ML19257C048

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Interim Deficiency Rept on Use of Invalid Seismic Amplified Response Spectra.Caused by Incorrect Analysis of Safety Class 2 & 3 Piping sys.Short-term Audit of Selected Seismic Category 1 Sys & Components Conducted
ML19257C048
Person / Time
Site: Seabrook  NextEra Energy icon.png
Issue date: 12/06/1979
From:
PUBLIC SERVICE CO. OF NEW HAMPSHIRE
To:
Shared Package
ML19257C046 List:
References
NUDOCS 8001240027
Download: ML19257C048 (9)


Text

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Public Service Company of New Hampshire Seabrook Station a.

Interim Report on .

Use of Invalid Seismic Amplified Response Spectra Date: December 6, 1979 1797 050 3001240 0 2_

Seabrook Project Interim Report on Use of Invalid Seismic Amolified Response Spectra

. Introduction On Tuesday, November 6,1979, Mr. J. DeVincentis, Seabrook Project Manager for Yankee Atomic Electric Company, reported by telephone to Mr. J. Mattia, NRC Region I Inspection and Enforcement inspector for the Seabrook Project, two significant design deficiencies under 10 CFR50.55(e). YAEC had that same day received written notice of the two deficiencies from the Seabrook architect-engineer-construction manager, United Engineers & Constructors Inc., under UE&C letter numbers SBU-31426 and SBU-31428.

The purpose of this_ report is to provide interim infor=ation on one of those reported deficiencies; namely, that identified in SBU-31426 (see Attachment 1) involving the use of incorrect seismic amplified response spectra (ARS) in the design of components supported by the centainment building annular steel frame.

Structural Description of Containment Buildine For plans and elevation arrangements of the Scabrook containment building internals, refer to Seabrook PSAR Figures 1.2-2 through 1.2-6.

The following i's a brief description of the Seabrook containment building and its internal structures:

1797 051

Structural Descriotion of Containment Building (Cont'd)

'The Containment Shell is a reinforced concrete cylinder with an hemi-spherical dome., both lined with carbon steel plate. The containment con-crete internals consist of the primary and secondary shield walls, support-ing columns for the gantry crane, the refueling canal and floor slabs at elevations 25 ft. and 0 ft. The Containment Shell and Internals are connected to the foundation mat which is founded on rock. The working floor slab at the bottom of the containment is at El. (-) 26'.

The structural steel frame involved in this design deficiency is the annular steel frame located inside the containment building in the annular space between the containment secondary shield wall and the containment outer shell. .

The annular steel frame consists of steel columns and platform fram-ings at elevations 25 ft. and 0 ft. It also has framings at various lower elevations which are essentially utilized for pipe supports. Several radial beams of the annular steel framing are rigidly connected to the containment secondary shield wall.

Design Deficiency In late September 1979, a UE&C employee assigned to perform the seismic response analysis of Safety Class 2 and 3 piping in the containment building (including piping running in the annulus, supported by the structural steel framing) was reviewing the file of Seabrook Amplified Response Spectra (ARS) for the proper input to his particular analysis. He came upon the document i797 052

Design Deficieaev (Cont'd) entitled " Seismic Analysis of the Annular Steel", with the unique identi-fication number SBSAG-14CS, dated October 7, 1977. In reviewing the

- contents of this document,* the analyst determined that certain of the ARS for portiods of the annular . structural steel in that document had consid-erably higher "g" values that those used as input to previous analyses of Safety Class 2 and 3 piping supported by the same annular structural steel.

Further investigation revealed that the seismic analyses of Safety Class 2 and 3 lines in the same area performed to that time used as input ARS extracted from a document entitled " Seismic Analysis of Containmenc Structure", with the unique identification number SBSAG-4CS4, dated 3/19/76.

This document presented the ARS for the reinforced concrete containment outer shell and the interior concrete structures including the secondary shield walls. The ARS values contained in this document are, in general, lower than the previously mentioned documsnt since, by their nature, concrete structures in general are stiffer than structural steel structures.

The Lesediate design deficiency was, therefore, that Safety Class 2 and 3 piping systems were' seismically analyzed using inc)rrect, low values of ARS. The possibility exists, therefore, that had this oeficiency not been revealed, one or more of the piping systems in question would be over-stressed under maximum seismic and operating loadings.

Corrective Action

1. UE&C is conducting a short-term audit of selected seismic Category I systems and components to assure use of correct Amplified Response Spectra in their seismic design.

.1797 053

Corrective Action (Cont'd) .

2. Containment building annular steel frame is being redesigned to increase its rigidity. The intent is to reduce the values of the ARS imposed on the piping systems and other components supported by the annular steel frame.
3. A " HOLD" has been placed on the design and analysis of piping systems located in the containment annulus.
4. UE&C will conduct a longer term audit of all seismic Category I aystems and components to assure use of correct ARS in their seismic design.
5. When the redesign of the annular steel framing is complete, a seismic analysis of it will be perfor=ed, generating new ARS at significant individual points.
6. Existing analyses of Safety Class 2 and 3 piping running in the containment annulus will be reviewed against ARS generated in
  1. 5 above. Where necessary, piping will be reanalyzed to assure confor=ance with cpplicable Code and regulatory requirements.
7. UE&C is currently reviewing the seismic design requirements of all other components supported by the containment annular steel frame. They are the following:
a. Containment Recirculating Air Units:

These would be used for post-LOCA hydrogen mixing and are Safety Class 3.

