05000250/LER-1979-001-31, /031-0 on 790213:A Fire Pump Found to Be Inoperable.Caused by Improper Operation of Power Supply Breaker.Procedural Methods Implemented to Ensure That Fire Pump Power Is Verified After Each Shift

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/031-0 on 790213:A Fire Pump Found to Be Inoperable.Caused by Improper Operation of Power Supply Breaker.Procedural Methods Implemented to Ensure That Fire Pump Power Is Verified After Each Shift
ML19259B787
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 03/13/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19259B786 List:
References
LER-79-001-031-02, LER-79-1-31-2, NUDOCS 7903230160
Download: ML19259B787 (1)


LER-1979-001, /031-0 on 790213:A Fire Pump Found to Be Inoperable.Caused by Improper Operation of Power Supply Breaker.Procedural Methods Implemented to Ensure That Fire Pump Power Is Verified After Each Shift
Event date:
Report date:
2501979001R31 - NRC Website

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