ML19253C196

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Forwards IE Info Notice 79-27, Steam Generator Tube Ruptures at Two PWR Plants. No Response Required
ML19253C196
Person / Time
Site: Grand Gulf  
Issue date: 11/16/1979
From: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Stampley N
MISSISSIPPI POWER & LIGHT CO.
References
NUDOCS 7911300136
Download: ML19253C196 (2)


Text

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'o, UNITED STATES NUCLEAR REGULATORY COMMISSION

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.E REGION li ih I 101 MARIETTA ST., N.W., SUITE 3100

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o ATLANTA, GEORGIA 30303 In Reply Refer To:

50- 16 Mississippi Power and Light Company Attn:

N. L. Stampley Vice President of Production P. O.

Box 1640 Jackson, Miss.ssippi 39205 Gentlemen:

The enclosed IE Information Notice No. 79-27 provides information with regard to the sequence of events that followed incidents involving steam generator tube ruptures at two PWR units.

Sincerely, 3

C~ *' 74 ~ ~

James P. O'Reill [s Director

Enclosures:

1.

IE Information Notice No. 79-27 2.

List of IE Information Notices Issued in the Last Six Months

)hk 79113001 3 6

NOV 161979 Mississippi Power and Light Company cc w/ encl:

C. K. McCoy Plant Manager Post Office Box 756 Port Gibson, Mississippi 39150

SSINS No.:

6870 Accession No.:

7910250488 UNITED STATES NUCI. EAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON D.C.

20555 Novembe* 16, 1979 IE Information Notice No. 79-27 STEAM GENERATOR TUBE RUPTURES AT TWO PWR PLANTS Description of Circumstances:

In recent months two incidents involving steam generator tube ruptures have occurred.

In both instances, the units were cooled down and placed in the residual heat removal mode with existing procedures.

s Event of June 25, 1979, at the Doel 2 Nuclear Power Plant in Belgium The first event occurred on June 25, 1979, at the Doel 2 nuclear power plant in Belgium.

The Doel unit is a 390 Mwe Westinghouse two-loop reactor.

The event consisted of a rupture of reveral tubes in the loop B steam generator. The resultant leakage between the primary and secondary systems was estimated to be 125 gpm.

The event started when the plant was heated up after a shutdown caused by a malfunction of the main steam isolation valve. At the time of the incident the primary coolant pressure was 2233 psi and the temperature 491 F.

The reactor remained subcritical throughout the event.

The first indication of abnormal behavior was a rapid decrease of the primary system pressure (approximately:

28 psi / min.).

This was followed by the sequence of events listed below:

Time, min.

1.

Increase of charging flow demand, charging pump.

2.

Automatic isolation of the CVCS 1 DUPLICATE DOCUMEN" 7

3.

Shut off of the pressurizer heate Entire document previously pressurizer.

entered into system under:

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of pages:

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