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, Corrective Action (Cont'd)

'b. Containment Cooling Units:

These are non-sdfety-related, non-seismic Category I. However, they will be seismically designed since they are located in a

' seismic Category I building.

c. Hydrogen Recombiners:

There are two thermal-type recombiners mounted on the annular steel frame. They are safety Class 3, seismic Category I.

d. Cable Trays and their Support Systems:

Tray supports are seismic Category I.

e. Heating, ventilating and Air Conditioning Ductwork Systems:

These are a mixture of Category I and non-Category I systems.

f. Air Compressors: ,

Two small non-Category I units for instru=entation and control supply.

8. Existing UE&C procedures involving seismic design, especially those treating Amplified Response Spectra, are under review to determine the need for revisions or additions which will upgrade ther in areas s

of selection, use and review of ARS.

9. Quality Assurance training sessions, in addition to those on the regular schedule, are planned on the subject of ARS treatment for all UE&C personnel who interface with ARS.

i797 0J55

Construction Status The Seabrook containment building, Unit 1, structural mat and fill mat have been poured. he cylindrical shell liner plate has been erected to El. 119'-0". Internal concrete, including pr* mary and secondary shield walls, are in various degrees of forming, reinforcing bar installation and concrete pouring to approximately Elevation O'.

The containnent annular steel has not been released for fabrication.

It is anticipated that the aforementioned annular steel redesign work and its seismic analysis will be complete in a timely manner so that the prefab-ricated steel can be deliverad and erected in accordance with the present construction schedule - July 1980.

The piping systems analyzed using incorrect ARS have been released for fabrication. Engineering experience and judgement predict that on reanalysis, the geometry and wall thicknesses of these systems will not change; perhaps only the number and location of seismic supports. In any case, geometry of prefabricated piping could be modified in the field. Pipe and other component erection in the 2ontain=ent annulus is scheduled to commence approximately July 1,1980, and to continue for t. period of about two years.

Final Report The final report on this subject, including a discussion of any safety implications, and the resulte of the corrective actions enumerated above, will be complete and issued by June 1,19'80.

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g mited engineers ace,-

30 South 17th Street mmM ECHELON moxwag Post Office Box 8223 PHILACELPHIA Philadelphia, PA 19101 VIA TELECOPIER November 6, 1979 SBU-31426 File: 3.1.6

, Catg: NRCD No Response Required Mr. John DeVincentis, Project Manager Yankee Atomic Electric Company Seabrook Station 20 Turnpike Road Westborough, Massachusetts 01581

Dear Mr. DeVincentis:

Public Service Company of New Hampshire Seabrook Station Discrepancy in the Seismic Design in the Containment Annular Area The purpose of this letter is to advise you of a design discrepancy in the amplified re;ponse spectra used in the seismic design of safecy related components supported by the containment annular steel frame.

It was recently discovered that the analyses being done for compo-nents supported by the containment annular steel frame were based on incorrect seismic amplified response spectra. The amplified rasponse spectra used for this design was that for the containment interior con-crete and not the annular steel frame which should have been used.

An evaluation has shown that the amplified- response spectra for die annular steel frame has "g" values greater than that used in the compo- ,

nent design. Some of the peak values are such that it is unlikely a satisfactory component design could be achieved.

Action is currently underway to redesign the containment annular steel frame by providing additional bracing in order to reduce the "g" -

values. The design of all components located in this area will then be checked against the redesigned containment annular steel frame and its resulting amplified response spectra.

The containment steel annular frame has not yet been released for fabrication and will be held until the additional bracing is designed.

The manufacture of a number of components in this area has been released, but it is not intended to place a hold on these items since it is believed that a satisfactory design can be achieved without significant changes to the components.

-,)

1797 057 A Raytheon Company .

e s .'

Mr. John DeVincentis Povember 6, 1979 Project Manager -

,8U-31426 -

~

In order to ensure that other discrepancies do not exist in the seismic design, an audit will be performed to ensure that the proper amp.'.ified response spectra was used in the design of all items on the Seab ook project.

We will keep you advised of our progress in resolving this problem and completing the audit of the other items.

It is our belief that this design discrepancy' is a reportable item in accordance with 10 CFR 50.55(e) and it is, therefore, recommended that it be reported to the Nuclear Regulatory Commission.

. Very truly yours,

,1

) c' ~~.

O

  • G. F. Cole Project Manager GFC:hr-cc: Messrs. John DeVincentis - YAEC - 4L -

B. B. Beckley - PSNH - 3L J. D. Haseltine - PSNH - 1L T. M. Sherry - YAEC - IL J. H. Herrin - PENE - YAEC Field Office - IL ,

([) 1797 058

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