your understanding of the recommendations on this matter, please contact this office.
Sincerely,
. %. h d i,f dL JamesG.Keppker Director
Enclosures:
1.
IE Circular No. 79-24 2.
Recently Issued IE Circulars cc w/encls:
Mr. J. R. Schott, Plant Superintendent Central Files Director, h3R/DPM Director, NRR/ DOR PDR Local PDR NSIC TIC Harold W. Kohn, Power Siting Commission Citizens Against a Radioactive Environment Helen W. Evans, State of Ohio 1523
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d9 7912100
Accession No: 7910250492 SSINS No. 6830 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C.
20555 November 26, 1979 IE Circular No. 79-24 PROPER INSTALLATION AND CALIBRATION OF CORE SPRAY PIPE BREAK DETECTION EQUIPMENT ON BWRs Descrip:. ion of Circumstances:
During 1976 the Iowa Electric Light and Power Company identified and corrected a potential problem involving the core spray (CS) pipe break detection system at the Duane Arnold Energy Center (DAEC). The problem relates to the setpoint, function, and installation of the differential pressure (dp) instrument which monitors for a CS pipe break that is located in the annulus area of the reactor vessel (i.e., located outside the core shroud but inside the reactor vessel).
The installed instrument, range of 0 - 24 psid, was found deflecting downscale (i.e., reading negative psid) during operation.
The licensee's investigation of the downscale deflection revealed that the original piping arrangement and calibration did not adequately take into account the effect of density changes of the water in the pressure leg connection The original installation had the high pressure side of the dp instrument (see attached Figure 1) connected to the reference leg in the vessel (Figure 1 Connection X) and the low pressure side to the core spray piping outside the vessel but inside the drywell (Figure 1 Connection Y). With the piping intact, this arrangement senses the ptessure difference between bottom and top of core. With a break in CS piping in the annulus area the instrument then senses the additional pressure drop across the separators (dp q 7 psi additional) and dryers (dp q 7-inches water).
This installation was in accordance with GE desigr requirements.
Also in accordance with GE instructions the calibration of the dp instrument was performed with the reactor in the cold a ndition and the alarm was set to trip at 5 psid increasing.
Because of this cold calibration the dp instrument then indicated full downscale negative during operation.
This negative dp was due to the heat up of the reference leg (Figure 1 Connection X) which caused the flui density to decrease as the plant reached hot conditions.
The magnitude of this c was determined to be about 3.5 psid following completion of the modification discussed below.
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