05000324/LER-1979-082-03, /03L-0:on 791019,during Hcpi Flow Test,High/Low Alarm Malfunctioned.Caused by Annunciator Card W/Incorrect Logic Configuration.Annunciator Card Replaced.Controls Being Developed

From kanterella
(Redirected from ML19256F116)
Jump to navigation Jump to search
/03L-0:on 791019,during Hcpi Flow Test,High/Low Alarm Malfunctioned.Caused by Annunciator Card W/Incorrect Logic Configuration.Annunciator Card Replaced.Controls Being Developed
ML19256F116
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 11/16/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19256F111 List:
References
LER-79-082-03L-01, LER-79-82-3L-1, NUDOCS 7911210444
Download: ML19256F116 (2)


LER-1979-082, /03L-0:on 791019,during Hcpi Flow Test,High/Low Alarm Malfunctioned.Caused by Annunciator Card W/Incorrect Logic Configuration.Annunciator Card Replaced.Controls Being Developed
Event date:
Report date:
3241979082R03 - NRC Website

text

' "

LICENSEE EVENT REPORT g

CC C

w J

CONTROL BLOCK:

l l

l l

l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

foTl I Nl Cl Bl El Pl 2l@l0 l0 l-l0 l0 l0 l0 10 l-l0 l0 l@{4 l1 l1 l1 l1 l@l l

l@

7 8 9 LICENSEE CODE 14

S LICENSE NUMBER 2$

26 L8 CENSE TYPE JO bi G T 58 CON'T lL gl 0l 5l 0l -l 0l 3l 2 l 4 @l 1l 0l 1l 9l 7 l 9 @

l l

l l

l l@

REPoR o

i 3a nC i

8 60 61 DOCKET NUM8ER hd 69 EVENT D ATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lWhile performing PT 9.5, HPCI Full Flow Test, torus level increased to >-27 inches.

g o

2 l The high/ low alarm did not actuate and the problem was not noted until the high-high g

o 3

l alarm annunciated.

l o

4 I

o s

I o 16 I l Technical Specifications 3.6.2.1, 6.9.1.9.b g

O 7

l l

l o

a l

80 7

8 9 l Sl Alg ]g l C lQ l Z l Z l Z l Z lZ l Z lQ l SOD'Eg g

CE CODE SUSCO E COMPONENT CODE SUS SU E

o 9

7 8

9 to 11 12 13 18 19 20 SEQUENTIAL CCCURRENCE REPORT REVISION EVENT YE AR R EPORT NO.

CODE TYPE O.

@ lLER F97 l9 I l-l IO a 2l l-l 10 l3 lLl l_]

l l

ygt 21 22 23 24 26 27 3

a 30 31 32 7 K N AC ON ON PL NT M

HOURS 27 S8 1 FOR B.

SU PLIE MANY A Y "lE Z

I x l@l x l@

lZI@

W@

l01010l l

W@

lYl@

I Zi@

I I

l l

33 J4 75 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS'@

l The HPCI turbine was immediately secured and the torus pumped to the normal operating ;

i o

W l band. The HPCI minimum flow valve F012 was found partially open and the annunciator g LLL;j l card for the high/ low alarm was found to have an annunciator card with the incorrect gl logic configuration, which resulted in an alarm in the ne. mal operating band and the ;

l alarm clearing when the level was either high or low. The F012 valve was (continued);

i 4

7 8 9 33 STA S

'. POW ER OTHER STATUS 015 0 RY DISCOVERY DESCRIPTION lE @ l 0] 8l 6l@l NA l

l A lgl System Alarm l

i 5

  • 8 80 CO'OrENT AC rivi ty RELE ASED CF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE NA l

l NA l

y y @ l Zlgl 8

PERSaw'Et e xposMES e

w*. F E H tvPE D E SCRIPTION NA l

l0l0l0l@lZl@l i

7 so PERscNNE t iN;uNics oEsCniPrioNh wa. men NA 0l0l0l@l l

i

/

d

'I il 12 80 LOM OF OH DAMALE 10 F ACILerv

'g-NA I.)s /3 560 i

TYPE DE SG Hip glgq lZi@l i

,o P1)HL tt' liv 79112104 4 NRC USE ONW I T l l N l@otscRiPrio~

mee n NA g

[; ;; ;;; 9 l 9 9 ; l, l

'J I"

GB 69 su

)

NAME OF PREPARER PHONE:

LER CONTINUATION - RO# 2-79-82 Facility: BSEP Unit #2 Event Date:

10-19-79 inspected and cycled four times with proper operation noted each time. The annunciator card was replaced with one using correct logic for this applica-tion. Controls will be developed to ensure annunciator cards with the proper logic configuration are always used. All I&C personnel will review this LER with emphasis placed on the proper use of electronic components for their intended application. All Operations personnel will review this LER with emphasis on using available instrumentation during normal and special (PT's, etc.) operation and not relying on alarms. An EWR will be prepared to have plant Engineering investigate the reasons for F012 not going fully shut on all occasions.

13/S

$61 e