ML19254D001
| ML19254D001 | |
| Person / Time | |
|---|---|
| Site: | Summer |
| Issue date: | 09/27/1979 |
| From: | James O'Reilly NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Mary Johnson SOUTH CAROLINA ELECTRIC & GAS CO. |
| References | |
| NUDOCS 7910190271 | |
| Download: ML19254D001 (2) | |
Text
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'o UNITED STATES 8
NUCLEAR REGULATORY COMMISSION o
g c
REGION ll b[
o, 101 MARIETTA GT N.W., SUITE 3100 g
o ATLANTA, GEORGIA 30303 In Reply Refer To:
SEP 2 71979 II:JPO.
5 0- 3 9 5__.'
South Carolina Electric and Gas Company Attn:
M. C. Johnson, Vice President Special Services and Purchasing P. O. Box 764 Columbia, South Carolina 29218 Gentlemen:
The enclosed Bulletin 79-24 is forwarded to you for action. Written responses are required.
If you desire additional information regarding this matter, please contact this office.
Cincerely, James P. O'Reill Director
Enclosure:
1.
Designated Applicants for Operating Licenses f
I e
g
SEP 2 71979 South Carolina Electric and Gas Company.
cc w/ encl:
T. B. Conners, Jr.
Conners, Moore and Corber 1747 Pennsylvania Avenue, N.W.
Washington, D.C.
20006 A. A. Smith Quality Assurance Post Office Box 8 Jenkinsville, South Carolina 29065 O. S. Bradham, Manager Nuclear Operations Post Office Box 8 Jenkinsville, South Carolina 29065 1i90 037
/
Accession No. 7908220114 SSINS No:
6820 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASH 1? TON, D.C.
20555 September 27, 1979 IE Bulletin No. 79-24 FR0 ZEN LINES Summa ry:
On January 3, 1979, an unusual event occurred at Davis-Besse, Unit 1.
The event involved the freezing of the water in a portion of the high pressure coolant injection (HPCI) system recirculation line that is common to both high pressure coolant injection pumps. The line was not thawed until Januarr 5,1979, and the event was not reported to NRC until March 12, 1979.
In addition, over the past five years, there have been several events involving frozen instrument and sampling lines.
Description of Circumstances:
The condition was discovered on January 3, 1979, while the reactor was operating at approximately 96 percent power. During a monthly surveillance test of the HPCI pumps, there was no flow through the recirculation line from the pump discharge to the Borated Water Storage Tank (BWST).
Investigation revealed that water in a portion of the line exposed to the outside weather was frozen.
This portion of the line to the BWST is common to both HPCI pumps.
The line has redundant heat tracing (a heated wire to prevent freezing); it is insulated; and it has a low-temperature alarm system to warn of freezing conditions.
Water in the line froze apparently because of prolonged sub-freezing temperatures and a defect in the insulation. There was no apparent malfunction of the heat tracing or temperature alarm circuits, although he temperature sensing elements are located in an area not exposed to the coldest temperature conditions.
This recirculation line serves two purposes: One is to provide a flow path for surveillance testing, and the other is to provide a minimum flow path to prevent possible damage to the pump in the event it is operated against a closed discharge valve or a reactor coolant system pressure greater than the maximum discharge pressure of the pump (approximately 1600 psig).
In the initial review of the event on January 3,1979, the licensee concluded that the pumps were still Operable with +'- -- '
no immediate action was taken to thaw the January 5,1979, the line was thawed and was successfully completed.
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