05000324/LER-1979-034-03, /03L-0 on 790510:while Performing PT 20.3,primary Containment Isolation Valve Local Leak Rate Test Containment Isolation Valves Would Not Seat & Hold Pressure.Caused by Valve Bushing Wear.Valves Dissassembled & Bushings Repl

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/03L-0 on 790510:while Performing PT 20.3,primary Containment Isolation Valve Local Leak Rate Test Containment Isolation Valves Would Not Seat & Hold Pressure.Caused by Valve Bushing Wear.Valves Dissassembled & Bushings Replaced
ML19259C127
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 06/08/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19259C123 List:
References
LER-79-034-03L-01, LER-79-34-3L-1, NUDOCS 7906120388
Download: ML19259C127 (1)


LER-1979-034, /03L-0 on 790510:while Performing PT 20.3,primary Containment Isolation Valve Local Leak Rate Test Containment Isolation Valves Would Not Seat & Hold Pressure.Caused by Valve Bushing Wear.Valves Dissassembled & Bushings Replaced
Event date:
Report date:
3241979034R03 - NRC Website

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8 t,U 61 DOCK E T " 'WE E R 68 fa EVENT DATE n1 HEPORT DATE 80 EVENT DESCRIPTION AND PROBABL E CMSEQUENCES h o 2 l While performing normal operator surveillance on the control. panel. it was nOted thatI

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the drywell equipment drain recorder was drivinn downscale,_an_d the integrator was o

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40 41 ty 43 44 47 CAUSE DESCRIPTION AND CORREC if VE AC T!ONS h l The recorder motor drive amplifier transistor failed, and the flow transmitter elec,_j li o

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l trical zero shifted from 10.0 ma to 9.4 ma.

The transistor _was replaced, the flow I

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The system was returned

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Thi', is considered an isolated incident.

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8 80 LOSS OF 09 DAMAGE TO F ACILITY TYPE D E SC RIP TION 7QQQlQQ W@l NA i

9 8 9 10 80 155UEt DESCRIP TION 8 9 to r, R r> 9 80 ;;

A. C. Tollison, Jr.

919-457-6701

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