ML19256F381
| ML19256F381 | |
| Person / Time | |
|---|---|
| Site: | Comanche Peak |
| Issue date: | 11/26/1979 |
| From: | Seyfrit K NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | Gary R TEXAS UTILITIES ELECTRIC CO. (TU ELECTRIC) |
| References | |
| NUDOCS 7912190056 | |
| Download: ML19256F381 (1) | |
Text
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November 26, 1979 In Reply Refer To:
RIV Docket Nos.
50-445/IE Circular No. 79-24 50-446/IE Circular No. 79-24 Texas Utilities Generating Company ATTN:
Mr. R. J. Gary, Executive Vice President and General Manager 2001 Bryan Tower Dallas, Texas 75201 Gentlemen:
The enclosed IE Circular No. 79-24 is forwarded to you for information. No written response is required.
Should you have any questions related to your understanding of the recommendations on this matter, please contact this office.
Sincerely,
[. "
- Kar V. Scy rit f
Director
Enclosures:
1.
IE Circular No. 79-24 2.
List of Recently Issued IE Circulars 1857 254
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Accession No: 7910250492 SSINS No. 6830 UNITED STATES NUCLEAR REGULATORY CO)Df!SSION OFFICE OF INSPECTION AND PiFORCEMENT WASilINGTON, D.C.
20555 IE Circular No. 79-24 Date: November 26, 1979 Page 1 of 3 PROPER INSTALLATION AND CALIBRATION OF CORE SPRAY PIPE BREAK DETECTION EQUIPMENT ON BWRs Description of Circumstances:
During 1976 the Iowa Electric Light and Power Company identified and corrected a potential prcblem involving the Core Spray (CS) pipe break detection system at the Duane Arnold Energy Center (DAEC). The problem relates to the setpoint, function, and installation of the differential pressure (dp) instrument which monitors for a CS pipe break that is located in the annulus area of the reactor vessel (i.e., located outside the core shroud but inside the reactor vessel).
The installed instrument, range of 0 - 24 psid, was found deflecting downscale (i.e., reading negative psid) during operation.
The licensee's investigation of the downscale deflection revealed that the original piping arrangement and calibration did not adequately take into account the ef fect of density changes of the water in the pressure leg connections.
The original installation had the high pressure side of the dp instrument (see attached Figure 1) connected to the reference leg in the vessel (Figure 1 Connection X) and the low pressure side to the core spray piping outside the vessel but inside the drywell (Figure 1 Connection Y).
With the piping intact, this arrangement senses the pressure difference between bottom and top of core. With a break in CS piping in the annulus area the instrument then senses the additional pressure drop across the separators (dp % 7 psi additional) and dryers (dp % 7 inches water).
This installation was in accordance with CE design requirements.
Also in accordance with CE instructions the calibration of the dp instrument was performed with the reactor in the cold condition and the alarm was set to trip at 5 psid increasing.
Because of this cold calibration the dp instrument then indicated full downscale negative during operation.
This negative dp was due to the heat up of the reference leg (Figure 1 Connection X) which caused the fluid density to decrease as the plant reach M is_d was determined to be about 3.5 psid fo discussed below.
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