05000324/LER-1979-092-03, /03L-1:on 791214,after Performing OD-1,found Fuel Bundles 9-26 & 43-28 Exceeded Linear Generation Rate.Caused by Approaching Limit with One Transient in-core Probe Not Available.Power Increases to Be Halted at 5%

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/03L-1:on 791214,after Performing OD-1,found Fuel Bundles 9-26 & 43-28 Exceeded Linear Generation Rate.Caused by Approaching Limit with One Transient in-core Probe Not Available.Power Increases to Be Halted at 5%
ML19257D483
Person / Time
Site: Brunswick 
Issue date: 01/28/1980
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19257D480 List:
References
LER-79-092-03L, LER-79-92-3L, NUDOCS 8002040463
Download: ML19257D483 (2)


LER-1979-092, /03L-1:on 791214,after Performing OD-1,found Fuel Bundles 9-26 & 43-28 Exceeded Linear Generation Rate.Caused by Approaching Limit with One Transient in-core Probe Not Available.Power Increases to Be Halted at 5%
Event date:
Report date:
3241979092R03 - NRC Website

text

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